LER-1982-064, Updated LER 82-064/03X-1:on 820823 & Jan 1984,Station II Cable Tray Fixed Spray Sys Did Not Meet Tech Spec Requirements.Caused by Restriction in Supply Line Strainer Due to Buildup of Silt & Clam Shells |
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| 2591982064R00 - NRC Website |
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UPDATE REPORT PREVIOUS REPORT DATE:
9/21/82
,N,,,FO RM 366 U S. NUCLE AR REGULATCRY C3MMlZ212N AP/40VED BY OMD 30CF SO LICENSEE EVENT REPORT 3:50 0011 CONTROL B LOCK:
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.e DOCKET NUMBER EVENT DaTE R EPORT D ATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o l2 } l During normal operation while performing SI li.11. A.1.g (Building Hydraulic l
lo 13 l l Performance Verification), it was determined that unit 1. Station II cable l
l0 l4 l l tray fixed spray system did not_ meet technical specification requirements as l
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.F CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 lil0ll Cause in each case was apparent estriction in supply line strainer (Fisher l
l i j i l l Governor Fre-Flo 2600) due to buildup of silt and clam shells.
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l t l 2 l l cleaned, flushed and satisfactorily retested. Strainers are routinely
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l i l 3 l l inspected and cleaned, and no problems have been detected.
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l t 14 l l strainer will be removed and cleaned every month.
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t Tennessee Valley Authority Form BF 17 Browns Ferry Nuclear Plant BF 15,2 2/1%d2 LER SUPPLEBIENTAL INFORb1ATION BFRO-50 259 /
82064R1 Technical Specification Involved 3 11.A.9 Reported Under Technical Specification 6.7 2.b(2) 4/21/ 84
- Date Due NRC Event Narrative:
- - Unii. 2 was in a refueling outage; unit 3 was operating at 95-percent power.
Units 2 and 3 were unaffected by this event. With unit 1 operating at 96-percent power, during the performance of Surveillance Instruction (SI) 4.11.A.1.g (Building Hydraulic Performance Verification), it was determined the Station II cable tray fixed spray system did not meet Technical Specifi-cation (T.S.) requirements as shown in Table 3 11. A.
There was no effect on public health and safety.
A patrolling fire watch was established in accordance with T.S. 3 11.A.2.
There are no redundant systems.
The strainer (Fisher Governor Co., Fre-Flo 260C) to this station was removed, cle,aned, flushed, and the station retested and found to meet T.S. require-ments. The cause was an apparent restriction in the supply line strainer due to a buildup of silt and clam shells. This station was retested within the following 18-months (T.S. frequency is once/3 years) in order to determine if any further changes in performance had occurred.
When retested (January 27, 1984), the unit 1 Station II cable tray fixed spray system again failed to meet T.S. requirements.
There was no effect on public health and safety.
A fire watch was established and the strainer to this station was again removed, cleaned, and flushed.
The station was retested and was found to meet T.S. limits. The station was out-of-service approximately six hours. The strainers on this system are routinely back-flushed every month and removed, checked, and cleaned once every three months per Mechanical Maintenance Instruction 122 (High Pressure Fire Protection System Flush, Strainer Inspection, and Strainer Cleaning). No specific problems have been detected based on the inspections.
The flow problem identified by surveillance testing appears to affect only Station II.
"In addition to the routine strainer inspections, Station II will have its strainer remqved, checked, and cleaned every month.
At the next scheduled performance of SI 4.11. A.1.g (June 1985), the effect of tripling the preven-tive maintenance frequency will be investigated.
- Previous Similar Events:
Retention :
'criod - Lifetime; Responsibility - Document Control Supervisor
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l lB TENNESSEE VALLEY. AUTHORITY Browns Ferry Nuclear Plant P. O. Box 2000 Decatur, Alabama 35602 1
d, D April 20, 1984 J
l Mr. James P. O'Reilly, Regional Administrator U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303 i
Dear Mr. O'Reilly:
TENNESSEE VALLEY AUTHORITY - BROWNS FERRY NUCLEAR PLANT UNIT 1 - DOCKET NO. 50-259 - FACILITY OPERATING LICENSE DPR REPORTABLE OCCURRENCE REPORT BFRO-50-259/82064 R1 The enclosed report provides followup information concerning unit 1, station II cable tray fixed spray system. This report is submitted in accordance with Browns Ferry Unit 1 Technical Specification 6.7.2.b.(2).
Very truly yours, l
TENNESSEE VALLEY AUTHORITY 6.
