05000318/LER-1979-022-03, /03L-0 on 790619:containment Gaseous & Particulate Radioactivity Monitoring Sys Failed.Caused by Loss of Sampling Pump.Pump Restarted After 45 Minutes.No Specific Maint Action Taken to Correct Cause of Failure

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/03L-0 on 790619:containment Gaseous & Particulate Radioactivity Monitoring Sys Failed.Caused by Loss of Sampling Pump.Pump Restarted After 45 Minutes.No Specific Maint Action Taken to Correct Cause of Failure
ML19241B903
Person / Time
Site: Calvert Cliffs 
Issue date: 07/19/1979
From: Davis S, Lagiewski J
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19241B900 List:
References
LER-79-022-03L, LER-79-22-3L, NUDOCS 7907250304
Download: ML19241B903 (1)


LER-1979-022, /03L-0 on 790619:containment Gaseous & Particulate Radioactivity Monitoring Sys Failed.Caused by Loss of Sampling Pump.Pump Restarted After 45 Minutes.No Specific Maint Action Taken to Correct Cause of Failure
Event date:
Report date:
3181979022R03 - NRC Website

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_8 60 61 DOCK ET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o

2 l At 2315 tha Unit 2 contai rmont casect.2 and particulate radioactivity monitorino l

systems failed due to a loss of the samolino cumo (T.S.3.4.6.1.).

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4 i restarted at 0001 6/20/79, returning the gaseous and particulate radioactivity I

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