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| 05000331/LER-1985-001, :on 850123,reactor Water Cleanup Sys Isolated Twice as Result of Momentary Spurious Signals from Reactor Water Cleanup Leak Detection Instrumentation.Cause Not Stated.Sys Will Be Tested in Refuel Outage |
- on 850123,reactor Water Cleanup Sys Isolated Twice as Result of Momentary Spurious Signals from Reactor Water Cleanup Leak Detection Instrumentation.Cause Not Stated.Sys Will Be Tested in Refuel Outage
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| 05000331/LER-1985-002, :on 850128,HPCI Declared Inoperable Due to Failure of Turbine Stop Valve to Open During Monthly Surveillance Test.Caused by Pilot Oil Trip Solenoid Valve Being Stuck in Open Position.Valve Replaced |
- on 850128,HPCI Declared Inoperable Due to Failure of Turbine Stop Valve to Open During Monthly Surveillance Test.Caused by Pilot Oil Trip Solenoid Valve Being Stuck in Open Position.Valve Replaced
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| 05000331/LER-1985-003, :on 850125,doors of Airlock Between Reactor & Turbine Bldgs Inadvertently Opened Simultaneously.On 850130, Doors of Railroad Airlock Opened Simultaneously.Caused by Bad Solenoid in Interlock Mechanism |
- on 850125,doors of Airlock Between Reactor & Turbine Bldgs Inadvertently Opened Simultaneously.On 850130, Doors of Railroad Airlock Opened Simultaneously.Caused by Bad Solenoid in Interlock Mechanism
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| 05000331/LER-1985-004, :on 850202,reactor Protection Sys Trip Occurred Due to APRM Upscale Trip.Caused by Shorted LPRM W/Common Inputs to APRM Channels a & B.Investigation to Determine Failure Mod Begun |
- on 850202,reactor Protection Sys Trip Occurred Due to APRM Upscale Trip.Caused by Shorted LPRM W/Common Inputs to APRM Channels a & B.Investigation to Determine Failure Mod Begun
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| 05000331/LER-1985-005, :on 850206,four MSIVs Failed to Meet Leakage Criteria of 11.5 Std Cubic Ft/H.Probably Caused by Seat & Disc Wear.Valves Being Repaired |
- on 850206,four MSIVs Failed to Meet Leakage Criteria of 11.5 Std Cubic Ft/H.Probably Caused by Seat & Disc Wear.Valves Being Repaired
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| 05000331/LER-1985-006, :on 850303,while Resetting Isolations & Alarms Resulting from Instrument Panel a Being Deenergized,Standby Diesel Generator a Which Had Not Been Locked Began to auto-start.Generator Secured |
- on 850303,while Resetting Isolations & Alarms Resulting from Instrument Panel a Being Deenergized,Standby Diesel Generator a Which Had Not Been Locked Began to auto-start.Generator Secured
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000331/LER-1985-007, :on 850221,during Disassembly of HPCI Turbine for Overhaul & Insp,Damage & Missing Parts Noted in Several of 10 Steam Reversing Chambers.Caused by Pressure Pulsing & Thermal Fatigue |
- on 850221,during Disassembly of HPCI Turbine for Overhaul & Insp,Damage & Missing Parts Noted in Several of 10 Steam Reversing Chambers.Caused by Pressure Pulsing & Thermal Fatigue
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| 05000331/LER-1985-008, :on 850311,eight Circuit Breakers on Instrument Ac Distribution Panel B Tripped.Caused by Falling Panel Cover Being Replaced Following Maint.Tripped Breakers Reset & Affected Sys Checked |
- on 850311,eight Circuit Breakers on Instrument Ac Distribution Panel B Tripped.Caused by Falling Panel Cover Being Replaced Following Maint.Tripped Breakers Reset & Affected Sys Checked