G. T. Jones Power Plant Superintendent Browns Ferry Nuclear Plant Enclosure oc (Enclosure):
U. S. Nuclear Regulatory Commission Document Control Desk Washington D.C.
.20555 NRC Inspector, Browns Ferry Nuclear Plant J
ll An Equal Opportunity Employer ggg
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| 05000296/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | | 05000259/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | | 05000259/LER-1982-001-03, /03L-0:on 820103,meteorological Instrumentation O-Tdr-90-103 Air Temp Delta T & O-XR-90-102-1 (30 Ft Air Speed) Failed.Caused by Lightning Damage to Transistors Q3 & Q4 & Blown Fuses in Panel 9-34 & at Meterological Station | /03L-0:on 820103,meteorological Instrumentation O-Tdr-90-103 Air Temp Delta T & O-XR-90-102-1 (30 Ft Air Speed) Failed.Caused by Lightning Damage to Transistors Q3 & Q4 & Blown Fuses in Panel 9-34 & at Meterological Station | | | 05000260/LER-1982-001, Forwards LER 82-001/01T-0 | Forwards LER 82-001/01T-0 | | | 05000260/LER-1982-001-01, /01T-0:on 820115,during Offsite Verification of Process Computer Programming Changes Involving Data in Tech Spec Tables 3.5.I-3 & 3.5.I-4,discovered Input Error.Caused by Personnel Error.Personnel Will Be Reinstructed | /01T-0:on 820115,during Offsite Verification of Process Computer Programming Changes Involving Data in Tech Spec Tables 3.5.I-3 & 3.5.I-4,discovered Input Error.Caused by Personnel Error.Personnel Will Be Reinstructed | | | 05000296/LER-1982-001-03, /03L-0:on 820114,fixed Spray Fire Protection Valve Accidentally Initiated,Causing Smoke Detector to Be Wetted & Emit False Smoke Alarm.Caused by Personnel Hanging Coats on Valve Station.Valve Reset & Smoke Detector Replaced | /03L-0:on 820114,fixed Spray Fire Protection Valve Accidentally Initiated,Causing Smoke Detector to Be Wetted & Emit False Smoke Alarm.Caused by Personnel Hanging Coats on Valve Station.Valve Reset & Smoke Detector Replaced | | | 05000259/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000259/LER-1982-002-03, /03L-0:on 820106,drywell High Pressure Switch 1-PS-64-58C Found Isolated.Apparently Caused by Performance of Surveillance Instruction 4.2.B.5.Switch Returned to Normal & All Other Valving 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| /03L-0:on 820116,during Reduced Load While Performing MSIV Closure Si,Scram Trip Logic Az Annunciation Failed to Alarm.Caused by Failure of Limit Switch 4 of FCV-1-52 to Open.Switch Will Be Replaced | | | 05000260/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000260/LER-1982-003-03, /03L-0:on 820116,during Normal Operation,While Performing Surveillance test,PS-3-74A Switch 1 & PS-68-96 Switch 1,low Pressure Switches,Were Out of Tolerance by 4% & 6%.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820116,during Normal Operation,While Performing Surveillance test,PS-3-74A Switch 1 & PS-68-96 Switch 1,low Pressure Switches,Were Out of Tolerance by 4% & 6%.Caused by Instrument Drift.Switches Recalibr | | | 05000260/LER-1982-003, Forwards LER 82-003/03L-0 | Forwards LER 82-003/03L-0 | | | 05000296/LER-1982-003-03, /03L-0:on 820123,during Refueling Outage,While Performing SI 4.2.A-39,temp Switches TS-69-30A,B,C & E on Reactor Cleanup Sys Floor Drain High Temp,Operated at Less than 160 F.Caused by Improper Calibr or Instrument Drift | /03L-0:on 820123,during Refueling Outage,While Performing SI 4.2.A-39,temp Switches TS-69-30A,B,C & E on Reactor Cleanup Sys Floor Drain High Temp,Operated at Less than 160 F.Caused by Improper Calibr or Instrument Drift | | | 05000296/LER-1982-003, Forwards LER 82-003/03L-0 | Forwards LER 82-003/03L-0 | | | 05000296/LER-1982-004, Forwards LER 82-004/03L-0 | Forwards LER 82-004/03L-0 | | | 05000296/LER-1982-004-03, /03L-0:on 820207,while Performing Surveillance Instruction,Temp Switches 3S-TS-73-2A & 3-TS-73-2B Operated Above Tech Specs Limit.Caused by Switches Being Out of Calibr.Switches Calibr | /03L-0:on 