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 Start dateReporting criterionEvent description
05000390/LER-2011-0019 May 201110 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On May 9, 2011 at 15:17 Eastern Standard Time (EST) with Watts Bar Nuclear Plant, Unit 1 in Mode 5, and the Reactor Coolant System (RCS) in a near water solid condition, the licensed operator started Safety Injection Pump 1A-A (SIP 1A-A) to fill and vent the Cold Leg Accumulators (CLAs) in accordance with System Operating Instruction SOI- 63.01. Following startup of SIP 1A-A, RCS pressure immediately began to rise and reached a maximum pressure of 328 psig before the operators secured the pump. The RCS pressure transient during this event did not exceed the Cold Overpressure Mitigation System (COMS) setpoint. The unexpected pressure transient was due to improper alignment of the Safety Injection System (SIS) when used to fill and vent the CLAs. Specifically, SIP 1A-A Crosstie Valve (1-FCV-63-152) was opened when it should have been closed. Misalignment of the SIS was due to a failure to follow procedures for a temporary clearance lift.

LCO 3.4.12 was not met because a SIP was capable of injecting into the RCS in Mode 5, which is reportable as a condition prohibited by Technical Specifications in accordance with 10 CFR 50.73(a)(2)(i)(B).

05000390/LER-2009-00127 May 200910 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On 5/27/09, TVA identified that the Watts Bar Nuclear Plant (WBN) Unit 1 Auxiliary Building (AB) Gas Treatment System (ABGTS) pressure test surveillance instruction was inadequate, as closed nonsafety related dampers could mask leakage through credited safety related dampers in the AB Secondary Containment Enclosure (ABSCE).

AB General Ventilation manipulation to place WBN in a known tested condition created a pressure differential that caused failure of temporary ABSCE boundary doors installed to facilitate Unit 2 construction. WBN entered LCO 3.7.12 Condition B for 2 trains of ABGTS inoperable. WA repaired the boundary, and the LCO Condition was exited in approximately 3.5 hours.

Subsequently, WA retested ABGTS, and both trains were verified as operable. From initial licensing until 5/27/09, WBN operated in noncompliance with TS because of the inadequate surveillance instruction.

On 6/27/09, another AB General Ventilation manipulation created a pressure differential that caused the temporary doors to fail once again. One temporary door and a permanent steel door are now closed to ensure boundary operability.

Failures of the temporary doors were due to an inadequate design and insufficient interim actions after the first event to prevent another failure. This event is reported in accordance with 10 CFR 50.73 (a)(2)(i)(B) and (a)(2)(v)(C) and (D).

05000390/LER-2008-00529 October 200810 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On October 29, 2008, a discrepancy in the setpoint of the particulate channel of the radiation monitor being credited for meeting Technical Specification (TS) 3.4.15 was identified and the appropriate Limiting Condition for Operation (LCO) was entered. On October 14, the radiation monitor had been calibrated to a setpoint that was no longer within the specified tolerance as a result of a design change. From October 14 to October 29, the Reactor Coolant System Leakage Detection System had been inoperable due to this incorrect setpoint. Consequently, WBN had been operating in a condition prohibited by Technical Specifications.

The cause of this event was determined to be a human performance error during the preparation of design change impact forms. An insufficient level of Question, Validate, and Verify (QV&V) was used, and self-checking was flawed by a wrong assumption regarding design change scope. The setpoint was corrected October 30.

05000390/LER-2008-00420 September 200810 CFR 50.73(a)(2)(iv)(A), System Actuation

During normal plant operation on September 20, 2008, unexpected annunciator alarms were received in the control room indicating an automatic reactor trip based on a loss of electrical load. Subsequently, the control room was informed by a Nuclear Assistant Unit Operator that he had tripped open the Exciter Field Breaker, leading to the turbine trip and successive reactor trip.

The cause of this event has been determined to be human performance error in that the NAUO failed to recognize the need to utilize error reduction techniques when opening the exciter field breaker cabinet door. Corrective action has been taken to add the applicable information to operator requalification programs.

As a result of the plant trip, the actuation of the Reactor Protection and the Auxiliary Feedwater Systems were reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), respectively, as ENS notification 44506. This event is also being reported as this Licensee Event Report in accordance with 10 CFR 50.73(a)(2)(iv)(A).

