LER-1982-020, During Normal Operation, Unidentified Drywell Leakage Increased & Exceeded Limits. Caused by vibration-induced Fatigue Crack in Reactor Water Cleanup Sys Test Connection.Line Rerouted |
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NRC FORM 36S U. S. NUCLE AP REGULATORY COMMISSION 87 M UPDATE REPORT, LICENSEE EVENT REPORT PREVIgDS RLFORT DATE 7/22/82
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7 8 9 LICENSEE CODE 14 15 LICENSE NUMUER 25 26 LICENSE TYPE JO 67 CAT $8 CON'T l0l1l
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60 61 DOCK ET NUMB ER 68 63 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h [O 7 71-1 Durine normal operation. unidentified drvve11 leakane as determined bv flow l
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recorder and flow' integrator suddenly increased and exceeded limits specified 101. l l in T.S.
3.6.C.1.
In accordance with T.S.
3.6.C.3 an orderly shutdown was I
10151I initiated and the reactor was in cold shutdown condition within ~ 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
There I
10 ls l l was no dancer to the health or enfety of the nublic.
The leakane never l
l0l7ll approached normal makeup canacity.
All enercency systems were available and l
l O 181 I operable.
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CAUSE
CAUSE COMP.
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to it 12 13 18 19 10 SEOUENTIAL OCCURRENCE REPORT REVISION L
EVENT YEAR REPORT NO.
CODE TYPE NO.
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CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h.
I 1 I O I l Leaknee resulted fron a vibration-induced f aticue crack in a 3/4-inch roactor water I
IiiilI cleanun system test connection.
Inndecuate brncini of the test connection line 1
l i 121 l allowed high-frecuency vibration.
The line was rerouted to decrease suscentibility l
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Insp$ tion was completed for similar conditions on unit 3.
Unit 2 1
4 I i ( 4 I l will be inspected durine the evcle 4 refueline outace.
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80 STA S
% POWER OTHER STATUS DSO RY DISCOVERY DESCRIPTION l l 5 l [_gj@ l 0 l 9 l 5 l@l NA l
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COSTENT i2 n
44 4s 40 80 ACnviTY RELEAcEO OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELE ASE l l6l[_Z)h,[Zj@l NA l
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PERSONNEL EXPOSU ES DESCRIPTION @
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7 8 9 13 68 69 80 3 William A. Roberts (205) 729-0788 NAME OF PREPARER PHONE:-
Browns Ferry Nuclear Plant BF 15.2 j
2/17/82 L$R SUPPLEMENTAL INFORMATION
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BFRO _ 259 /_3LO_20 R2 Technical Specification Involved 3.6.c.1 & 3.6.c.3 i
Reported Under Technical Specification _6.7 2.b.(2)* Date Due NRC 5
Event Narrative:
f Unit 1 - 1,045 We (steady state)
Unit 2 - 1,085 We (preconditioning up to full load)
Unit 3 - 0 W e (refuel outage)
During nonnal operation, unidentified drywell leakage as determined by the floor drain sump pump flow from FR-77-6 and flow integrator FQ-77-6 suddenly increased and exceeded limits specified in Technical Specification 3.6.c.1.
In accordance with Technical Specificaticn 3 6.C.3, an orderly shutdown was initiated and the reactor was in cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. There was no danger to the health and safety of the public. All emergency systems were available and operable. An inspection identified the leakage as being from a crack in a 3/4-inch test connection which ties into the 6-inch pipe adjacent to reactor water cleanup I
i system valve FCV-69-1. 2 1s test line and its associated manual isolation valves j
(69-583 and 69-584) were inadequately supported which led to high-frequency fatigue and subsequent cracking of the line.
Repair was made by removing a 90-degree elbow and shortening the line thus orientating the test valves in vertical plane perpendicular to the 6-inch line instead of being orientated in a horizontal plane parallel to the 6-inch pipe. W e crack in the 3/4-inch pipe occurred above a socket weld and extended around approximately 60 percent of the circumference. The broken test line was repaired.
