LER-1980-053, Discovered Leak on Heat Exchanger During Steady State Operation.Caused by Leaking Inner Head Gasket on RHR Heat Exchanger Due to Loose Flange Nuts.Gasket Replaced & New Nuts W/Locking Tabs Installed |
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8 60 el QQCK ET NUM8 ER 64 69 EvtNT OATE 74 79 REPGRT DAT E 40 EVENT CESCRIPTION AND PROBABLE CONSEGUENCES h Iot2i lWith unit in steady state operation it was found durine TI-36A that there was leak on I go,3, lthe 2C heat exchanger. Redundant systems were available. There waP no public health l in14; l hazard.
See technical specification 3.5.B.S.
Previous occurrences
BFRO-50-259/7823.I io,3, l8043; 260/8033, 8034, 8035.
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40 el 42 43 44 47 CAUSE OESCRIPTION AND CCARECTIVE ACTICM h l i l o l lCause was a leakine inner head nasket on the PER heat evchancer due to loose flance I i i i i Inuts resulting from thernal eyelint and vibratien. The m ket un, en1 n pa _ m A l
i,#71 inew nuts with lockine tabs were installed. The heat exchancer was then satisfactorfiv i til,Iltested per MMI-49.
The addition of lockine tabs was the recurrence control.
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Tir.n.ssro *.'t.11ey Authority Form DF-17 Browns Ferry Nuclear Plant BF 15.2 3/24/81 LER SUPPLEMENTAL INFORMATION BFRO-50 260 /_80053R1 Technical Specification Involved 3.5.B.5 Reported Under Technical Specification
- 6. 7. 2. b (2)
Date of Occurrence 12/5/80 Time of Occurrence 1240 Unit 2
Identification and Description of Occurrence:
During routine test TI-36A, it was found that RHR heat exchanger 2C was leaking.
Cenditions Prior to Occurrence:
Unit 1 at 99% steady state power.
i Unit 2 at 97% steady state power Unit 3 refuel outage Action specified in the Technical Specification Surveillance Requirements met due to inoperable ecuipment. Describe.
Perforned testing required by Tech. Spec. 4.5.B.5 Apparent Cause of Occurrence:
Leaking inner head gasket due to loose flange nuts caused by thermal cpeling and vibration.
Analysis of Occurrence:
There was no danger to the health or safety of the public, no damage to plant or equipment and no resulting significant chain of events.
Ccerective Action:
The gasket was replaced and new nuts with locking tabr ere used to hold the gasket in place. The heat exchanger was then tested par F0!I-49.
Failure Dat:1:
259/8043, 259/7823, 260/8033, 260/8034, 260/8035.
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Period - Lifetime; Responribility - Document Centrol Supervisor I4[
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ATTACHMENT 2 BFRO-50-260/8053 R1 Recurrent problems have been evident concerning leaking floating head gaskets on the RHR heat exchangers. Apparently thermal cycling and vibration caused loosening of the lock nuts.
Corrective action has consisted of increasing the torque applied to the nuts, installing half size lock nuts, monitoring the RHR system for radiation present, and installing locking tabs.
A report dated February 5, 1981' entitled, " Browns Ferry Nuclear Plant RHR Heat Exchanger Floating Head Stud Tensioning Investigation Report and Recommendations," proposes the following conclusions and recommendations.
Conclusions:
1.
The 750 ft-lb torque applied to the nuts does not exert consistent.
uniform seating stress to the existing gaskets.
2.
There is a possibility of exceeding stud yield tension if the torque is incraased above 750 ft-lbs unless stud elongacion is monitored.
3.
RHR heat exchanger floating heads should be reassembled using stud elongation as the acceptance criteria rather than torque vf_ *e.
Accuracy of the elongation measuring device must be t.001 in.
or less to assure proper stress levels and to detect any relaxation of stress over operating periods.
Recommendations:
1.
Develop an elongation measuring tool and stud end design capable of measuring elongation with a repeatable accuracy of
.001 inch.
2.
Perform 100% baseline measurement on the next coavenient heat exchanger to verify stressed and unstressed stud elongation measure-ment of 0.025 t.002 inches.
3.
Remeasure elongation af ter a minimum of one shutdown cooling cycle comparing measurements to the original stressed condition.
4.
Reassemble RHR heat exchangers 2D and 3C using lock tabs and 0.25 1 002 inches stud elongation.
3.
Revise MM7-49 to reflect these procedures.
