05000390/FIN-2017001-03
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Finding | |
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Title | Licensee-Identified Violation |
Description | The following licensee-identified violation of NRC requirements was determined to be of very low safety significance or Severity Level IV and met the NRC Enforcement Policy criteria for being dispositioned as a non-cited violation.Watts Bar Nuclear Plant (WBN) Unit 1 Operating License Number NPF-90, condition 2.F, requires, in part, that TVA shall implement and maintain in effect all provisions of the approved Fire Protection Program as described in the Fire Protection Report for the facility, as described in NUREG-0847, Supplement 29. The WBN Fire Protection Report was developed for WBN to ensure compliance with the requirements of this licensee condition. Fire Protection Report, Part II, is the Fire Protection Plan (FPP). FPP Section 14, Fire Protection Systems and Features Operating Requirements (ORs), Subsection 14.10(b), Fire Safe Shutdown Equipment, paragraph 14.10.4, requires an hourly roving fire watch be established in auxiliary building rooms 757-A1 and 757-A10 within an hour of closure of pressurizer block valve 1-FCV-68-332-B. Contrary to the above, on January 11, 2017, the licensee failed to perform a fire watch as required for fire safe shutdown equipment. Specifically, an hourly fire watch was not established or conducted when valve 1-FCV-68-332-B was closed for WO 117615614 for 1-SI-68-93, 18 Month Channel Calibration of PORV 1-PCV-69-334 Cold Overpressure Mitigation System Actuation Channel. The licensee determined valve 1-FCV-68-332-B was closed for about 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> when it was opened to restore compliance. 25 This violation is of very low safety significance (GREEN) based on the results of the IMC 0609, Appendix F, Fire Protection Significance Determination Process, Phase I Screening Approach. The inspectors determined that this issue did not affect the Unit 1 reactors ability to reach and maintain safe shutdown (either hot or cold) condition. This violation was documented in the licensees corrective action program as CR 1250743 |
Site: | Watts Bar |
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Report | IR 05000390/2017001 Section 4OA7 |
Date counted | Mar 31, 2017 (2017Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | |
Inspectors (proximate) | A Blamey J Hamman J Jandovitz J Nadel J Seat |
Violation of: | Technical Specification |
INPO aspect | |
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Finding - Watts Bar - IR 05000390/2017001 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Watts Bar) @ 2017Q1
Self-Identified List (Watts Bar)
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