05000346/FIN-2016001-06
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Finding | |
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Title | Less than Adequate Procedural Instructions for Restoring Main Feedwater Following a Reactor Trip |
Description | A self-revealed finding of very low safety significance (Green), and an associated NCV of TS 5.4.1(a) were identified for the licensees failure to establish and implement adequate procedural guidance for restoring MFW following a reactor trip. Specifically, the guidance in licensee procedure DBOP06910, Trip Recovery Procedure, for restoring MFW to the SGs using the motor-driven feedwater pump (MDFP) did not ensure that the MFW piping had been sufficiently re-pressurized prior to opening the MFW to SG isolation valves. This lack of satisfactory procedural guidance allowed control room operators to prematurely open the MFW to SG No. 1 isolation valve, which resulted in a SFRCS actuation on the reverse delta pressure (P) function. This issue was entered into the licensees CAP. Corrective actions planned by the licensee included changes to licensee procedure DBOP06910, Trip Recovery Procedure, to ensure that MFW header pressure is greater that SG pressure prior to opening the MFW to SG isolation valves. This finding was of more than minor safety significance because it affected the design control and procedure quality attributes of the Mitigating Systems cornerstone of reactor safety, and adversely impacted the cornerstone objective of ensuring the availability, reliability, and capability of the units MFW system and main condenser for decay heat removal. The finding was determined to be of very low safety significance based on the results of a detailed risk evaluation conducted by the NRC Region III Senior Reactor Analyst (SRA). The inspectors determined that the finding had a cross-cutting aspect in the area of human performance. The inspectors assigned the cross-cutting aspect of Resources to the finding because the licensee had failed to ensure that the procedural instructions and guidance available to plant operators restoring MFW during reactor trip recovery actions took into account all relevant technical details (e.g., the differences between MFW piping runs, the amount of time needed to re-pressurize MFW piping, etc.) |
Site: | Davis Besse |
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Report | IR 05000346/2016001 Section 4OA3 |
Date counted | Mar 31, 2016 (2016Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | D Kimble J Cameron T Briley L Alvaredo |
Violation of: | Technical Specification - Procedures Technical Specification |
CCA | H.1, Resources |
INPO aspect | LA.1 |
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Finding - Davis Besse - IR 05000346/2016001 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Davis Besse) @ 2016Q1
Self-Identified List (Davis Besse)
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