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| 05000259/LER-1980-001, Supplemental LER 80-001/01T-1:on 800107,during Performance of Ster 7902 Per IE Bulletin 79-23,diesel Generator 3A Lost Speed Control.Caused by Deteriorated Elastomer Spider Coupling.Spider Coupling Replaced | Supplemental LER 80-001/01T-1:on 800107,during Performance of Ster 7902 Per IE Bulletin 79-23,diesel Generator 3A Lost Speed Control.Caused by Deteriorated Elastomer Spider Coupling.Spider Coupling Replaced | | | 05000259/LER-1980-001-01, /01T-0:on 800107,in Cold Shutdown While Performing Tests Per IE Bulletin 79-28,speed Control on Diesel Generator 3A Was Lost.Caused by Broken Coupling Which Connects Speed Pickup to Generator Shaft.Coupling Replaced | /01T-0:on 800107,in Cold Shutdown While Performing Tests Per IE Bulletin 79-28,speed Control on Diesel Generator 3A Was Lost.Caused by Broken Coupling Which Connects Speed Pickup to Generator Shaft.Coupling Replaced | | | 05000296/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000260/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000296/LER-1980-001-03, /03L-0:on 791230,w/Unit 3 in Shutdown,Bus Tie Board Was de-energized for Startup.Caused by Feeder Cable Failure.Work in Progress to Bypass Bad Cable Sections | /03L-0:on 791230,w/Unit 3 in Shutdown,Bus Tie Board Was de-energized for Startup.Caused by Feeder Cable Failure.Work in Progress to Bypass Bad Cable Sections | | | 05000260/LER-1980-001-03, /03L-0:on 791229,during Normal Operation,While Performing SI 4.2.B-1,switch 1 on Reactor Water Level LITS-3-58D Failed to Operate.Caused by Rendom Failure of Switch in Yarway Model 4418CE.Switch Replaced | /03L-0:on 791229,during Normal Operation,While Performing SI 4.2.B-1,switch 1 on Reactor Water Level LITS-3-58D Failed to Operate.Caused by Rendom Failure of Switch in Yarway Model 4418CE.Switch Replaced | | | 05000259/LER-1980-002-03, /03L-0:on 800112,during Shutdown for Refueling, Wind Direction Channel at 33-ft Elevation Failed Upscale. Caused by Lightning Damage at Meteorological Tower.Series 312D Millivolt to Current Converter Repaired | /03L-0:on 800112,during Shutdown for Refueling, Wind Direction Channel at 33-ft Elevation Failed Upscale. Caused by Lightning Damage at Meteorological Tower.Series 312D Millivolt to Current Converter Repaired | | | 05000259/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000260/LER-1980-002-03, /03L-0:on 791222,w/unit in Cold Shutdown,Found That Flow Control Valve 2-FCV-68-79 on Recirculation Sys Would Not Operate.Caused by Motor Pinion Gear Being Installed Backwards.Installment Procedures Will Be Revised | /03L-0:on 791222,w/unit in Cold Shutdown,Found That Flow Control Valve 2-FCV-68-79 on Recirculation Sys Would Not Operate.Caused by Motor Pinion Gear Being Installed Backwards.Installment Procedures Will Be Revised | | | 05000296/LER-1980-002-03, /03L-0:on 800117,while Performing Surveillance Instruction 4.5.B.1.d,residual Heat Removal Sys Flow Control Valve FCV.74-73 Tripped in mid-position.Caused by Valve Stem Lubricant Losing Lubricity,Causing Force on Motor | /03L-0:on 800117,while Performing Surveillance Instruction 4.5.B.1.d,residual Heat Removal Sys Flow Control Valve FCV.74-73 Tripped in mid-position.Caused by Valve Stem Lubricant Losing Lubricity,Causing Force on Motor | | | 05000260/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000296/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000260/LER-1980-003, Updated LER 80-03L/01X-1:on 800914,during EOC-3 Fuel Shuffling Operations,Fuel Assemblies Tz 758 & Tz 399 Discovered Misoriented 90 Degrees.Caused by Misorientation of 16 Fuel Assemblies During Previous Refueling Outage | Updated LER 80-03L/01X-1:on 800914,during EOC-3 Fuel Shuffling Operations,Fuel Assemblies Tz 758 & Tz 399 Discovered Misoriented 90 Degrees.Caused by Misorientation of 16 Fuel Assemblies During Previous Refueling Outage | | | 05000259/LER-1980-003-03, /03L-0:on 800112,while Performing Local Leak Rate Testing During Refueling Shutdown,Path Leakage Through MSIVs for 3 of 4 Main Steam Lines Exceeded Leak Rate Per Tech Specs.Caused by Normal Wear & Erosion | /03L-0:on 800112,while