05000390/LER-2008-0037 August 200810 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

NRC Inspection Report 05000390 identified in a noncited violation (NCV) that WA started Watts Bar Nuclear Plant (WBN) Unit 1 since initial plant startup without an operable channel of auxiliary feedwater (AFW) automatic start on a trip of all main feedwater pumps as required by Technical Specification (TS) 3.3.2 Function 6.e. The NCV finding was determined to be of very low safety significance because the finding did not represent an actual loss of safety function of a single train for greater than its TS allowed outage time since other initiation signals were available to automatically start the auxiliary feedwater pumps if needed.

With this inspection report, NRC clarified that the instrumentation channels must not only be capable of transmitting a trip signal, but must also reflect the actual operating condition of the main feedwater pump.

WA has submitted a TS change to permit operation without the AFW autostart on trip of all main feedwater pumps until a main feedwater pump is actually providing feedwater flow to the steam generators. Until operation in accordance with the revised TS is approved, WA will startup using all three AFW pumps, which will eliminate the need for the autostart, since the signal would be to start the pumps that are already running.

05000390/LER-2008-00120 March 200810 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Jumpers installed near the beginning of the Cycle 8 refueling outage to block automatic actuation of Safety Injection (Auto SI) had not been removed when Mode 4 was achieved at 0020 EDT on March 20, 2008, or when Mode 3 was entered at 0100 EDT on March 21, 2008. At 0913 EDT on March 21, 2008, plant personnel identified that the jumpers installed during the outage had not been removed. The Auto SI function is required in Modes 1, 2, 3, and 4 per Function 1.b of Table 3.3.2-1 of LCO 3.3.2. Since both trains of Auto SI actuation instrumentation were inoperable, LCO 3.0.3 was entered until jumpers were removed at 0958 EDT. At 2133 EDT on March 21, 2008, it was identified that the Auto SI function was still inoperable because the Auto SI function had not been reset. The reactor trip breakers were cycled to reset Auto SI and LCO 3.0.3 exited at 2206 EDT. Safety consequences of this event were not significant for the existing plant conditions. The cause assessment for the event identified an inadequate General Operating (GO) Instruction and an inadequate Instrument Maintenance Instruction (IMI). The corrective actions include revisions to selected GOs, the IMI, and establishment of a jumper tracking program.
05000390/LER-2006-00510 CFR 50.73(a)(2)(iv), System Actuation

On July 31, 2006, at approximately 12:13 EDT, the control room unexpectedly received an exciter field overcurrent alarm, followed immediately thereafter ( An event team was assembled subsequent to the plant trip. The most likely cause was determined to be in the main generator automatic excitation control circuitry. Corrective action taken was to retum the plant to service while monitoring several input and output signals associated with the automatic controls so that any subsequent events could be captured and analyzed. The excitation system would also be operated in TEST mode instead of AUTOMATIC to preclude the possibility of an additional plant trip.

Since restarting the plant, there have been several instances where the output of the Maximum Excitation Limiter (MXL) circuit board in the automatic excitation control circuitry has changed significantly (+14 volts dc to -15 volts dc) with no corresponding change on any of the inputs. Had the automatic circuit been in service, the MXL output change would have driven the excitation controls into a loss of the exciter field which was the case during the plant trip. Based on this data, during the current refueling outage, the MXL circuit board will be removed to determine if a discreet component on the device has failed and an inspection performed of the interface wiring to the MXL circuit board to determine if degraded wiring caused the failure.

As a result of the plant trip, the actuation of the Reactor Protection and the Auxiliary Feedwater Systems were reported in accordance with 10 CFR 50.72(b)(2)(iv) and 10 CFR 50.72(b)(3)(iv), respectively. This event is also being reported as this Licensee Event Report in accordance with 10 CFR 50.73 (a)(2)(iv).

