05000315/LER-1979-020-03, /03L-O on 790323:pressurizer Relief Tank Rupture Disk Blew Out While in Mode 3.Caused by Repeated Pressure Fluctuations Causing Rupture Disk to Weaken.Corrective Action Unnecessary Since Doors Functioned as Designed

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/03L-O on 790323:pressurizer Relief Tank Rupture Disk Blew Out While in Mode 3.Caused by Repeated Pressure Fluctuations Causing Rupture Disk to Weaken.Corrective Action Unnecessary Since Doors Functioned as Designed
ML17317B112
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 04/17/1979
From: Dickson J
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B111 List:
References
LER-79-020-03L, LER-79-20-3L, NUDOCS 7904240380
Download: ML17317B112 (2)


LER-1979-020, /03L-O on 790323:pressurizer Relief Tank Rupture Disk Blew Out While in Mode 3.Caused by Repeated Pressure Fluctuations Causing Rupture Disk to Weaken.Corrective Action Unnecessary Since Doors Functioned as Designed
Event date:
Report date:
3151979020R03 - NRC Website

text

U S NUCLEAR REGULATORY COMMISSIOPJ ENT REPORT (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATIONI 0

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METHOD OF OTHER STATUS ~

DISCOVERY NA

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