Performing Local Leak Rate Testing During Refueling Shutdown,Path Leakage Through MSIVs for 3 of 4 Main Steam Lines Exceeded Leak Rate Per Tech Specs.Caused by Normal Wear & Erosion | | | 05000296/LER-1980-003-03, /03L-0:on 800126,while Performing Control Rod Exercise,Control Rod 18-55 Would Not Insert W/Normal Drive Pressure.Caused by Failed Seal in Hydraulic Control Unit Directional Control Valve.Valve Repaired | /03L-0:on 800126,while Performing Control Rod Exercise,Control Rod 18-55 Would Not Insert W/Normal Drive Pressure.Caused by Failed Seal in Hydraulic Control Unit Directional Control Valve.Valve Repaired | | | 05000260/LER-1980-003-03, /03L-0:on 800122,during Normal Operation,Momentary Breach of Secondary Containment Occurred When Air Lock Doors Between Turbine & Reactor Bldg Were Simultaneously Opened.Caused by Misaligned Latch Lock & Latch Bolt | /03L-0:on 800122,during Normal Operation,Momentary Breach of Secondary Containment Occurred When Air Lock Doors Between Turbine & Reactor Bldg Were Simultaneously Opened.Caused by Misaligned Latch Lock & Latch Bolt | | | 05000296/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000259/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000260/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000296/LER-1980-004-03, /03L-0:on 800129,4160 Volt Bus Tie Board de-energized & Restored to Normal Cooling Tower Transformer Feeder.Caused by Need to Return Electrical Sys to Normal Configuration.No Recurrence Control Required | /03L-0:on 800129,4160 Volt Bus Tie Board de-energized & Restored to Normal Cooling Tower Transformer Feeder.Caused by Need to Return Electrical Sys to Normal Configuration.No Recurrence Control Required | | | 05000296/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000259/LER-1980-004-01, /01T-0:on 800118,during Refueling Outage,Ndt Insp Revealed Linear Indication 7/8 Inch Long in Reactor or Water clean-up Sys Weld DRWC-1-2.Cause Unknown.Defect Will Be Removed & Weld Repaired Prior to Startup | /01T-0:on 800118,during Refueling Outage,Ndt Insp Revealed Linear Indication 7/8 Inch Long in Reactor or Water clean-up Sys Weld DRWC-1-2.Cause Unknown.Defect Will Be Removed & Weld Repaired Prior to Startup | | | 05000260/LER-1980-004-03, /03L-0:on 800122,reactor Water Level Switch LIS-3- 203D Switch 2 Exceeded Tech Spec Limit During Normal Operation.Caused by Model 288A Switch Drifting Above Setpoint.Switch Tested,Inspected & Recalibr | /03L-0:on 800122,reactor Water Level Switch LIS-3- 203D Switch 2 Exceeded Tech Spec Limit During Normal Operation.Caused by Model 288A Switch Drifting Above Setpoint.Switch Tested,Inspected & Recalibr | | | 05000259/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000296/LER-1980-005-03, /03L-0:on 800205,during Normal Operation,Fcv 74-73 Found Inoperable While Performing Surveillance Instruction. Caused by Random Failure of Gear Tooth in Limit Switch,Size SMB-2,Model 3-G.Limit Switch Replaced | /03L-0:on 800205,during Normal Operation,Fcv 74-73 Found Inoperable While Performing Surveillance Instruction. Caused by Random Failure of Gear Tooth in Limit Switch,Size SMB-2,Model 3-G.Limit Switch Replaced | | | 05000260/LER-1980-005-03, /03L-0:on 800125,while Performing Special Instruction 4.2.B-1 During Normal Operation,Switches 1,2 & 4 on LIS-3-58A Did Not Operate at Proper Setpoint.Caused by Switch 4 Hanging on Magnet.Switches Adjusted | /03L-0:on 800125,while Performing Special Instruction 4.2.B-1 During Normal Operation,Switches 1,2 & 4 on LIS-3-58A Did Not Operate at Proper Setpoint.Caused by Switch 4 Hanging on Magnet.Switches Adjusted | | | 05000260/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000259/LER-1980-005, Forwards LER 80-005/01T-0 | Forwards LER 80-005/01T-0 | | | 05000296/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000259/LER-1980-005-01, /01T-0:on 800118,during Refueling Outage,While Performing Insp Per IE Bulletin 79-14,found No Seismic Restraints in Drywell of Reactor Bldg Closed Cooling Water 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800203,while Running Electrical Checks on Recirculation Pump,Reactor Recirculation Pump 2A Was Accidentally