ENS 51962
ENS Event | |
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17:20 Mar 28, 2016 | |
Title | Invalid Specified System Actuation |
Event Description | This 60-day report, as allowed by 10 CFR 50.73(a)(1), is being made pursuant to 10 CFR 50.73(a)(2)(iv)(A) to describe an unplanned, invalid actuation of containment isolation valves in more than one system.
On 3/28/16, at approximately 1320 [EDT], a loss of power occurred on the Unit 2 E124 480 volt load center due to an equipment operator inadvertently opening the main feed breaker during the process of applying a clearance to de-energize the E124-P-A motor control center for planned maintenance. Loss of the E124 load center resulted in Group II and Group III primary containment isolations due to an invalid ESF actuation signal. Systems impacted by the containment isolations included containment instrument nitrogen, containment atmospheric monitoring, reactor water cleanup, and secondary containment. Balance of plant impacts included partial loss of feedwater heating and a reduced condenser vacuum. Reactor power lowered to 86% as a result of the event and further decreased to approximately 80 percent when re-establishing the 3A, 4A and 5A feedwater heaters. Following direction from the control room, the E124 main feed breaker was promptly re-closed by equipment operators. Affected equipment was restored to its normal or planned configuration and containment isolations were reset at 1406. The containment isolation signal was generated as a result of the loss of power to the E124 load center and was not due to actual plant conditions or parameters meeting design criteria for containment isolation. Therefore, this is considered to be an invalid actuation. The licensee has notified the NRC Resident Inspector. |
Where | |
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Peach Bottom Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1432.03 h59.668 days <br />8.524 weeks <br />1.962 months <br />) | |
Opened: | Dan Dullum 09:22 May 27, 2016 |
NRC Officer: | Bethany Cecere |
Last Updated: | May 27, 2016 |
51962 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (80 %) |
WEEKMONTHYEARENS 562802022-11-12T04:33:00012 November 2022 04:33:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-DAY Telephonic Notification ENS 548202020-06-08T08:24:0008 June 2020 08:24:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 529612017-07-14T18:53:00014 July 2017 18:53:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 519622016-03-28T17:20:00028 March 2016 17:20:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 500892014-03-09T21:13:0009 March 2014 21:13:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Actuation of an Emergency Service Water System ENS 479072012-03-13T20:04:00013 March 2012 20:04:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Report - Invalid Primary Containment Isolation System Actuation ENS 449402009-03-02T15:55:0002 March 2009 15:55:00 10 CFR 50.73(a)(1), Submit an LER Invalid Primary Containment Isolation Signal Due to Maintenance Error ENS 444652008-07-24T03:25:00024 July 2008 03:25:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation Due to Loss of One Offsite Power Circuit to Safety Buses ENS 439102007-12-11T21:45:00011 December 2007 21:45:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Notification of an Invalid Actuation of Units 2 and 3 Primary Containment Isolation Systems ENS 411932004-09-28T06:00:00028 September 2004 06:00:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to Bus Voltage Dip During Recirc Mg Start ENS 411922004-09-18T08:57:00018 September 2004 08:57:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to Off Site Power Source Fast Transfer ENS 408192004-04-25T05:05:00025 April 2004 05:05:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 401982003-09-25T04:00:00025 September 2003 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.73(a)(1), Submit an LER Initiation of a Technical Specification Required Shutdown at Peach Bottom 2 ENS 401042003-07-27T22:39:00027 July 2003 22:39:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Report 2022-11-12T04:33:00 | |