ENS 42996
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ENS Event | |
---|---|
07:26 Nov 16, 2006 | |
Title | |
Event Description | At 0226, North Anna Power Station Unit 2 automatically tripped on steam flow greater than feed flow with low steam generator water level on 'B' Steam Generator. This was caused by a Steam Flow Channel (Channel 3) Low failure. After the reactor trip, Auxiliary Feedwater Pumps automatically started on Low-Low Steam Generator Level.
All control rods fully inserted. RCPs are in operation transferring decay heat to the steam generators. The steam generators are discharging steam to the main condenser using the condenser steam dumps. Main feedwater pumps are running to maintain steam generator water levels. Unit 1 was not affected. The licensee will notify the NRC Resident Inspector. |
Where | |
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North Anna Virginia (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-3.48 h-0.145 days <br />-0.0207 weeks <br />-0.00477 months <br />) | |
Opened: | James Johnstone 03:57 Nov 16, 2006 |
NRC Officer: | Bill Gott |
Last Updated: | Nov 16, 2006 |
42996 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
North Anna with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 571482024-05-29T10:24:00029 May 2024 10:24:00
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ECCS Discharge Reactor Trip and Spurious Safety Injection ENS 432172007-03-07T08:05:0007 March 2007 08:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Autostart on Loss of "B" Reserve Station Service Transformer ENS 430722007-01-03T23:03:0003 January 2007 23:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Card Failure ENS 429962006-11-16T07:26:00016 November 2006 07:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip ENS 424832006-04-08T02:31:0008 April 2006 02:31:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Group Step Counter Failure During Reactor Startup ENS 418982005-08-06T02:28:0006 August 2005 02:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Apparently Due to Lightning Strike ENS 408042004-06-10T17:13:00010 June 2004 17:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip While Performing Scheduled Solid State Protection Testing ENS 407842004-05-29T06:02:00029 May 2004 06:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Control Rod Position Indication Failure During Hot Rod Drop Test 2024-05-29T10:24:00 | |
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