05000390/LER-2006-002

On January 27, 2006, engineering personnel identified a scenario involving a potential loss of cooling water to the Chemical and Volume Control System (CVCS) Seal Water Heat Exchanger during an Appendix R fire event. The scenario involves a loss of Component Cooling System (CCS) flow to the Seal Water Heat Exchanger due to fire damage. The loss of CCS flow results in a potential high suction temperature on the running CVCS Centrifugal Charging Pump (CCP) causing a loss of adequate suction head. During an Appendix R fire event, CCP suction is aligned to the Refueling Water Storage Tank (RWST), normal charging and letdown are isolated and the only makeup flow to Reactor COolant System (RCS) is via the Reactor Coolant Pump (RCP) seal injection flow path. If the Seal Water Heat Exchanger cooling is lost, the CCP recirculation flow and RCP seal return flow are not being cooled. The outlet of the heat exchanger combines with cool water from the RWST. The net result is that the CCP suction temperature could reach saturation temperature leading to pump cavitation. The temperature increase could be h gh enough to potentially damage both the CCP and the RCP seals, which would result in increased seal leakage and a potential loss of RCS inventory.

The cause of this event is a latent error in the WBN Fire Safe Shutdown Analysis. The original analysis did not evaluate the ramifications of not protecting cooling water flow to the CVCS Seal Water Heat Exchanger. Corrective actions include: 1) posting of roving fire watches in the areas affected, 2) procedure revisions to provide operator actions and 3) to issue a design change to reroute andor protect the identified vulnerable cables.

0NRC FORM 366 (6-2004) PRINTED ON REC"CLED PAPER

05000390/LER-2003-00610 CFR 50.73(a)(2)(i)

On October 21, 2003, WBN Unit I was returning to service after completion of the Cycle 5 refueling outage. The unit was in Mode 1 at approximately 36% reactor power, when it was established that 6.9KV Shutdown Board breaker, 1-BKR-72-10, was not connected and was not capable of supplying power to the Containment Spray System (CSS) Pump 1B-B. In accordance with LCO 3.6.6, "CSS," Pump 1B-9 is required to be operable In Mode 4.

The restoration of the breaker should have been performed in accordance with Section 5.2.8 of General Operating (GO) Instruction 1, "Unit Startup from Cold Shutdown to Hot Standby," and verified in accordance with Step 6 of Appendix B, 'Wade 5-to-Mode 4 Review and Approval," of GO-1. Due to the CSS pump not being operable as the unit transitioned from Mode 5 to Mode i, the mode change restrictions of LCO 3.0.4 were not met. The total time CSS Pump 1B-B was inoperable was approximately 113.6 hours. Considering this, Action A of LCO 3.6.6, "CSS," requires that an inoperable CSS train be restored within 72 hours. When this action is not met, Action C.1 requires that the Unit be in Mode 3 in 6 hours. Neither of these actions were met. The failure to comply with the requirements of LCO 3.0.4 and LCO 3.6.6 is being reported as a violation of the Technical Specifications in accordance with 10 CFR 50.73 (a)(2)(i)(B).

NRC FORM 26t3 (7.2001)

05000390/LER-2003-00510 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material

On October 3, 2003, Watts Bar Nuclear Plant Unit 1 was in Mode 6 during a refueling outage with core re-load in progress. At 1516 hrs (EDT), main control room personnel became aware that an activity involved with an upcoming test had inappropriately placed the B-Train Auxiliary Building Gas Treatment System (ABGTS) Exhaust Fan 460v breaker in the OPEN position. An operator was immediately dispatched and the breaker was closed at 1521 hrs, restoring the train to OPERABLE status. The opening of this breaker at about 1324 hrs caused the B ABGTS train to be INOPERABLE at a time when the A-train ABGTS was available to start but technically inoperable due to an unavailable emergency power supply (2A-A Emergency Diesel Generator). The ABGTS system is required for the mitigation of a postulated fuel handling accident. The immediate cause of the event was human error by a shift test director who did not realize the A-Train ABGTS was inoperable when he directed opening the subject breaker in support of equipment alignments for the upcoming test. Corrective actions include counseling of involved individuals on their awareness of plant conditions and need for adequate communications and adding a separate item to the Outage Schedule for preliminary alignments for 18 Month Blackout tests.

The safety significance of this event was low. � in an actual FHA, performance of site emergency procedures would have detected and quickly restored ABGTS Train B. Further, with off site power available, ABGTS Train A would have immediately responded to an event. Dose consequences assuming loss of all ABGTS were determined to remain with regulatory limits.