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(see attached page)
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NONE Retention:
?criod - Lifetime; Responsibility - Document Control Supervisor
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1 2-LER SUPPLEMENTAL INFORMATION BFRO-50-259/82020 R2 The average ficw rate'of water from the cracked line was approximately 12 gallons per minute. The total amount or water lost during the event was approximately 17,200 gallons. These values were derived frcm the actual ficw rate as recorded on strip chart FR-77-6 for a 24-hour period on March 20, 1982.
During the inspection to locate the leak, it was noted that this vent connecticn had previously been provided with a vibration support. Support requirements for this vent connection were not snown on TVA drawings. The support had apparently been removed at some time for maintenance or modificaticn work. Reinstallatien had not been performed because vibration support requirements were not shown on 3
design drawings. The fatigue crack occurred because the support had not been reinstalled on the line.
An evaluation of any suspect units 1 and 2 safety-related piping system will be conducted to verify that similar problems do not. exist on other test, vent, or drain connections. If any discrepancies are found, appropriate corrective acticn will be taken. This inspection will be performed during the unit 1, cycle 5 and unit 2-cycle 4 refueling outages presently scheduled for completion July 17, 1983, ana January 30, 1983, respectively.
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| 05000296/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | | 05000259/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | | 05000259/LER-1982-001-03, /03L-0:on 820103,meteorological Instrumentation O-Tdr-90-103 Air Temp Delta T & O-XR-90-102-1 (30 Ft Air Speed) Failed.Caused by Lightning Damage to Transistors Q3 & Q4 & Blown Fuses in Panel 9-34 & at Meterological Station | /03L-0:on 820103,meteorological Instrumentation O-Tdr-90-103 Air Temp Delta T & O-XR-90-102-1 (30 Ft Air Speed) Failed.Caused by Lightning Damage to Transistors Q3 & Q4 & Blown Fuses in Panel 9-34 & at Meterological Station | | | 05000260/LER-1982-001, Forwards LER 82-001/01T-0 | Forwards LER 82-001/01T-0 | | | 05000260/LER-1982-001-01, /01T-0:on 820115,during Offsite Verification of Process Computer Programming Changes Involving Data in Tech Spec Tables 3.5.I-3 & 3.5.I-4,discovered Input Error.Caused by Personnel Error.Personnel Will Be Reinstructed | /01T-0:on 820115,during Offsite Verification of Process Computer Programming Changes Involving Data in Tech Spec Tables 3.5.I-3 & 3.5.I-4,discovered Input Error.Caused by Personnel Error.Personnel Will Be Reinstructed | | | 05000296/LER-1982-001-03, /03L-0:on 820114,fixed Spray Fire Protection Valve Accidentally Initiated,Causing Smoke Detector to Be Wetted & Emit False Smoke Alarm.Caused by Personnel Hanging Coats on Valve Station.Valve Reset & Smoke Detector Replaced | /03L-0:on 820114,fixed Spray Fire Protection Valve Accidentally Initiated,Causing Smoke Detector to Be Wetted & Emit False Smoke Alarm.Caused by Personnel Hanging Coats on Valve Station.Valve Reset & Smoke Detector Replaced | | | 05000259/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000259/LER-1982-002-03, /03L-0:on 820106,drywell High Pressure Switch 1-PS-64-58C Found Isolated.Apparently Caused by Performance of Surveillance Instruction 4.2.B.5.Switch Returned to Normal & All