ENS 45726
ENS Event | |
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19:18 Feb 25, 2010 | |
Title | Invalid Actuation of Containment Isolation Valves |
Event Description | This 60-day notification is being made in accordance with 10 CFR 50.73(a)(1), which states that in case of an invalid actuation reported under 10 CFR 50.73(a)(2)(iv)(A), other than the actuation of the Reactor Protection System (RPS) when the reactor is critical, the licensee may provide a telephone notification to the NRC within 60 days after discovery of the event instead of submitting a written LER. Because plant conditions necessary to prompt a containment isolation were not present, this event constitutes an invalid system actuation under 10 CFR 50.73(a)(2)(iv)(A). The condition meets the criteria of 10 CFR 50.73(a)(2)(iv)(B)(2) because the loss of the Unit 1 'B' RPS bus affected containment isolation valves in more than one system.
On 1/4/2010 at 1418 hours0.0164 days <br />0.394 hours <br />0.00234 weeks <br />5.39549e-4 months <br />, the Unit 1 'B' RPS bus was lost. This event resulted in a half scram and primary containment isolations. By design, when the RPS MG set output breaker trips, all EPA breakers downstream of the MG set also trip resulting in a half scram and primary containment isolation signals. An event investigation found the Unit 1 'B' RPS MG set running with its output breaker tripped. The output voltage was indicating 120VAC, which indicates that the voltage regulator was operating properly. Upon removal of the MG set cover, the underfrequency relay (UFR) contacts were found to be chattering, with frequency steady at approximately 60 Hz. A review of plant drawings indicated that a chattering UFR could cause the MG set output breaker to trip. Voltage readings were taken and no additional electrical problems (other than the UFR) were identified. The affected RPS loads were subsequently powered from their alternate source and all actuations and isolations were reset. Inspection and test of the failed UFR found that one leg of a capacitor on the UFR electronic board had broken adjacent to its solder joint connection on the board. It is suspected that the capacitor lead may have been flawed during manufacture of the board. The failure was accelerated by the constant vibration that the connection is subjected to, as the UFR is mounted on the MG set. The failed UFR electronic board was subsequently replaced and successfully passed all functional tests. There were no actual safety consequences associated with this event. Valves affected by the invalid signal fulfilled their isolation function by successfully closing. The RPS loads were transferred to their alternate power supply and the trips and isolations were reset. In addition, the Unit 1 'B' RPS bus did not experience an underfrequency condition. The licensee has notified the NRC Resident Inspector. |
Where | |
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Susquehanna Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+-2.97 h-0.124 days <br />-0.0177 weeks <br />-0.00407 months <br />) | |
Opened: | David Borger 16:20 Feb 25, 2010 |
NRC Officer: | John Knoke |
Last Updated: | Feb 25, 2010 |
45726 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (94 %) |
After | Power Operation (94 %) |
Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (94 %) |
After | Power Operation (94 %) |
WEEKMONTHYEARENS 541032019-04-18T05:10:00018 April 2019 05:10:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification Due to Invalid Specified System Actuation ENS 527722017-04-03T01:27:0003 April 2017 01:27:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid Specified System Actuation ENS 480922012-05-14T13:28:00014 May 2012 13:28:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Emergency Service Water Actuation ENS 457262010-02-25T19:18:00025 February 2010 19:18:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 435552007-06-09T09:11:0009 June 2007 09:11:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of the 'C' Emergency Diesel Generator ENS 424892006-03-11T09:32:00011 March 2006 09:32:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 407662004-04-04T18:57:0004 April 2004 18:57:00 10 CFR 50.73(a)(1), Submit an LER 60 -Day Report: Invalid Actuation of the "E" Emergency Diesel Generator ENS 407332004-03-21T16:32:00021 March 2004 16:32:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Signals in More than One System ENS 401732003-08-29T14:25:00029 August 2003 14:25:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves 2019-04-18T05:10:00 | |