05000315/LER-1980-027-03, /03L-0:on 801218,spent Fuel Pool,Diesel Generator Room Floor & Containment Spring Line Peak Recording Accelerographs Found Out of Calibr.Cause Unknown.Peak Recording Accelerographs Recalibr

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/03L-0:on 801218,spent Fuel Pool,Diesel Generator Room Floor & Containment Spring Line Peak Recording Accelerographs Found Out of Calibr.Cause Unknown.Peak Recording Accelerographs Recalibr
ML17331A574
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 01/15/1981
From: Delong S
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17326A827 List:
References
LER-80-027-03L, LER-80-27-3L, NUDOCS 8101200371
Download: ML17331A574 (2)


LER-1980-027, /03L-0:on 801218,spent Fuel Pool,Diesel Generator Room Floor & Containment Spring Line Peak Recording Accelerographs Found Out of Calibr.Cause Unknown.Peak Recording Accelerographs Recalibr
Event date:
Report date:
3151980027R03 - NRC Website

text

U. S. NUCLEAR REGULATORY COMMISSION tCENSEE EVENT REPORT QI (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 1Q20 0

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DURING A CALXBRATION CHECK OF THE SEISMXC MONITORXNG PEAK RECORDING AND CONTAXNMENT SPRING LINE PRA'S WERE FOUND TO BE OUT OF CALIBRATION.

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