Other Valving Involved Verified Correct | /03L-0:on 820106,drywell High Pressure Switch 1-PS-64-58C Found Isolated.Apparently Caused by Performance of Surveillance Instruction 4.2.B.5.Switch Returned to Normal & All Other Valving Involved Verified Correct | | | 05000296/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000296/LER-1982-002-03, /03L-0:on 820121,during Surveillance Test SI 4.11.C.1 & 5 Smoke Detector in Auxiliary Instrument Room 3 Would Not Alarm.Caused by Loose Annunciator Point Card Due to Incorrect Installation of Retainer Bar | /03L-0:on 820121,during Surveillance Test SI 4.11.C.1 & 5 Smoke Detector in Auxiliary Instrument Room 3 Would Not Alarm.Caused by Loose Annunciator Point Card Due to Incorrect Installation of Retainer Bar | | | 05000260/LER-1982-002-03, /03L-0:on 820116,during Reduced Load While Performing MSIV Closure Si,Scram Trip Logic Az Annunciation Failed to Alarm.Caused by Failure of Limit Switch 4 of FCV-1-52 to Open.Switch Will Be Replaced | /03L-0:on 820116,during Reduced Load While Performing MSIV Closure Si,Scram Trip Logic Az Annunciation Failed to Alarm.Caused by Failure of Limit Switch 4 of FCV-1-52 to Open.Switch Will Be Replaced | | | 05000260/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000260/LER-1982-003-03, /03L-0:on 820116,during Normal Operation,While Performing Surveillance test,PS-3-74A Switch 1 & PS-68-96 Switch 1,low Pressure Switches,Were Out of Tolerance by 4% & 6%.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820116,during Normal Operation,While Performing Surveillance test,PS-3-74A Switch 1 & PS-68-96 Switch 1,low Pressure Switches,Were Out of Tolerance by 4% & 6%.Caused by Instrument Drift.Switches Recalibr | | | 05000260/LER-1982-003, Forwards LER 82-003/03L-0 | Forwards LER 82-003/03L-0 | | | 05000296/LER-1982-003-03, /03L-0:on 820123,during Refueling Outage,While Performing SI 4.2.A-39,temp Switches TS-69-30A,B,C & E on Reactor Cleanup Sys Floor Drain High Temp,Operated at Less than 160 F.Caused by Improper Calibr or Instrument Drift | /03L-0:on 820123,during Refueling Outage,While Performing SI 4.2.A-39,temp Switches TS-69-30A,B,C & E on Reactor Cleanup Sys Floor Drain High Temp,Operated at Less than 160 F.Caused by Improper Calibr or Instrument Drift | | | 05000296/LER-1982-003, Forwards LER 82-003/03L-0 | Forwards LER 82-003/03L-0 | | | 05000296/LER-1982-004, Forwards LER 82-004/03L-0 | Forwards LER 82-004/03L-0 | | | 05000296/LER-1982-004-03, /03L-0:on 820207,while Performing Surveillance Instruction,Temp Switches 3S-TS-73-2A & 3-TS-73-2B Operated Above Tech Specs Limit.Caused by Switches Being Out of Calibr.Switches Calibr | /03L-0:on 820207,while Performing Surveillance Instruction,Temp Switches 3S-TS-73-2A & 3-TS-73-2B Operated Above Tech Specs Limit.Caused by Switches Being Out of Calibr.Switches Calibr | | | 05000296/LER-1982-005, Forwards LER 82-005/03L-0 | Forwards LER 82-005/03L-0 | | | 05000259/LER-1982-005, Forwards Updated LER 82-005/03X-1 | Forwards Updated LER 82-005/03X-1 | | | 05000260/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000260/LER-1982-006-03, /03L-0:on 820125,while Performing SI 4.1.A-7,low Water Level Switch LIS-3-203B,switch 1 Found 3% Out of Tolerance.Caused by Setpoint Drift.Switch Recalibr | /03L-0:on 820125,while Performing SI 4.1.A-7,low Water Level Switch LIS-3-203B,switch 1 Found 3% Out of Tolerance.Caused by Setpoint Drift.Switch Recalibr | | | 05000259/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000259/LER-1982-006-03, /03L-0:on 