05000313/LER-1979-021-03, /03L-0:on 791115,while Securing Makeup & Purification Sys,Inside Containment Isolation Seal Return Valve Failed to Fully Close on Demand.Caused by Valve Operator Torque Switch Failing to Make Up.Switch Replaced

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/03L-0:on 791115,while Securing Makeup & Purification Sys,Inside Containment Isolation Seal Return Valve Failed to Fully Close on Demand.Caused by Valve Operator Torque Switch Failing to Make Up.Switch Replaced
ML19211A252
Person / Time
Site: Arkansas Nuclear 
Issue date: 12/06/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19211A250 List:
References
LER-79-021-03L-01, LER-79-21-3L-1, NUDOCS 7912170264
Download: ML19211A252 (1)


LER-1979-021, /03L-0:on 791115,while Securing Makeup & Purification Sys,Inside Containment Isolation Seal Return Valve Failed to Fully Close on Demand.Caused by Valve Operator Torque Switch Failing to Make Up.Switch Replaced
Event date:
Report date:
3131979021R03 - NRC Website

text

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NRC F ORM 366

. NUCLE AR REGUL ATORY COMMISSION (7 77)

LICENSEE EVENT REPORT EXHIBIT A CONTROL 8 LOCK: l l l l \\ \\ lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

1 AlR l Al N O ji lgl$0 l0 l -l0 0l 0l 0l0l-l0l0 l g 1 l1l1 l1lgl l lg o i 9

LeCENsit CODE le l

UCENst NUM8tH 25 26 UCLNbt ITP6 JO bI C A T stb 7

8 CON'T LoJ_J J, "C LL_l@l0i5p 0 i ois il 3 GI il1i il.1 71 9 @ l1 12l 01 6 7l 91@

3 8

60 Si DOCKET NuM8Ea 68 63 EVENT DATE 74 PS HE,OR T D ATE So EVENT OESCRIPTION AND PROSAGLE CONSEQUENCES h ITTTlI While securing rho Makeun & Puri fienrinn 9vsrom. with the unit in the I

Lo_U]1 cold shutdown condition. the Inside Contninrent Isolation Seal Return I

loI.II Valve for RCP "B".

CV-1272, failed to fully close on demand.

The out-1 0

5 sido enntnin-one Tcnlarinn 9pn1 Rornrn Vnivo enc nrnven nnernh19 & n1,redl o 6 l in the closed nosition.

IFR's 50-713/78-010 nnd 78-002 were due to 1

0 2

I similar failures of limitorcue type SMB torcue switch failures. Report-Inhin nnr T_9 6 1?_t? h I

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E LCCE suBC E COuPONENT COtJE

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OJE Lc_dJ l P I cl@ lE_l@ LAl@ IV l A l Ll VI O l Pl@ LAJ@ l_ZJ @

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9 10 in 12 TJ in i t, 2u sf oVENTI AL OCLupprNCf

    • E aOa r Atvis?uN

,_EVENTvfAR p{ PORT No.

CODE Int NO

@ " Lim seol21 7l9 I L-_J lO 21 1 I tr.J l o I 31 LLJ 1--J LO_J u'l,N,',

22 23 24 26 27 28 9

N 31 D

TAE N A T oN PLA T METMoD HOURS s8 T D

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3J 34 35 36 31 do el 42 43 44 as CAUSE OESCR.PTION AND CORRECrlVE ACTIONS lTnuneeig,einn rovanlod eh,e ehn valvo nnornenr enroup cuirch fnfled to I

i o

litil

-,1c o un in ehn fully nnon nncirinn_ ebne re,i n en i r,i n g e n, e rn1 nf the I

f7TTl I c 1 n c i n g ci rcni r nna dien11nuing tha valvo en cloce.

The toroue switch I

W lwas renlaced nnd rho valve was cycled several ti-es to verifv Droper I

ila I nnernrinn.

t

's T'AUE oT sasTArus @ "'s57sv' oisco.eur osses rio, @

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[.1]..] d@ l OI Ol O l@l enld shutdown l W @l NA l

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7 a 9 11 12 80 LosL O, om oAMAGE TO, ACILITY TYPE ot sCR'P TION (Lj@l NA l

' 9 3

n 9 to PU8LICITv Ed 4

issufD NRC UST oNLY A ULj@otscas, TION l

NA 1 llllll;;;i Chris N. Shively 5d5/968-2519 AME OF PREPARER

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