05000315/LER-1979-016-03, /03L-0 on 790304:two Manual Containment Isolation Valves Were Inadvertantly Left Open Following Routine Sample of Instrument Room.Caused by Personnel Oversight.Both Valves Were Returned to Their Normally Closed Positions

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/03L-0 on 790304:two Manual Containment Isolation Valves Were Inadvertantly Left Open Following Routine Sample of Instrument Room.Caused by Personnel Oversight.Both Valves Were Returned to Their Normally Closed Positions
ML17317B069
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 04/03/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B068 List:
References
LER-79-016-03L, LER-79-16-3L, NUDOCS 7904090187
Download: ML17317B069 (2)


LER-1979-016, /03L-0 on 790304:two Manual Containment Isolation Valves Were Inadvertantly Left Open Following Routine Sample of Instrument Room.Caused by Personnel Oversight.Both Valves Were Returned to Their Normally Closed Positions
Event date:
Report date:
3151979016R03 - NRC Website

text

U. S. NUCI.EAR REGULATORY COMMISSION NRC FORM 366 LtCENSEE EVENT REPOR

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80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES ~10 TWO MANUAL CONTAINMENT ISOLATION VALVES USED FOR INSTRUMENT ROOM SAMPLING WERE DISCOVERED TO BE IN THE OPEN POSITION.

UPON DISCOVERY, BOTH VALVES WERE RETURNED TO THEIR NORMALLY CLOSED POSITIONS IN ACCORDANCE WITH T.S. 3.6.3.1.

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TO PREVENT RECURRENCE, THE IMPORTANCE OF THE CONTAINMENT ISOLATION VALVES WAS DISCUSSED WITH THE AFFECTED PERSONNEL DURING A SECTION MEETING, 3

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