Tripped.Caused by Misinterpretation of Labels on Recirculation Pump Trip Breakers | | | 05000296/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000260/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000259/LER-1980-006-03, /03L-0:on 800122,during Refueling Operations, Control Rod Driveline Accumulator Level Switch LS-1-305-129 on Unit 38-11 Was Found Inoperable.Caused by Broken Reed Switch.Switch Replaced | /03L-0:on 800122,during Refueling Operations, Control Rod Driveline Accumulator Level Switch LS-1-305-129 on Unit 38-11 Was Found Inoperable.Caused by Broken Reed Switch.Switch Replaced | | | 05000259/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000260/LER-1980-007-03, /03L-0:on 800203,during Normal Operation,Reactor Recirculation Pump 2B Tripped.Caused by Pickup of Recirculation Motor Generator Set Generator Stator Temp Relay.Tests Run,No Problems Found | /03L-0:on 800203,during Normal Operation,Reactor Recirculation Pump 2B Tripped.Caused by Pickup of Recirculation Motor Generator Set Generator Stator Temp Relay.Tests Run,No Problems Found | | | 05000296/LER-1980-007-03, /03L-0:on 800301,after Offsite Power Was Restored to 4-kV Bus Tie Board,Short Period of Time Elapsed Before Reclosure of Bus Tie Boarder Feeder Breaker.Apparent Disagreement in Time Is Still Being Investigated | /03L-0:on 800301,after Offsite Power Was Restored to 4-kV Bus Tie Board,Short Period of Time Elapsed Before Reclosure of Bus Tie Boarder Feeder Breaker.Apparent Disagreement in Time Is Still Being Investigated | | | 05000260/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000259/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000259/LER-1980-007-03, /03L-0:on 800125,while Performing SI 4.2.A-16, Calibr Reactor Bldg Isolation &/Or Logic Timers,B Logic Channel Did Not Isolate.Caused by Intermittent Sticking of Relay R1B Resulting in Time Delay Contacts Being Closed | /03L-0:on 800125,while Performing SI 4.2.A-16, Calibr Reactor Bldg Isolation &/Or Logic Timers,B Logic Channel Did Not Isolate.Caused by Intermittent Sticking of Relay R1B Resulting in Time Delay Contacts Being Closed | | | 05000296/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000296/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000260/LER-1980-008-31, /03L-0:on 800206,while Conducting Automatic Depressurization Sys Logic Functional Test,Relay 10A-K26 Manually Operated in Place of Relay 2E-K26 Causing Recirculation Pump 2B Trip.Caused by Operator Error | /03L-0:on 800206,while Conducting Automatic Depressurization Sys Logic Functional Test,Relay 10A-K26 Manually Operated in Place of Relay 2E-K26 Causing Recirculation Pump 2B Trip.Caused by Operator Error | | | 05000296/LER-1980-008-03, /03L-0:on 800402,3B Diesel Generator Governor Actuator Would Not Respond Properly During Operability Surveillance Instruction.Cause Unknown.Oil Contamination Suspected.Sump Flushed & Refilled | /03L-0:on 800402,3B Diesel Generator Governor Actuator Would Not Respond Properly During Operability Surveillance Instruction.Cause Unknown.Oil Contamination Suspected.Sump Flushed & Refilled | | | 05000259/LER-1980-008, Forwards Updated LER 80-008/03L-1 | Forwards Updated LER 80-008/03L-1 | | | 05000260/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000259/LER-1980-008-03, During Scheduled Refueling Outage,Hpci Turbine Had Crack in Coupling Bearing Support Pedestal.Possibly Caused by Water Hammer in Main Steam Supply Line | During Scheduled Refueling Outage,Hpci Turbine Had Crack in Coupling Bearing Support Pedestal.Possibly Caused by Water Hammer in Main Steam Supply Line | | | 05000296/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000296/LER-1980-009-03, /03L-0:on 800404,during Normal Operation,Relay 16A-K63B Overheated & Failed,Blowing Fuse Causing Containment Isolation Sys Group 6 Valves to Fail Closed. Caused by Natural Aging of Relay.Relay & Fuse Replaced | /03L-0:on 800404,during Normal Operation,Relay 16A-K63B Overheated & Failed,Blowing Fuse Causing Containment Isolation Sys Group 6 Valves to Fail Closed. Caused by Natural Aging of Relay.Relay & Fuse Replaced | |
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