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| 05000331/LER-1985-009, :on 850315,reactor Protection Sys Actuated Due to Intermediate Range Monitor High Flux Upscale Trips.Caused by Induction Heat Stress Improvement Work Performed on Recirculation Piping.Trips Reset |
- on 850315,reactor Protection Sys Actuated Due to Intermediate Range Monitor High Flux Upscale Trips.Caused by Induction Heat Stress Improvement Work Performed on Recirculation Piping.Trips Reset
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| 05000331/LER-1985-010, :on 850310,piping Ultrasonic Insps Revealed Several Welds in Recirculation Piping W/Circumferential &/Or Axial Indications.Cause Not Stated.Welds Being Repaired W/ Overlays |
- on 850310,piping Ultrasonic Insps Revealed Several Welds in Recirculation Piping W/Circumferential &/Or Axial Indications.Cause Not Stated.Welds Being Repaired W/ Overlays
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| 05000331/LER-1985-011, :on 850321,full Reactor Protection Sys Trip Signal & Isolation Signal Received While Reactor Shut Down & Defueled.Caused by Radiography Source Used During NDT of MSIV C |
- on 850321,full Reactor Protection Sys Trip Signal & Isolation Signal Received While Reactor Shut Down & Defueled.Caused by Radiography Source Used During NDT of MSIV C
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000331/LER-1985-012, :on 850425,w/reactor Shut Down & Defueled,Group III Isolation & Both Standby Gas Treatment Sys auto- Initated on Downscale Reactor Bldg Vent Radiation Monitor Trips.Caused by Procedural Error |
- on 850425,w/reactor Shut Down & Defueled,Group III Isolation & Both Standby Gas Treatment Sys auto- Initated on Downscale Reactor Bldg Vent Radiation Monitor Trips.Caused by Procedural Error
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| 05000331/LER-1985-013, :on 850501,reactor Water Cleanup Sys Isolated on High Differential Flow Condition.Caused by Maint Personnel Bumping Speed Controller.Sys Returned to Normal Svc |
- on 850501,reactor Water Cleanup Sys Isolated on High Differential Flow Condition.Caused by Maint Personnel Bumping Speed Controller.Sys Returned to Normal Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000331/LER-1985-014, :on 850506,standby Gas Treatment Sys Actuated. Caused by Jumper Cable Disconnecting Due to Opening Door Panel.Jumper Reinstalled W/More Secure Mechanism.Isolation & Ventilation Sys Reset |
- on 850506,standby Gas Treatment Sys Actuated. Caused by Jumper Cable Disconnecting Due to Opening Door Panel.Jumper Reinstalled W/More Secure Mechanism.Isolation & Ventilation Sys Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000331/LER-1985-015, :on 850529,w/reactor Shut Down & Electric & Diesel Fire Pumps Removed from Svc,Well Water Pump Aligned for Fire Suppression.On 850531,nearby Fire Main Ruptured. Damaged Piping Isolated & Repaired |
- on 850529,w/reactor Shut Down & Electric & Diesel Fire Pumps Removed from Svc,Well Water Pump Aligned for Fire Suppression.On 850531,nearby Fire Main Ruptured. Damaged Piping Isolated & Repaired
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| 05000331/LER-1985-016, :on 850601,unintentional Momentary Violation of Secondary Containment Occurred & Two Secondary Containment Airlock Doors Simultaneously Opened.Caused by out-of-adjustment Door Interlock Mechanism |
- on 850601,unintentional Momentary Violation of Secondary Containment Occurred & Two Secondary Containment Airlock Doors Simultaneously Opened.Caused by out-of-adjustment Door Interlock Mechanism
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| 05000331/LER-1985-017, :on 850411,during Testing at Wyle Labs,Four Main Steam Safety/Relief Valves Lifted Below Min Allowable Pressure.Caused by Leakage Due to Minor Steam Cutting of Valve Seating Surfaces.Valves Rebuilt |