820207,while Performing Surveillance Instruction,Temp Switches 3S-TS-73-2A & 3-TS-73-2B Operated Above Tech Specs Limit.Caused by Switches Being Out of Calibr.Switches Calibr | | | 05000296/LER-1982-005, Forwards LER 82-005/03L-0 | Forwards LER 82-005/03L-0 | | | 05000259/LER-1982-005, Forwards Updated LER 82-005/03X-1 | Forwards Updated LER 82-005/03X-1 | | | 05000260/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000260/LER-1982-006-03, /03L-0:on 820125,while Performing SI 4.1.A-7,low Water Level Switch LIS-3-203B,switch 1 Found 3% Out of Tolerance.Caused by Setpoint Drift.Switch Recalibr | /03L-0:on 820125,while Performing SI 4.1.A-7,low Water Level Switch LIS-3-203B,switch 1 Found 3% Out of Tolerance.Caused by Setpoint Drift.Switch Recalibr | | | 05000259/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000259/LER-1982-006-03, /03L-0:on 820112,1-PS-3-74B Switch Number 1 Found Operating Below Tech Spec Limit.Caused by Instrument Drift. Barton Model 288 Pressure Switch Recalibr.Action Plan Re Design Change Will Be Forwarded | /03L-0:on 820112,1-PS-3-74B Switch Number 1 Found Operating Below Tech Spec Limit.Caused by Instrument Drift. Barton Model 288 Pressure Switch Recalibr.Action Plan Re Design Change Will Be Forwarded | | | 05000296/LER-1982-007-03, /03X-1:on 820318,ice Storm Caused Loss of Offsite Power to 4-kV bus-tie Board.Caused by Interruption of Power to Cooling Tower Transformers & 4-kV Switchgear Feeding bus-tie Board Due to Loss of 161-kV Lines | /03X-1:on 820318,ice Storm Caused Loss of Offsite Power to 4-kV bus-tie Board.Caused by Interruption of Power to Cooling Tower Transformers & 4-kV Switchgear Feeding bus-tie Board Due to Loss of 161-kV Lines | | | 05000260/LER-1982-007-03, /03L-0:on 820126,while Performing SI 4.2.A-3, Reactor low-water Level Switch Lis-3-56A Switch Number 2 Was Found 8% Out of Tolerance.Caused by Setpoint Drift.Yarway Model 4418c Switch Recalibr & Functionally Tested | /03L-0:on 820126,while Performing SI 4.2.A-3, Reactor low-water Level Switch Lis-3-56A Switch Number 2 Was Found 8% Out of Tolerance.Caused by Setpoint Drift.Yarway Model 4418c Switch Recalibr & Functionally Tested | | | 05000260/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | | 05000296/LER-1982-007, Forwards LER 82-007/03X-1 | Forwards LER 82-007/03X-1 | | | 05000259/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | | 05000259/LER-1982-007-03, /03L-0:on 820113,XR-90-104 Lost Indication for Wind Direction & Wind Speed Channel C,Elevation 887 Msl. Caused by Anemometer & Vane Icing Due to Inclement Weather. Anemometer & Vane Allowed to Thaw | /03L-0:on 820113,XR-90-104 Lost Indication for Wind Direction & Wind Speed Channel C,Elevation 887 Msl. Caused by Anemometer & Vane Icing Due to Inclement Weather. Anemometer & Vane Allowed to Thaw | | | 05000259/LER-1982-008, Forwards LER 82-008/03L-0 | Forwards LER 82-008/03L-0 | | | 05000296/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000259/LER-1982-008-03, /03L-0:on 820116,CAM 1-90-250 (Refuel Floor) Rendered Inoperable Due to Broken Drive Belt.Caused by Normal Wear Due to Continuous Operation.Std V-belt for Schwitzer Model 325 Series Air Pump Replaced | /03L-0:on 820116,CAM 1-90-250 (Refuel Floor) Rendered Inoperable Due to Broken Drive Belt.Caused by Normal Wear Due to Continuous Operation.Std V-belt for Schwitzer Model 325 Series Air Pump Replaced | | | 05000296/LER-1982-008-03, /03L-0:on 820331,while Performing Daily Source & Background Check of CAM-390-250,reactor & Turbine Bldg Vent Monitor,Inlet Sample Line Discovered Disconnected.Caused by Personnel Error.Sample Lines Reconnected | /03L-0:on 820331,while Performing Daily Source & Background Check of CAM-390-250,reactor & Turbine Bldg Vent Monitor,Inlet Sample Line Discovered Disconnected.Caused by Personnel Error.Sample Lines Reconnected | | | 05000260/LER-1982-008-03, /03L-0:on 820127,after Calibr,Rod Block Monitor Channel B Failed to Pass Functional