05000366/LER-1982-143-03, /03L-0:on 821215,personnel Found Fire Protection Isolation Valves - Position & Lubrication Checks Procedure Performed 2 Days Late.Caused by Personnel Error.Personnel Admonished as to Importance of Surveillance

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/03L-0:on 821215,personnel Found Fire Protection Isolation Valves - Position & Lubrication Checks Procedure Performed 2 Days Late.Caused by Personnel Error.Personnel Admonished as to Importance of Surveillance
ML20028E066
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 01/11/1983
From: Tipps S
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028E063 List:
References
LER-82-143-03L, LER-82-143-3L, NUDOCS 8301200319
Download: ML20028E066 (1)


LER-1982-143, /03L-0:on 821215,personnel Found Fire Protection Isolation Valves - Position & Lubrication Checks Procedure Performed 2 Days Late.Caused by Personnel Error.Personnel Admonished as to Importance of Surveillance
Event date:
Report date:
3661982143R03 - NRC Website

text

,

NPC F0FtM 366.

U. S. NUCLEAR REGULATORY COMMISSION tr.m LICENSEE EVENT REPORT 1

CONTROL BLOCK: l l

l l

l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

lo l 1 l l G l A l E l I l H l 2 l@l 0 l 0 I - 10 l 0 l 0 l 0 l 0 l-l 0 l 0 l@l 4 i l l 1 l 1 l 1 l@l l

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7 8 9 LICENSEE CODE 14 15 LICENSE NUM8ER 25 26 LICENSE TYPE 30 57 CAT 58 CbN'T IOIiI 3ggy l L l@l 0 l 5 l 0 l 0 l 0 l 3 l 6 l 6 @l 1 l 2 l 1 l 5 l 8 l 2 @l0 l1 l1 l 1 l 8 l 3 l@

7 8

60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121lon 12-15-82 while reviewina surveillance data. personnel found the I

lolal l" FIRE PROTECTION ISOLATION VALVES - POSITION AND LUBRICATION CHECKS",

l 1o141l Procedure was performed two days late. This is a failure to meet T.S. - 1e l o i s i 14. 7.6.1.c. which requires verifying at least every 31 days that each l

IOlslIvalve in the flow path for the fire suppression water system is in its 1

10l71lcorrect position. The health and safety of the public were not affected.1 l O 181 lThis event is repetitive as last reported by LER 50-366/1982-137.

I 7

8 9 80 DE CODE S BC E COMPONENT CODE SU8 CODE S

E lol9l l A l B l @ W @ W @ l Z l Zl Z l Z l Z l Z lh [_Z_j @ [Z_l @

7 8

9 10 11 12 13 18 19 20 SEQUEN TI AL OCCUR R E NCE REPORT REVISION

_ EVENT YE AR REPORT NO.

CODE TYPE N O.

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l 0l 31 [L l

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_ 21 22 23 24 26 27 28 29 30 31 32 TAKEf A T N ON PL NT T

HOURS 22 S8 li FOR 8.

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JJ 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11101lThe cause of this event was attributed to personnel error.

Personnel l

litiil received and entered incorrect completion date into the surveillance I

j, g7i l computer, causing an incorrect surveillance due date on subsequent l

lijajl computer printout.

All responsible personnel were admonished as to l

l limportance of reporting and performing surveillance accurately.

l i 4 l

7 8 9 80 STA S

  • sPOWER OTHER STATUS IS O RY D'SCOVERY DESCRIPTION l i l 5 l b@ l 1 l 0 l 0 l@l NA l

l A l@l Surveillance Data Review l

ACTIVITY CONTENT HELE ASED OF RE LE ASE AYOUNT OF ACTIVITY LOCATION OF RELEASE LZ_l @ lZ_1@l NA l

l NA l

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7 8 9 10 11 44 45 80 PE HSONNE L i XPOSUHES NUPAR E H TYPE D E SCRIP TION ;

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PE n sONN A'imUJ,E S DESCniPriON@

..UveEn l li Is l 10101 ol@l NA l

7 8 9 11 12 80 i OSS OF OH DAMAGE TO F ACILt TY tvPE D E SC HIP T ION LZJ@l NA l

i o PUHLI YY c

9301200319 830111 NRC USE ONLY PDR ADOCK 05000366 issue n@lotScniP Tion U LNj S

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R 3 10 68 69 80 5 NAME OF PHCPAREH

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