- on 850411,during Testing at Wyle Labs,Four Main Steam Safety/Relief Valves Lifted Below Min Allowable Pressure.Caused by Leakage Due to Minor Steam Cutting of Valve Seating Surfaces.Valves Rebuilt
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| 05000331/LER-1985-018, :on 850606,reactor Protection Sys Trip Occurred.Caused by Spurious Signal from LPRM Due to Noise Spike During Testing & Reinstallation.Reactor Protection Sys Reset & APRM Channel B Bypassed |
- on 850606,reactor Protection Sys Trip Occurred.Caused by Spurious Signal from LPRM Due to Noise Spike During Testing & Reinstallation.Reactor Protection Sys Reset & APRM Channel B Bypassed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000331/LER-1985-019, :on 850607,control Rods Adjacent to Cell in Which Maint Being Performed Not Electrically Disarmed.Caused by Operator Error.Administrative Duties Lessened & Procedural Mods Instituted |
- on 850607,control Rods Adjacent to Cell in Which Maint Being Performed Not Electrically Disarmed.Caused by Operator Error.Administrative Duties Lessened & Procedural Mods Instituted
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| 05000331/LER-1985-020, :on 850610,inadvertent Reactor Protection Sys Actuation Occurred.Caused by Manual Trip of Supply Feed Breaker,Momentary Upscale Average Power Range Monitor Signal & Scram Discharge Vol Level Signal |
- on 850610,inadvertent Reactor Protection Sys Actuation Occurred.Caused by Manual Trip of Supply Feed Breaker,Momentary Upscale Average Power Range Monitor Signal & Scram Discharge Vol Level Signal
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| 05000331/LER-1985-021, :on 850614,discovered That Spent Fuel Pool 5 Inches Below Tech Spec Level of 36 Ft.Caused by Small leak-through of Cask Pool Drain Valve.Maint Action Requests Initiated to Repair Valves |
- on 850614,discovered That Spent Fuel Pool 5 Inches Below Tech Spec Level of 36 Ft.Caused by Small leak-through of Cask Pool Drain Valve.Maint Action Requests Initiated to Repair Valves
| 10 CFR 50.73(a)(2)(i) |
| 05000331/LER-1985-022, :on 850617 & 20,actuations of Standby Gas Treatment Sys & Half of Group III Primary Containment Isolation Sys Valves Occurred.Caused by Plant Mod & Procedural Deficiency.Procedure Revised |
- on 850617 & 20,actuations of Standby Gas Treatment Sys & Half of Group III Primary Containment Isolation Sys Valves Occurred.Caused by Plant Mod & Procedural Deficiency.Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000331/LER-1985-023, :on 850702,reactor Water Cleanup Sys Isolated as Result of Momentary Spurious Signal in Leak Detection Instrumentation.Again on 850713 & 15,sys Isolated Due to Procedural Deficiency.Procedural Rev Initiated |
- on 850702,reactor Water Cleanup Sys Isolated as Result of Momentary Spurious Signal in Leak Detection Instrumentation.Again on 850713 & 15,sys Isolated Due to Procedural Deficiency.Procedural Rev Initiated
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| 05000331/LER-1985-024, :on 850707,two Reactor Protection Sys Trips Occurred.Caused by Unattached Trip Coil Inside Damping Spring on Feeder Breaker 1B42.Breaker Manufacturer Will Be Notified |
- on 850707,two Reactor Protection Sys Trips Occurred.Caused by Unattached Trip Coil Inside Damping Spring on Feeder Breaker 1B42.Breaker Manufacturer Will Be Notified
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| 05000331/LER-1985-025, :on 850708,inadvertent Steam Line High Radiation Protection Sys Trip Occurred During Surveillance Test.Caused by Procedural Deficiency.Trip Reset & Procedure Permanently Corrected |
- on 850708,inadvertent Steam Line High Radiation Protection Sys Trip Occurred During Surveillance Test.Caused by Procedural Deficiency.Trip Reset & Procedure Permanently Corrected