NRC FORM 368 (7

  • 200il
05000390/LER-2003-00310 CFR 50.73(a)(2)(iv)(A), System Actuation

On August 25, 2003, Watts Bar (WBN) Unit 1 was operating at 100 percent power when there was an operation of the 2 out of 3 logic for the Sudden Pressure Relays (SPRs) for Main Transformer Bank 1C. The actuation of the relays resulted in a turbine trip and a subsequent reactor trip at approximately 0945 EDT. All control rods inserted as required and the safety systems actuated as designed including the motor and turbine driven pumps for the Auxiliary Feedwater (AFW) System. AFW pump 1B-8 was available but not operable at the time of the trip due to work on an associated penetration room cooler. The pump started as required. There was no loss of safety function. Unit 1 was stabilized in Mode 3.

The immediate cause of the trip was the actuation of the SPRs which were initiated by a worker bumping into the junction box that houses the relays in the switchyard. Subsequent to this, it was identified that the design of the SPA configuration was sensitive to actuation when force was applied to the relay housing junction box.

Corrective actions include a modification to improve the vibration isolation of the SPRs and the installation of a permanent protective barrier fence with access gate around each of the four SPRs, pipe, hydraulic hose, junction box, and support installations to prevent accidental impact during normal plant operations. Trip hazard signs have been placed on the fence barrier.

ARC FORM 355 (7.200 r) i NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION

05000390/LER-2003-00210 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On May 21, 2003, WBN Unit 1 was operating at 100 percent reactor power. At approximately 2153 EDT, the WBN operators were alerted to potential instrument channel III trouble when control room alarms were received. � This equipment provides channel III process instrumentation of the engineered safety features actuation subsystem portion of the Reactor Protection System. The operators were able to clear the alarms and plant continued operation. However, throughout the early morning of May 22, 2003, alarms indicating the same trouble continued.

Maintenance personnel performed troubleshooting and identified that a faulty power distribution panel located within Reactor Protection Set Channel III, Panel 1-R-9 was the source of the problem. The faulty power distribution panel was replaced and Panel 1-R-9 was returned to service.

Throughout this event, the operators did not identify Panel 1-R-9 as inoperable since after clearing the alarms, plant parameters were within range (with an exception of entry into LCO 3.4.1 "RCS Pressure, Temperature, and Flow DNB Limits due to reactor coolant pressure less than 2214 for a short period) and plant operation continued. � However, it was concluded after the event that the panel should have been declared inoperable and Technical Specifications actions completed within the 6 hour time requirements. This event is being reported under 10 CFR 50.73 (a)(2)(i)(B) as operation prohibited plant technical specifications.

The cause for this event was that there was no specific guidance to assist the operators In diagnosing a panel malfunction of the sort that would also affect operability of the Reactor Protection System panel. � Corrective actions include the development of an Abnormal Operating Procedure to address panel malfunctions. Additionally, the initial maintenance troubleshooting activities identified the problem to be in the data link handler portion of the rack which would not affect operability.

05000390/LER-2003-00110 CFR 50.73(a)(2)(iv)(A), System Actuation

On March 10, 2003, at 0012 Eastern Standard Time, with Watts Bar 1 at 100 percent power, a Generator Backup Relay unexpectedly actuated causing an automatic turbine/reactor trip. The relay actuated due to a ground fault caused by a broken o-ring in the C phase main transformer's high side bushing capacitance tap connector. Plant safety equipment performed as designed which included the auto-start of the auxiliary feedwater system.

The root cause of this event was inadequate preventive maintenance procedure. Corrective actions include repairing the connector, revising preventative maintenance (PM) procedures, and a design change to the affected single point vulnerability relay scheme.

