LER-1980-037, /03L-0:on 800418,steam Generator Level Transmitter LTSP9A6 & LTSP9B6 to Steam & Feedwater Rupture Control Sys Found Out of Calibr.Caused by Zero Shift on Instruments Coupled W/Tightening of Tolerances.Instruments re-calibr |
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U.S. NUCLE AR REGULATORY COMMISSION NRC FORM 766 (7 ??)
LICENSEE EVENT REPORT nh CONTROL BLOCK: l l
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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo ltl l0 lH lD lB lS l1 l@l0 l0 l0 l0 l0 l0 l0 l0 l0 l0 l0 l@l 4l 1l 1l lj 1]@l l
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7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TY PE Jo 57 CAT 68 lolil 5$n"CE l L l@l 0 l 5 l 0 l-l 0 l 3 l 4 l 6 l@l 0 l4 l1 l8 l8 l0 l@l0 l 5 l1 l 618
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8 60 61 DOOKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 6J EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o l 2 ] l (NP-33-80-46) On 4/18/80 at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> during Steam Generator Level to Steam and Feed-l 5031.16, Steam Generator l l water Rupture Control System (SFRCS) Refueling Calibration ST o 3 A check of the other l
l Level Transmitter LTSE9A6 was found to be out of calibration.
o 4 J O J s j j seven revealed that only one additional level transmitter was out of calibration.
Be-l ling in Mode 5, the station did not enter the action statement of Technical Specifica-l o c 10171 I tion 3.3. 2.2.
There was no danger to the health and safety of the public or station l
l lo18l l personnel. Only two of the eight were out of tolerance.
DE CODE SUBC E COMPONENT CODE SUSC dE SU E
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40 41 42 43 44 47 33 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lilollThe cause was a zero shift on the two above mentioned instruments coupled with a tightqn-ling of tolerances a - a direct result of the recent change in steam generator low level ]
i i l bistable setpoints on 11/17/79, see LER NP-32-79-12 (79-105). On 4/18/80, LTSP9A6 wasl
, 7 lrecalibrated per ST 5031.16. On 5/1/80, LTSP9B6 was recalibrated under Maintenance j
, 3 ii g4 i l Work Order IC361-80 to within specification.
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8 9 10 419-259-5000, Ext. 235 2 DVR 80-069 Dadel hautman PHONE:
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TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-80-46 PATE OF EVENT: April 18, 1980 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:
Steam Generator Level Transmitter LTSP9A6 and LTSP9B6 to Steam and Feedwater Rupture Control System (SFRCS) Out of Calibration The unit was in Mode 5, with Power (MRT) = 0 and Conditions Prior to Occurrence:
Load (Gross MRE) = 0.
Description of Occurrence:
On' April 18, 1980 at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> during Steam Generator Level to SFRCS Refueling Calibration Surveillance Test ST 5031.16, Steam Generator Level Transmitter LTSP9A6 was found to be out of calibration.
At an applied differ-ential pressure of 359.4 inches differential pressure, which corresponds to the low level and trip setpoint, the output from Analog Amplifier AA01 in Steam Generator Level Instrument Cabinet Channel 1 was found to be 0.8338 volts DC, whereas the maximum 7
j amount allowed was.8245 volts DC.
I Further evaluation on April 27, 1980 of the maximum allowed amount showed an error in the calculation. As a result of this evaluation, one other Steam Generator Level Transmitter LTSP9B6 was found to be out of tolerance at this specific level.
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Neither occurrence placed the unit in the action statement of Technical Specification 3.3.2.2 since it required the inoperable channel to be placed in the tripped condition within one hour in Modes 1, 2, and 3 only. The unit was in Mode 5 at the time of the occurrence.
Designation of Apparent Cause of Occurrence: The apparent cause of the occurrence l
was determined to be a zero shift on the two above mentioned instruments coupled with a tightening of tolerances as a direct result of the recent change in steam generator low level bistable setpoints on November 17, 1979, see Licensee Event Report NP-32-79-12.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. Of the total of eight steam generator level transmitters to the SFRCS, two of the eight were found to be out of the allowed tolerance. The actual levels displayed based on instrument tolerance and applied differential pressure were 4
rore conservative than the levels that would have been achieved on steam generator low l
level trips prior to changes made to _ steam generator low level bistable setpoints on November 17, 1979, s'e Licensee Event Report NP-32-79-12.
The results of the safety avaluation performed based'on previous steam generator low level bistable setpoints have shown no cause for a safety concern.