820112,1-PS-3-74B Switch Number 1 Found Operating Below Tech Spec Limit.Caused by Instrument Drift. Barton Model 288 Pressure Switch Recalibr.Action Plan Re Design Change Will Be Forwarded | /03L-0:on 820112,1-PS-3-74B Switch Number 1 Found Operating Below Tech Spec Limit.Caused by Instrument Drift. Barton Model 288 Pressure Switch Recalibr.Action Plan Re Design Change Will Be Forwarded | | | 05000296/LER-1982-007-03, /03X-1:on 820318,ice Storm Caused Loss of Offsite Power to 4-kV bus-tie Board.Caused by Interruption of Power to Cooling Tower Transformers & 4-kV Switchgear Feeding bus-tie Board Due to Loss of 161-kV Lines | /03X-1:on 820318,ice Storm Caused Loss of Offsite Power to 4-kV bus-tie Board.Caused by Interruption of Power to Cooling Tower Transformers & 4-kV Switchgear Feeding bus-tie Board Due to Loss of 161-kV Lines | | | 05000260/LER-1982-007-03, /03L-0:on 820126,while Performing SI 4.2.A-3, Reactor low-water Level Switch Lis-3-56A Switch Number 2 Was Found 8% Out of Tolerance.Caused by Setpoint Drift.Yarway Model 4418c Switch Recalibr & Functionally Tested | /03L-0:on 820126,while Performing SI 4.2.A-3, Reactor low-water Level Switch Lis-3-56A Switch Number 2 Was Found 8% Out of Tolerance.Caused by Setpoint Drift.Yarway Model 4418c Switch Recalibr & Functionally Tested | | | 05000260/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | | 05000296/LER-1982-007, Forwards LER 82-007/03X-1 | Forwards LER 82-007/03X-1 | | | 05000259/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | | 05000259/LER-1982-007-03, /03L-0:on 820113,XR-90-104 Lost Indication for Wind Direction & Wind Speed Channel C,Elevation 887 Msl. Caused by Anemometer & Vane Icing Due to Inclement Weather. Anemometer & Vane Allowed to Thaw | /03L-0:on 820113,XR-90-104 Lost Indication for Wind Direction & Wind Speed Channel C,Elevation 887 Msl. Caused by Anemometer & Vane Icing Due to Inclement Weather. Anemometer & Vane Allowed to Thaw | | | 05000259/LER-1982-008, Forwards LER 82-008/03L-0 | Forwards LER 82-008/03L-0 | | | 05000296/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000259/LER-1982-008-03, /03L-0:on 820116,CAM 1-90-250 (Refuel Floor) Rendered Inoperable Due to Broken Drive Belt.Caused by Normal Wear Due to Continuous Operation.Std V-belt for Schwitzer Model 325 Series Air Pump Replaced | /03L-0:on 820116,CAM 1-90-250 (Refuel Floor) Rendered Inoperable Due to Broken Drive Belt.Caused by Normal Wear Due to Continuous Operation.Std V-belt for Schwitzer Model 325 Series Air Pump Replaced | | | 05000296/LER-1982-008-03, /03L-0:on 820331,while Performing Daily Source & Background Check of CAM-390-250,reactor & Turbine Bldg Vent Monitor,Inlet Sample Line Discovered Disconnected.Caused by Personnel Error.Sample Lines Reconnected | /03L-0:on 820331,while Performing Daily Source & Background Check of CAM-390-250,reactor & Turbine Bldg Vent Monitor,Inlet Sample Line Discovered Disconnected.Caused by Personnel Error.Sample Lines Reconnected | | | 05000260/LER-1982-008-03, /03L-0:on 820127,after Calibr,Rod Block Monitor Channel B Failed to Pass Functional Test of SI 4.2.C-2. Caused by Electronic IC Failure Possibly Due to Voltage Spike During Calibr.Ge 136B1333G1 Gain Change Card Replaced | /03L-0:on 820127,after Calibr,Rod Block Monitor Channel B Failed to Pass Functional Test of SI 4.2.C-2. Caused by Electronic IC Failure Possibly Due to Voltage Spike During Calibr.Ge 136B1333G1 Gain Change Card Replaced | | | 05000260/LER-1982-008, Forwards LER 82-008/03L-0 | Forwards LER 