05000390/LER-2002-00527 September 2002

At 0824 EDT on September 27, 2002, Watts Bar Nuclear Plant (WBN) Unit 1 was operating at 100% power when 6.9 kV shutdown logic board panel 1A-A load stripping relay actuated. At 0842 EDT, the 6.9 kV shutdown logic board panel 1B-B load stripping relay actuated. These actuations occurred due to a loss of both offsite power lines which resulted in an automatic start and loading of both trains of Emergency Diesel Generators. At 0852 EDT, WBN declared a notification of unusual event (NOUE) due to the loss of both offsite power sources which resulted from a fire at the Watts Bar Hydroelectric Generating Plant (WBH). The WBN fire brigade was dispatched to fight the fire and remained there until the fire was extinguished. Since the brigade remained at the fire location and callout of additional brigade staffing took greater than two hours, 10 CFR 50.54(x) was invoked to address this departure from the minimum fire brigade staffing requirement of the WBN Fire Protection Report. WBN remained at 100% power with all four emergency diesel generators operating throughout the event. Offsite power was restored using an interim offsite configuration from Sequoyah and Rockwood lines. TVA evaluated and determined this configuration to be a Generic Letter (GL) 91-18 non-conforming condition that supports functionality and operability of both 161 kV preferred power sources per GDC 17. Condition D of LCO 3.8.1 was exited at 0125 EDT on September 28, 2002, when the first qualified offsite source was returned to service. WBN remained in Condition A of LCO 3.8.1 until the second qualified offsite source was returned to service at 0300 EDT. The NOUE was exited at 0308 EDT on September 28, 2002.

F RN1 "-2001

05000390/LER-2002-00410 CFR 50.73(a)(2)(iv)(A), System ActuationWhile operating at 100% power on September 21, 2002, Watts Bar Unit 1 experienced a momentary loss of the 161 kV offsite power feed to Common Station Service Transformer (CSST) D. WBN's two offsite power supplies are fed from a remote switchyard located at the Watts Bar hydroelectric plant. The affected offsite power source through CSST D is the primary power source for 6900V Shutdown Boards 1B-B and 2B-B. The partial loss of offsite power was caused by the inadvertent manual operation of a breaker at the hydroelectric plant switchyard. The opening of the breaker occurred at 11:00:20 (EDT) and the breaker was reset to provide offsite power at 11:00:34 (EDT). 0 Due to this event, and the loss of the primary feed to the shutdown boards, a valid engineered safety function (ESF) actuation occurred which started all four of the standby diesel generators (DGs), along with, as designed, the 1B-B Motor Driven Auxiliary Feedwater (AFW) Pump and the Turbine Driven AFW Pump. The DGs provided power to the affected Shutdown Boards and other required blackout loads during the event.
05000390/LER-2002-00313 July 200210 CFR 50.73(a)(2)(iv)(A), System Actuation

On July 13, 2002, at approximately 1622 EDT, while the plant was in Mode 1, at 100% power, Watts Bar Unit 1 experienced an automatic turbine/reactor trip when a C-Phase Main Transformer differential relay actuated This occurred because a bolted cable splice associated with a C-phase current transformer (CT) came into contact with the CT junction box; thereby shorting the differential relay protection circuit to ground.

The apparent factors contributing to this short circuit condition include temperature, cable splice material, vibration, and configuration of the splice inside the junction box.

All control rods inserted properly in response to the reactor trip. The Auxiliary Feedwater (AFW) System actuated in response to the trip, as designed. Plant response was in accordance with design with no complications. Operations shift personnel performance was in accordance with applicable procedures.

Subject to confirmatory laboratory testing, the root cause of this event was determined to be inadequate work instructions that allowed lower temperature rated tape to be used on a cable replacement and/or inadequate application of splice material. Corrective actions include revision and training on TVA's engineering and maintenance procedures for high temperature jacketing material, laboratory analysis of damaged splices, and reinspection and taping of similar vulnerable cable splices.