LER #80-037 i
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1 TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE PAGE 2 SUPPLEMENTAL INFORMATION FOR LER NP-33-80-46 a
Corrective Action
On April 18, 1980, Level Transmitter LTSP9A6 was recalibrated per i
Surveillance Test ST 5031.16 to within specification. On May 1, 1980, Level Trans-mitter LTSP9B6 was recalibrated under Maintenance Work Order IC-361-80 to within apectfIcatLon.
Failure Data: There have been no previous occurrences of calibration problems with 4
l analog amplifiers.
LER #80-037 I
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| 05000346/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000346/LER-1980-001-01, /01T-0:on 800103,during Plant Heatup,Safety Features Actuation Sys Channels 1 & 3 Tripped at 1,600 Psig, Causing Level 2 Actuation.Operators Correctly Tripped Reactor Coolant Pumps.Caused by Procedural Deficiency | /01T-0:on 800103,during Plant Heatup,Safety Features Actuation Sys Channels 1 & 3 Tripped at 1,600 Psig, Causing Level 2 Actuation.Operators Correctly Tripped Reactor Coolant Pumps.Caused by Procedural Deficiency | | | 05000346/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000346/LER-1980-002-03, /03L-0:on 800103,after Actuating of Safety Features Actuation Sys Level 2,demin Water Valve DW68318 Did Not Indicate Closed & Monitor Light Did Not Indicate Properly.Caused by Maladjusted Position Indicator Switch | /03L-0:on 800103,after Actuating of Safety Features Actuation Sys Level 2,demin Water Valve DW68318 Did Not Indicate Closed & Monitor Light Did Not Indicate Properly.Caused by Maladjusted Position Indicator Switch | | | 05000346/LER-1980-003-03, /03L-0:on 800103,during Auxiliary Feedwater Pump Test,Pump l-1 Was Declared Inoperable.Caused by Improperly Adjusted Slip Clutch Between Governor Manual Speed Adjustment Shaft & Remotely Controlled Speed Changer Motion | /03L-0:on 800103,during Auxiliary Feedwater Pump Test,Pump l-1 Was Declared Inoperable.Caused by Improperly Adjusted Slip Clutch Between Governor Manual Speed Adjustment Shaft & Remotely Controlled Speed Changer Motion | | | 05000346/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000346/LER-1980-004-03, /03L-0:on 800107,control Rod 5-11 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals.Possibly Caused by Isolation of Position Indication Cabling & Electrical Penetration | /03L-0:on 800107,control Rod 5-11 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals.Possibly Caused by Isolation of Position Indication Cabling & Electrical Penetration | | | 05000346/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000346/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000346/LER-1980-005-03, /03L-0:on 800110,Tech Spec Late Date Passed W/O Performance of Boric Acid Flowpath Heat Tracing Weekly Test. Caused by Known Deficiency in Design of Sys Resulting in Inability to Maintain Min Temp Necessary During Startup | /03L-0:on 800110,Tech Spec Late Date Passed W/O Performance of Boric Acid Flowpath Heat Tracing Weekly Test. Caused by Known Deficiency in Design of Sys Resulting in Inability to Maintain Min Temp Necessary During Startup | | | 05000346/LER-1980-006-03, /03L-0:on 800112,found Fiberglass Insulation Stuffed Into Open Wall Ventilator Between Water Treatment Bldg & Svc Water Valve Room,Causing Fire Damper to Be Inoperable.Figerglass Removed | /03L-0:on 800112,found Fiberglass Insulation Stuffed Into Open Wall Ventilator Between Water Treatment Bldg & Svc Water Valve Room,Causing Fire Damper to Be Inoperable.Figerglass Removed | | | 05000346/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000346/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000346/LER-1980-007-03, /03L-0:on 800116,ref Position Verification for Group 5,rod 11,was Made 1-h & 40 Minutes Late.Caused by Operator Oversight Due to Lack of Adequate Reminder Sys. Multiple Timer Sys Will Prevent Recurrence | /03L-0:on 800116,ref Position Verification for Group 5,rod 11,was Made 1-h & 40 Minutes Late.Caused by Operator Oversight Due to Lack of Adequate Reminder Sys. Multiple Timer Sys Will Prevent Recurrence | | | 05000346/LER-1980-008-03, Gap Discovered in Wall Where Five two-inch Conduits Go from Electrical Penetration Room 2 to Cable room.Six-inch Gap Around Ventilation Duct Also Found.Caused by Improper Initial