82-008/03L-0 | | | 05000259/LER-1982-009-03, /03L-0:on 820117,during Normal Operation,Smoke Detector in Relay Room Alarmed & Would Not Clear.Caused by Increased Detector Sensitivity Due to Natural Aging.Kidde FT-200 Ionization Smoke Detector Replaced | /03L-0:on 820117,during Normal Operation,Smoke Detector in Relay Room Alarmed & Would Not Clear.Caused by Increased Detector Sensitivity Due to Natural Aging.Kidde FT-200 Ionization Smoke Detector Replaced | | | 05000259/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000296/LER-1982-009-03, /03L-0:on 820407,during Refueling Outage,While Performing SI 4.2.A.6,pressure Switches 3-PS-1-76 & 3-PS-1-82 Had as-found Setpoints of 815.7 Psig & 813.7 Psig, Respectively.Caused by Setpoint Drift.Switches Recalibr | /03L-0:on 820407,during Refueling Outage,While Performing SI 4.2.A.6,pressure Switches 3-PS-1-76 & 3-PS-1-82 Had as-found Setpoints of 815.7 Psig & 813.7 Psig, Respectively.Caused by Setpoint Drift.Switches Recalibr | | | 05000296/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000259/LER-1982-010-03, /03L-0:on 820112,stack Monitor Was Declared Inoperable After Low Flow Alarm.Caused by 6 Ft Segment of Sample Line Freezing,Inhibiting Sampling Flow to Monitor | /03L-0:on 820112,stack Monitor Was Declared Inoperable After Low Flow Alarm.Caused by 6 Ft Segment of Sample Line Freezing,Inhibiting Sampling Flow to Monitor | | | 05000259/LER-1982-010, Forwards LER 82-010/03L-0 | Forwards LER 82-010/03L-0 | | | 05000296/LER-1982-010-03, /03L-0:on 820406,during Refueling & Routine Performance of SI 4.2.F-10,pressure Switch 3-PS-64-67 Had as-found Calibr of 35.5 Psig.Caused by Setpoint Drift.Model 50-560-111AAAC1 Alarm Recalibr | /03L-0:on 820406,during Refueling & Routine Performance of SI 4.2.F-10,pressure Switch 3-PS-64-67 Had as-found Calibr of 35.5 Psig.Caused by Setpoint Drift.Model 50-560-111AAAC1 Alarm Recalibr | | | 05000296/LER-1982-010, Forwards LER 82-010/03L-0 | Forwards LER 82-010/03L-0 | | | 05000260/LER-1982-010, Corrected LER 82-010/03L-0 on 811021,during Full Power,Avg Power Range Monitor Output Signal Calibr Was Not Performed within Required Frequency During 811014-28.Caused by Personnel Error.Personnel Instructed to Be More Careful | Corrected LER 82-010/03L-0 on 811021,during Full Power,Avg Power Range Monitor Output Signal Calibr Was Not Performed within Required Frequency During 811014-28.Caused by Personnel Error.Personnel Instructed to Be More Careful | | | 05000260/LER-1982-010-03, /03L-0:on 820121,during Full Power Operation SI 4.1.B.2 (APRM Output Signal Calibr) Not Performed within Required Frequency During 811014-28.Caused by Personnel Error | /03L-0:on 820121,during Full Power Operation SI 4.1.B.2 (APRM Output Signal Calibr) Not Performed within Required Frequency During 811014-28.Caused by Personnel Error | | | 05000260/LER-1982-011, Forwards LER 82-011/03L-0 | Forwards LER 82-011/03L-0 | | | 05000259/LER-1982-011, Forwards LER 82-011/03L-0 | Forwards LER 82-011/03L-0 | | | 05000296/LER-1982-011, Forwards LER 82-011/01T-0 | Forwards LER 82-011/01T-0 | | | 05000296/LER-1982-011-01, /01T-0:on 820414,while Performing SI 4.1.A-7 Reactor Protection Sys Water Level Switches 3-LIS-3-203A, 203B & 203D Operated Out of Tech Spec Allowance.Caused by Setpoint Drift | /01T-0:on 820414,while Performing SI 4.1.A-7 Reactor Protection Sys Water Level Switches 3-LIS-3-203A, 203B & 203D Operated Out of Tech Spec Allowance.Caused by Setpoint Drift | |
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