LER-1979-025, /01T-0:on 790926,during Normal Operation,Main Steam Lines Not Isolated within 8-h Following Main Steam Line High Temp Logic Actuation.Caused by Misinterpretation of Tech Specs.Revision of Specs Proposed |
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E nr.i i i r, ;w io a,..an gno.t AdLE CO*.it GUE NCES h L. stinnormal onexation due to variation in interpretation of technical specification,
"l-FR[ the main _ steam lines were not isolated following main steam line high temperature log,
! ic actuation within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> as required by Technical Specification Table 3.2. A. There o
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A techr. cal specification revision for clarification is being creoosed. The new Ltechnical specification intrepretation has since been discussed with plant mana i
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7925 Trehr.. ell.^.pterfication inm!vt !
3*2.A P.e p e e : Unsier '"e d.nical Spe,:tf! cation,
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Date,f 0;currar.cc _ 9/26/79
'i';;r.e of Occurrence 1525 Unit 1
Identif:c3* ion and De scription <>f Occurrence:
Due to variation in interpretation of technical specification the main steam lines were not isolated within eight hours as req.iired kv Technical Specification Table 3.2.A.
Conditions Prior to Occurrence:
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U-3 0 0% refueling outage A: tiun s;v cifieu in the Technical Sp;cificHica Surveinance Requirer.:en's met
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MSIV's not closed within eight hours.
At> tem n Caur. c,f Occut re nce A half isolation signal was received from the "D" logic d'u'e toan ' apparentl'y fauTtf temperature switch.
A JIWR was reviewed by PORC and placed
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on main steam line "D" logic to clear the isolation signal and allow safe personnel entry.
While troubleshooting the logic problent the "A" logic rain steam high temperature circuit fuse opened due to an open cable.
During the event, no violation of the technical specification was recognized.
Af ter review of the event the next day, it was determined that the main steam lines should have been isolated by 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />.
The reactor was shut down at 1859 hours0.0215 days <br />0.516 hours <br />0.00307 weeks <br />7.073495e-4 months <br /> on 9/26/79, and main steam lines were isolated at 0114 hours0.00132 days <br />0.0317 hours <br />1.884921e-4 weeks <br />4.3377e-5 months <br /> on 9/27/79 Analysis of Occurrence There was no damage to plant equipment, no activity released, no personnel exposure or injury, and no ha::ard to health or safety of the public.
Full automatic isolation capabi Corr <:c:lity s*.111 existed.
- ve Ac: ton: The fuse was replaced on the "A" line returning it to service; and an investigation on the "D" line revealed that cable 1FC143II3 was open, and the open cable was replaced.
During the investigation cable IPC144-IIB was damaged and was repaired.
A technical specification revision for clarification is being proposed.
The i'nterpre-tation of this particular technical specification has been discussed with plant management through PORC.
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| 05000296/LER-1979-001-03, /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | | | 05000296/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000259/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000259/LER-1979-001-01, /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | | | 05000260/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000260/LER-1979-001-03, /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | | | 05000296/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000259/LER-1979-002-03, /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | | | 05000259/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000260/LER-1979-002-03, /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | | | 05000260/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000296/LER-1979-002-03, /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | | | 05000296/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000259/LER-1979-003-01, /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | | | 05000259/LER-1979-003, Forwards LER 79-003/01T-1 | Forwards LER 79-003/01T-1 | | | 05000260/LER-1979-003-01, /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | | | 05000259/LER-1979-003-03, /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | | | 05000296/LER-1979-003-03, /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | | | 05000260/LER-1979-003, Forwards LER 79-003/01T-0 | Forwards LER 79-003/01T-0 | | | 05000260/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004-03, /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on | /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on Site | | | 05000296/LER-1979-004-03, /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | | | 05000260/LER-1979-004-03, /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | | | 05000296/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000296/LER-1979-005, Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. 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Caused by Setpoint Drift.Switches Recalibr | /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | | | 05000260/LER-1979-007-03, /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | | | 05000260/LER-1979-008-01, /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | | | 05000259/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000259/LER-1979-008-03, /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | | | 05000296/LER-1979-008-03, /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | | | 05000260/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000296/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000296/LER-1979-009-03, /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | | | 05000260/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000296/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | |
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