Installation | Gap Discovered in Wall Where Five two-inch Conduits Go from Electrical Penetration Room 2 to Cable room.Six-inch Gap Around Ventilation Duct Also Found.Caused by Improper Initial Installation | | | 05000346/LER-1980-008, Forwards Revised LER 80-008/03L-1 | Forwards Revised LER 80-008/03L-1 | | | 05000346/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000346/LER-1980-009-03, /03L-0:on 800122,discovered That NI-7 Indication on Computer Group 38 Was Reading Less than Heat Balance Power,Putting NI-7 Below Instrumentation Operability Limit Line.Caused by Extremely Tight Calibr Band at 100% Power | /03L-0:on 800122,discovered That NI-7 Indication on Computer Group 38 Was Reading Less than Heat Balance Power,Putting NI-7 Below Instrumentation Operability Limit Line.Caused by Extremely Tight Calibr Band at 100% Power | | | 05000346/LER-1980-010-01, /01T-0:on 800214,reanalysis of RCS Pipe Restraints Per IE Insp Rept 50-346/79-23 Revealed Design Deficiency on Two Reactor Coolant Hot Leg Pipe Whip Restraints at Top of Each RCS Hot Leg.Caused by Design Error | /01T-0:on 800214,reanalysis of RCS Pipe Restraints Per IE Insp Rept 50-346/79-23 Revealed Design Deficiency on Two Reactor Coolant Hot Leg Pipe Whip Restraints at Top of Each RCS Hot Leg.Caused by Design Error | | | 05000346/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000346/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000346/LER-1980-011-03, /03L-0:on 800131,during Normal Operation, Operations Personnel Received Half Trip on Steam & Feedwater Rupture Control Sys Channels 1/3.Caused by Spurious Trip from +25 Volt Dc Power Supply PS03 in Sglic Channel 1 | /03L-0:on 800131,during Normal Operation, Operations Personnel Received Half Trip on Steam & Feedwater Rupture Control Sys Channels 1/3.Caused by Spurious Trip from +25 Volt Dc Power Supply PS03 in Sglic Channel 1 | | | 05000346/LER-1980-012-03, /03L-0:on 800201,operator Noticed Loss of Control Room Position Indication for Letdown Cooler Isolation Valve MU2A.Caused by Design Deficiency.Apparently,Someone Brushed Up Against Disconnect Breaker Switch.Switch Reposition | /03L-0:on 800201,operator Noticed Loss of Control Room Position Indication for Letdown Cooler Isolation Valve MU2A.Caused by Design Deficiency.Apparently,Someone Brushed Up Against Disconnect Breaker Switch.Switch Repositioned | | | 05000346/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000346/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000346/LER-1980-013-03, /03L-0:on 800208,w/reactor Startup in Progress, Personnel Noted Control Rod 5-11 Absolute Position Indication Was Not Responding.Caused by Blown Fuse F14 in Position Ref Panel | /03L-0:on 800208,w/reactor Startup in Progress, Personnel Noted Control Rod 5-11 Absolute Position Indication Was Not Responding.Caused by Blown Fuse F14 in Position Ref Panel | | | 05000346/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000346/LER-1980-014-03, /03L-0:on 800208,pressurizer Sample Sys Containment Isolation Valve RC240B Failed to Close Twice. 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Caused by Improper Torque Switch Setting & Stripped Screw on Closing Contactor.Settings Readjusted & Switch Replaced | | | 05000346/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000346/LER-1980-015-03, /03L-0:on 800210,during Normal Startup,Control Rod 5-11 Absolute Position Indication Declared Inoperable.Caused by Numerous Asymmetric Rod Alarms.Data from Current Failure Evaluated | /03L-0:on 800210,during Normal Startup,Control Rod 5-11 Absolute Position Indication Declared Inoperable.Caused by Numerous Asymmetric Rod Alarms.Data from Current Failure Evaluated | | | 05000346/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000346/LER-1980-016-03, /03L-0:on 800213,while Reviewing Station Log,Shift Foreman Discovered That Containment Airlock Seal Leakage Test Had Not Been Performed After Last Entry Into Containment During Startup.Caused by Procedural Inadequacy | /03L-0:on 800213,while Reviewing Station Log,Shift Foreman Discovered That Containment Airlock Seal Leakage Test Had Not Been Performed After Last Entry Into Containment During Startup.Caused by Procedural Inadequacy | | | 05000346/LER-1980-017-03, /03L-0:on 800217,operations Personnel Noted That Safety Features Actuation Sys Channel 3 Borated Water