ENS 50346
ENS Event | |
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22:34 Aug 5, 2014 | |
Title | Automatic Reactor Scram |
Event Description | This notification is being provided pursuant with SAF 1.6 10CFR50.72(b)(2)(iv)(B) and SAF 1.7 10CFR50.72(b)(3)(iv)(A).
At 1734 CDT on August 5, 2014, LaSalle Unit 2 automatically scrammed due to an RPS actuation. The MSIVs isolated on a Group 1 signal, the cause is under investigation. The reactor water cleanup system isolated during the transient. The plant is stable with Reactor Pressure Control being maintained by the Reactor Core Isolation Cooling System and SRVs and level being controlled by the Low Pressure Core Spray System. The plant is planned to remain in hot shutdown pending investigation of the trip." The Unit 2 electric plant is in a normal shutdown lineup. All control rods inserted fully on the scram. Unit 1 was not affected by the Unit 2 transient. The licensee notified the NRC Resident Inspector.
The initial notification to the NRC stated that the reactor water cleanup system had isolated during the transient. The actual status is being corrected to state that the reactor water cleanup pump tripped during the transient. The licensee has notified the NRC Resident Inspector. Notified R3DO (Stone). |
Where | |
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Lasalle Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000374/LER-2014-001 |
Time - Person (Reporting Time:+-0.23 h-0.00958 days <br />-0.00137 weeks <br />-3.15054e-4 months <br />) | |
Opened: | Jason Adams 22:20 Aug 5, 2014 |
NRC Officer: | Jeff Rotton |
Last Updated: | Aug 6, 2014 |
50346 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Shutdown (0 %) |
LaSalle with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 570832024-04-20T12:04:00020 April 2024 12:04:00
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