05000390/LER-2002-002

On March 7, 2002, while the plant was in Mode 6, an on-shift senior reactor operator discovered two inspection covers missing from the guard pipe which encapsulates the Unit 1 four inch Auxiliary Feedwater Pump Turbine (AFWPT) steam supply line where this line passes through the Unit 1 Auxiliary Building elevation 692.0 penetration room and enters into the AFWPT room. The guard pipe is used as a barrier to isolate a steam leak in case of a steam supply line rupture and vent steam into the AFWPT room where redundant temperature sensors will initiate isolation by closure of redundant valves located in the south main steam valve vault room. This guard pipe was installed primarily to prevent unacceptable damage to essential equipment located in the auxiliary building. The encapsulation serves to restrain the pipe thus preventing pipe whip and confines the steam jet. Upon initial evaluation, it was postulated that a circumferential rupture at the 90° elbow (near the area where these inspection covers were found missing), could have resulted in potentially unacceptable impact on environmental qualification of safety related equipment needed to mitigate the event. In addition to the missing covers, a penetration seal was found to be inappropriately installed in the mechanical sleeve which connects the guard pipe to the AFWPT room which may have delayed automatic isolation of the postulated rupture of the steam supply line. However, since that time, TVA has performed an extensive evaluation and determined that equipment required to mitigate the event would perform required functions.

This LER is being provided as a voluntary report.

The cause of the condition has not been identified. The condition appears to have existed since prior to initial fuel load in November of 1995. Corrective actions included fabrication and replacement of the pipe covers, removal of the penetration seal, and a confirmation review of similar configurations in the plant.

05000390/LER-2002-001

On March 1, 2002 at approximately 0258 hours, with Watts Bar Unit 1 in Mode 6 (Refueling) and RCS temperature at 100 degrees F, while attempting to realign the RHR system from RWST supply to RCS loop operation, operators isolated the common suction to the Residual Heat Removal (RHR) pumps on two occasions over a three minute span. At the time of the event, operators were performing full flow testing of ECCS lines in conjunction with reactor cavity fill.

The crew had not been briefed during shift turnover of other work activities which removed power from a rack which provided a permissive pressure switch signal to two valves which required manipulation during the realignment. The root cause of this event was inadequate work review and scheduling coupled with less than expected transfer of information, pre-job brief, and response to an emergent operating condition. Corrective actions to include: Counsel/coach individuals/groups involved, include this event in training, refine the scheduling and planning process by which work activities are tied to specific plant conditions or milestones and impacts are evaluated based on plant conditions and scheduled activities. (Voluntary Report)

05000390/LER-2001-00419 December 200110 CFR 50.73(a)(2)(iv)(A), System ActuationOn December 19, 2001, an invalid AMSAC signal was initiated that resulted in a turbine/reactor trip. The unit was operating at 100% power at the time of the event and work was in process for the placement of a clearance (tagout) to support the implementation of a design change to the control instrumentation for the Turbine Driven Auxiliary Feedwater (TDAFW) pump. The clearance activities opened the breakers which supply power to the instrumentation. The loss of power to the instruments resulted in an invalid steam generator (SG) lo lo level (12%) signal and satisfied the logic (3 out of 4 SGs less than 12% level) for the initiation of an AMSAC signal. All control rods inserted properly and the Auxiliary Feedwater (AFW) system started, as required, in response to the AMSAC signal and the reactor trip. The cause of the event was inadequate interface requirements in the planning and scheduling of trip sensitive activities along with inadequate implementation of the clearance preparation process. The corrective actions included the review of open on-line clearances, development of a standard for the tagging of low voltage equipment, establishment of a formal process which reviews plant work activities for trip sensitive actions, counseling of involved personnel, training on the lessons learned from the event, identification and labeling of trip sensitive breakers, development of an instruction to define the expectations for independent review and to provide controls for the operation and tagging of low voltage breakers.
05000390/LER-2001-00310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On September 29, 2001, a blockage in an instrument sense line was discovered. A review of computer trend data for the Watts Bar Unit 1 #4 steam generator pressure transmitter loop, determined the channel may not have performed its design function, and thus had been inoperable without being placed in the "trip" position for about 8 hours and 40 minutes longer than the 6 hour period allowed by the ESFAS technical specifications.

Although the channel had been providing the correct pressure value to the ESFAS system and the control room, the blockage had slowed the time response to pressure changes beyond the time assumed in the FSAR.

The other two channels which were part of the two out of three logic circuit were operable during the time period to provide the required signal to the ESFAS system.

The clearing of the blockage corrected the immediate cause, and recurrence control actions included : Back filling of a sampling of the main steam pressure and flow transmitters during the upcoming refueling outage, and providing information to Operations and Engineering on this event and symptoms of a sense line blockage.