Test of SI 4.2.C-2. Caused by Electronic IC Failure Possibly Due to Voltage Spike During Calibr.Ge 136B1333G1 Gain Change Card Replaced | /03L-0:on 820127,after Calibr,Rod Block Monitor Channel B Failed to Pass Functional Test of SI 4.2.C-2. Caused by Electronic IC Failure Possibly Due to Voltage Spike During Calibr.Ge 136B1333G1 Gain Change Card Replaced | | | 05000260/LER-1982-008, Forwards LER 82-008/03L-0 | Forwards LER 82-008/03L-0 | | | 05000259/LER-1982-009-03, /03L-0:on 820117,during Normal Operation,Smoke Detector in Relay Room Alarmed & Would Not Clear.Caused by Increased Detector Sensitivity Due to Natural Aging.Kidde FT-200 Ionization Smoke Detector Replaced | /03L-0:on 820117,during Normal Operation,Smoke Detector in Relay Room Alarmed & Would Not Clear.Caused by Increased Detector Sensitivity Due to Natural Aging.Kidde FT-200 Ionization Smoke Detector Replaced | | | 05000259/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000296/LER-1982-009-03, /03L-0:on 820407,during Refueling Outage,While Performing SI 4.2.A.6,pressure Switches 3-PS-1-76 & 3-PS-1-82 Had as-found Setpoints of 815.7 Psig & 813.7 Psig, Respectively.Caused by Setpoint Drift.Switches Recalibr | /03L-0:on 820407,during Refueling Outage,While Performing SI 4.2.A.6,pressure Switches 3-PS-1-76 & 3-PS-1-82 Had as-found Setpoints of 815.7 Psig & 813.7 Psig, Respectively.Caused by Setpoint Drift.Switches Recalibr | | | 05000296/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000259/LER-1982-010-03, /03L-0:on 820112,stack Monitor Was Declared Inoperable After Low Flow Alarm.Caused by 6 Ft Segment of Sample Line Freezing,Inhibiting Sampling Flow to Monitor | /03L-0:on 820112,stack Monitor Was Declared Inoperable After Low Flow Alarm.Caused by 6 Ft Segment of Sample Line Freezing,Inhibiting Sampling Flow to Monitor | | | 05000259/LER-1982-010, Forwards LER 82-010/03L-0 | Forwards LER 82-010/03L-0 | | | 05000296/LER-1982-010-03, /03L-0:on 820406,during Refueling & Routine Performance of SI 4.2.F-10,pressure Switch 3-PS-64-67 Had as-found Calibr of 35.5 Psig.Caused by Setpoint Drift.Model 50-560-111AAAC1 Alarm Recalibr | /03L-0:on 820406,during Refueling & Routine Performance of SI 4.2.F-10,pressure Switch 3-PS-64-67 Had as-found Calibr of 35.5 Psig.Caused by Setpoint Drift.Model 50-560-111AAAC1 Alarm Recalibr | | | 05000296/LER-1982-010, Forwards LER 82-010/03L-0 | Forwards LER 82-010/03L-0 | | | 05000260/LER-1982-010, Corrected LER 82-010/03L-0 on 811021,during Full Power,Avg Power Range Monitor Output Signal Calibr Was Not Performed within Required Frequency During 811014-28.Caused by Personnel Error.Personnel Instructed to Be More Careful | Corrected LER 82-010/03L-0 on 811021,during Full Power,Avg Power Range Monitor Output Signal Calibr Was Not Performed within Required Frequency During 811014-28.Caused by Personnel Error.Personnel Instructed to Be More Careful | | | 05000260/LER-1982-010-03, /03L-0:on 820121,during Full Power Operation SI 4.1.B.2 (APRM Output Signal Calibr) Not Performed within Required Frequency During 811014-28.Caused by Personnel Error | /03L-0:on 820121,during Full Power Operation SI 4.1.B.2 (APRM Output Signal Calibr) Not Performed within Required Frequency During 811014-28.Caused by Personnel Error | | | 05000260/LER-1982-011, Forwards LER 82-011/03L-0 | Forwards LER 82-011/03L-0 | | | 05000259/LER-1982-011, Forwards LER 82-011/03L-0 | Forwards LER 82-011/03L-0 | | | 05000296/LER-1982-011, Forwards LER 82-011/01T-0 | Forwards LER 82-011/01T-0 | | | 05000296/LER-1982-011-01, /01T-0:on 820414,while Performing SI 4.1.A-7 Reactor Protection Sys Water Level Switches 3-LIS-3-203A, 203B & 203D Operated Out of Tech Spec Allowance.Caused by Setpoint Drift | /01T-0:on 820414,while Performing SI 4.1.A-7 Reactor Protection Sys Water Level Switches 3-LIS-3-203A, 203B & 203D Operated Out of Tech Spec Allowance.Caused by Setpoint Drift | |
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