05000366/LER-1978-084-03, /03L-0 on 781213:during Visual Insp of Standby Gas Treatment Sys snubbers,R69 Snubber Found to Be Low on Fluid. Caused by Fluid Leaking Past Refill Plug

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/03L-0 on 781213:during Visual Insp of Standby Gas Treatment Sys snubbers,R69 Snubber Found to Be Low on Fluid. Caused by Fluid Leaking Past Refill Plug
ML19259A757
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 12/29/1978
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19259A752 List:
References
LER-78-084-03L, LER-78-84-3L, NUDOCS 7901100266
Download: ML19259A757 (1)


LER-1978-084, /03L-0 on 781213:during Visual Insp of Standby Gas Treatment Sys snubbers,R69 Snubber Found to Be Low on Fluid. Caused by Fluid Leaking Past Refill Plug
Event date:
Report date:
3661978084R03 - NRC Website

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