Storage Tank Level Indication Was Six Feet Higher than Other Meters.Caused by Freezing of Transmitter Sensing Line | /03L-0:on 800217,operations Personnel Noted That Safety Features Actuation Sys Channel 3 Borated Water Storage Tank Level Indication Was Six Feet Higher than Other Meters.Caused by Freezing of Transmitter Sensing Line | | | 05000346/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000346/LER-1980-018-03, /03L-0:on 800226,safety Features Actuation Sys Channel 3 Borated Water Storatge Tank Level Indication Was Discovered Reading Four Feet Higher than Other Three Channels.Caused by Inadequate Design of Freeze Protection | /03L-0:on 800226,safety Features Actuation Sys Channel 3 Borated Water Storatge Tank Level Indication Was Discovered Reading Four Feet Higher than Other Three Channels.Caused by Inadequate Design of Freeze Protection | | | 05000346/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000346/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000346/LER-1980-019-01, /01T-0:on 800325 Reactor Flux/Flow Trip Setpoints Were Not Verified to Be Properly Reset within 4-h of Manual Shutdown of Rcp.Caused by Attention Given to Feedwater Swings.Trip Setpoints Verified Later | /01T-0:on 800325 Reactor Flux/Flow Trip Setpoints Were Not Verified to Be Properly Reset within 4-h of Manual Shutdown of Rcp.Caused by Attention Given to Feedwater Swings.Trip Setpoints Verified Later | | | 05000346/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000346/LER-1980-020-03, /03L-0:on 800306,control Operator Noted No Control Room Indication for Containment Vacuum Relief Isolation Valve CV5072.Caused by Breaker BE1139 Being Closed,Probably Resulting from Someone Bumping Into Breaker | /03L-0:on 800306,control Operator Noted No Control Room Indication for Containment Vacuum Relief Isolation Valve CV5072.Caused by Breaker BE1139 Being Closed,Probably Resulting from Someone Bumping Into Breaker | | | 05000346/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000346/LER-1980-021-03, /03L-0:on 800313,during Diesel Fire Protection Pump Weekly Test,Pump Could Not Be Stopped W/Control Button. 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Once Stopped,Pump Could Not Be Started.Cause Not Determined by Scheme Check.Retrial of Pump Proved Successful | | | 05000346/LER-1980-022-03, /03L-0:on 800317,operations Personnel Noticed Loss of Control Room Indication for Containment Dihydrogen Analyzer 2 Discharge Line Valve CV5010E.Caused by Const Personnel Accidentally Opening Breaker | /03L-0:on 800317,operations Personnel Noticed Loss of Control Room Indication for Containment Dihydrogen Analyzer 2 Discharge Line Valve CV5010E.Caused by Const Personnel Accidentally Opening Breaker | | | 05000346/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000346/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000346/LER-1980-023-03, /03L-0:on 800327,discovered That Control Rod Groups 3 & 4 Were Moving in on Their Own.Group 3 Was 0% Withdrawn.Group 4 Was 90% Withdrawn.Caused by Component Failure.Component Replaced | /03L-0:on 800327,discovered That Control Rod Groups 3 & 4 Were Moving in on Their Own.Group 3 Was 0% Withdrawn.Group 4 Was 90% Withdrawn.Caused by Component Failure.Component Replaced | | | 05000346/LER-1980-024-03, /03L-0:on 800327,following Normally Initiated Reactor Trip,Auxiliary Feed Pump Turbine 1-2 Main Steam Isolation Valve MS-107 Closed.Cause Unknown.Further Investigation of Valve & Operator Will Be Pursued | /03L-0:on 800327,following Normally Initiated Reactor Trip,Auxiliary Feed Pump Turbine 1-2 Main Steam Isolation Valve MS-107 Closed.Cause Unknown.Further Investigation of Valve & Operator Will Be Pursued | | | 05000346/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000346/LER-1980-025-03, /03X-1:on 800330,control Rod Group 5,rod 11 Absolute Position Indication Declared Inoperable.Caused by Fluctuating Signals Resulting in Numerous Asymmetric Rod Alarms Due to Defective Reed Switch Assemblies | /03X-1:on 800330,control Rod Group 5,rod 11 Absolute Position Indication Declared Inoperable.Caused by Fluctuating Signals Resulting in Numerous Asymmetric Rod Alarms Due to Defective Reed Switch Assemblies | | | 05000346/LER-1980-025, Forwards LER 80-025/03X-1 | Forwards LER 80-025/03X-1 | |
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