ENS 50116
ENS Event | |
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23:20 May 15, 2014 | |
Title | Unit 1 and Unit 2 Emergency Diesel Generators Start and Load Due to Loss of One 34.5Kv Line |
Event Description | On 5-15-2014 at 1920 hours0.0222 days <br />0.533 hours <br />0.00317 weeks <br />7.3056e-4 months <br /> [EDT], with Unit 1 & 2 operating at 100% power, the North Anna 34.5 kV Bus 5, offsite power feed to the 'C' Reserve Station Service Transformer, was lost which resulted in the loss of power to the Unit 1 'H' Emergency Bus and the Unit 2 'J' Emergency Bus. As a result of the power loss, the 1H Emergency Diesel Generator and the 2J Emergency Diesel Generator automatically started as designed and restored power to the associated emergency bus. During this event, the Unit 2 'A' Charging Pump, 2-CH-P-1A, automatically started as designed due to the loss of power event.
The valid actuation of these ESF [Engineered Safety Feature] components due to the loss of electrical power is reportable per 10 CFR 50.72 (b)(3)(iv)(A). The Unit 1 'H' Emergency Bus off-site power source was restored to service and the 1H Emergency Diesel Generator was secured and returned to automatic. The Unit 1 Action Statement of Technical Specification 3.8.1 was cleared at 2115 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.047575e-4 months <br /> on 5-15-2014. The Unit 2 'J' Emergency Bus power feed continues to be from the 2J Emergency Diesel Generator and this line-up will remain until the off-site power source can be restored to operable status. The Unit 2 'A' Charging Pump has been secured and returned to automatic. Both Units are in a stable condition. An investigation is underway to determine the cause of the 34.5 kV Bus 5 loss of power. Power was returned to the Unit 1 'H' Emergency Bus via the Unit 1 'B' Reserve Station Service Transformer. The licensee will be notifying local Louisa County officials and has notified the NRC Resident Inspector. |
Where | |
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North Anna Virginia (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.17 h-0.00708 days <br />-0.00101 weeks <br />-2.32866e-4 months <br />) | |
Opened: | Page Kemp 23:10 May 15, 2014 |
NRC Officer: | Howie Crouch |
Last Updated: | May 15, 2014 |
50116 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (96 %) |
WEEKMONTHYEARENS 558432022-04-14T13:28:00014 April 2022 13:28:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Control Rod Testing ENS 535792018-09-03T04:00:0003 September 2018 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Start of the Emergency Diesel Generator ENS 518922016-04-30T02:14:00030 April 2016 02:14:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Offsite Power to the a Reserve Station Service Transformer ENS 516782016-01-23T22:03:00023 January 2016 22:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Partial Loss of Power Results in Emergency Diesel Generators Starting ENS 509462015-04-02T08:26:0002 April 2015 08:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Main Generator Voltage Regulator Failure ENS 508512015-02-26T20:11:00026 February 2015 20:11:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Feedwater Regulating Valve Failing Closed ENS 501162014-05-15T23:20:00015 May 2014 23:20:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 and Unit 2 Emergency Diesel Generators Start and Load Due to Loss of One 34.5Kv Line ENS 497842014-02-02T13:59:0002 February 2014 13:59:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Following Loss of the "a" Main Feedwater Pump ENS 494292013-10-11T17:17:00011 October 2013 17:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Turbine and Reactor Trip Due to Station Service Transformer Lockout ENS 490752013-05-28T19:07:00028 May 2013 19:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to a Feedwater Transient ENS 490202013-05-10T10:12:00010 May 2013 10:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to High Turbine Bearing Vibration ENS 484362012-10-24T05:47:00024 October 2012 05:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Steam Generator Water Level ENS 460202010-06-16T23:20:00016 June 2010 23:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Lightning Storm ENS 459602010-05-28T04:03:00028 May 2010 04:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Reactor Coolant Pump ENS 458772010-04-27T20:37:00027 April 2010 20:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Following a Generator Lockout During Automatic Voltage Regulator Testing ENS 455562009-12-09T19:23:0009 December 2009 19:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Unit 2 and Edg Start on Both Units Due to Inadvertent Loss of "C" Reserve Station Service Transformer ENS 450262009-04-28T13:53:00028 April 2009 13:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Auto-Start Due to Loss of the "B" Reserve Station Service Transformer ENS 439722008-02-08T23:12:0008 February 2008 23:12:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Control Rod Position Deviation ENS 438662007-12-26T02:10:00026 December 2007 02:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Trip of "B" Reactor Coolant Pump ENS 434622007-06-29T21:52:00029 June 2007 21:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Reactor Trip and Spurious Safety Injection ENS 432172007-03-07T08:05:0007 March 2007 08:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Autostart on Loss of "B" Reserve Station Service Transformer ENS 430722007-01-03T23:03:0003 January 2007 23:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Card Failure ENS 429962006-11-16T07:26:00016 November 2006 07:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip ENS 424832006-04-08T02:31:0008 April 2006 02:31:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Group Step Counter Failure During Reactor Startup ENS 418982005-08-06T02:28:0006 August 2005 02:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Apparently Due to Lightning Strike ENS 408042004-06-10T17:13:00010 June 2004 17:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip While Performing Scheduled Solid State Protection Testing ENS 407842004-05-29T06:02:00029 May 2004 06:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Control Rod Position Indication Failure During Hot Rod Drop Test 2022-04-14T13:28:00 | |