05000366/LER-1980-155-03, /03L-0:on 801111,RHR Test Line Isolation Valve 2E11-FO24B & Condensate Drain Isolation Valve 2B21-F16 Found to Be Leaking.Cause Unknown.Investigation Underway.Valves Will Be Repaired Prior to Startup

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/03L-0:on 801111,RHR Test Line Isolation Valve 2E11-FO24B & Condensate Drain Isolation Valve 2B21-F16 Found to Be Leaking.Cause Unknown.Investigation Underway.Valves Will Be Repaired Prior to Startup
ML19345D870
Person / Time
Site: Hatch 
Issue date: 12/09/1980
From: Coggin C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19345D864 List:
References
LER-80-155-03L, LER-80-155-3L, NUDOCS 8012170637
Download: ML19345D870 (2)


LER-1980-155, /03L-0:on 801111,RHR Test Line Isolation Valve 2E11-FO24B & Condensate Drain Isolation Valve 2B21-F16 Found to Be Leaking.Cause Unknown.Investigation Underway.Valves Will Be Repaired Prior to Startup
Event date:
Report date:
3661980155R03 - NRC Website

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61 DOCKET NUVSEH 6d 69 EVENT OATE 74 75 REPOHT O ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h IO l2l l 0n 11-7-80, with Unit 2 in cold shutdown an LLRT by procedure HNP-2-3952

[ O ; 3, lwas performed on the RHR test line isolation valve.2E11-F024B and the l

l condensate drain isolation valv-2B21-F016.

On 11-11-8b, the LLRT co-l 0 4 lO lst I ordinator reviewed the tests and determined that both valves were leak-l 101s 1 I i ng in excess of specified acceptance criteria.

This is a repetitive i

10171 I occurrence - see LER 50-366/1980-154.

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s-3J 34 35 3ti 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11101 I The cause of the leakaoes is unknown at oresent.

Investiaation is un-l 1 i Iderwav: an update report will be submitted.

The valves will be ren-I ITTTl I a i re d p ri o r to s t a r t u o.

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50-366/1980-155 Licensee:

Ceorgia Power Company Facility Name:

Edwin I.

Hatch Docket #: '30-366

Narrative

Report for LER 50-366/1980-155 Gn 11-7-80, with Unit 2 it cold shutdown, a local leak rate test, per procedure HNP-2-3952, " Primary Containment Periodic performed on the RhR Type B and Type C Leakage Tests," was oest line isol,ation valve 2E11-F024B and the condensate drain isolation valve 2B21-F016.

On 11 8 0',

t h e LLRT coordinator reviewed the test data sheets and determined that both valve eriteria,, The RRR test l'eakages exceeded specified acceptance n line isolation valve 2E11-F024B leaka'ge of 6027 accci-wou1dl 3

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i 30-da sealed water-inventory acceptance.

have caused that t oru s'y water valves specified by 10CFR50

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criteria for all section III.C.3 to be exceeded.

The 200 acem leakage of the condensate drain isolation valve 2B21-F016 was such that the

.009 La (544 acem) overall allowable leakage limit for bypass specified by Tech Specs 3.6.1.2.B.2 would path penetration as see LER repetitive occurrence have been exceeded.

This is a 50-366/1980-154.

There were no effects on public health or safety due to this event.

The cause of the leakages is unknown at present.

Investiga-tion is underway; an update report will be submitted.

The valves will be repaired prior to startup.

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