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000331/LER-1985-026, :on 850522,personnel Identified Two Shock Suppressors (Snubbers) in Installed Configuration That Could Result in Overstressing of Snubber During Dbe.Insp of Snubbers Performed |
- on 850522,personnel Identified Two Shock Suppressors (Snubbers) in Installed Configuration That Could Result in Overstressing of Snubber During Dbe.Insp of Snubbers Performed
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| 05000331/LER-1985-027, :on 850721,fire Watch on HPCI Deluge Sys Discovered Prematurely Canceled 3 Days Earlier.Caused by Ineffective Personnel Communications.Need to Communicate Between Shifts Reemphasized |
- on 850721,fire Watch on HPCI Deluge Sys Discovered Prematurely Canceled 3 Days Earlier.Caused by Ineffective Personnel Communications.Need to Communicate Between Shifts Reemphasized
| 10 CFR 50.73(a)(2)(1) |
| 05000331/LER-1985-028, :on 850720,RCIC Sys Tripped on Overspeed While auto-starting During Monthly/Quarterly Testing.Caused by Faulty Flow Controller & Ramp Generator Operation |
- on 850720,RCIC Sys Tripped on Overspeed While auto-starting During Monthly/Quarterly Testing.Caused by Faulty Flow Controller & Ramp Generator Operation
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| 05000331/LER-1985-029, :on 850812,during Diesel Fire Pump Operability Test,Leak Detected in Fire Main Outside Reactor Bldg.Caused by Air Hammer.Portion of Fire Main Isolated to Initiate Repairs |
- on 850812,during Diesel Fire Pump Operability Test,Leak Detected in Fire Main Outside Reactor Bldg.Caused by Air Hammer.Portion of Fire Main Isolated to Initiate Repairs
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) |
| 05000331/LER-1985-030, :on 850731,two Secondary Containment Airlock Doors Simultaneously Opened.Caused by out-of-adjustment Door Interlock Mechanism.Defective Mechanism Repaired |
- on 850731,two Secondary Containment Airlock Doors Simultaneously Opened.Caused by out-of-adjustment Door Interlock Mechanism.Defective Mechanism Repaired
| 10 CFR 50.73(a)(2)(i) |
| 05000331/LER-1985-031, :on 850802,RCIC Sys Turbine/Pump Initiation & Control Power Static Inverter Removed from Svc,Rendering RCIC Sys Inoperable.Caused by Failure of Inverter Unit. Inverter Replaced |
- on 850802,RCIC Sys Turbine/Pump Initiation & Control Power Static Inverter Removed from Svc,Rendering RCIC Sys Inoperable.Caused by Failure of Inverter Unit. Inverter Replaced
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| 05000331/LER-1985-032, :on 850802,plant Operated for Period in Excess of 7 H W/O Performing Required Surveillance in Neutron Noise Region.Caused by Operator Error.Personnel Counseled |
- on 850802,plant Operated for Period in Excess of 7 H W/O Performing Required Surveillance in Neutron Noise Region.Caused by Operator Error.Personnel Counseled
| 10 CFR 50.73(a)(2)(1) |
| 05000331/LER-1985-033, :on 850805,emergency Diesel Generator a Removed from Svc for Air Blower Insp.Emergency Diesel Generator B Declared Inoperable Due to High Fuel Oil Sediment Levels. Emergency Diesel Generators Returned to Svc |
- on 850805,emergency Diesel Generator a Removed from Svc for Air Blower Insp.Emergency Diesel Generator B Declared Inoperable Due to High Fuel Oil Sediment Levels. Emergency Diesel Generators Returned to Svc
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000331/LER-1985-034, :on 850709,reactor Protection Sys a Tripped During Reenergization of Sys B.Caused by Operational Amplifiers Saturating When First Energized.Amplifiers Replaced |
- on 850709,reactor Protection Sys a Tripped During Reenergization of Sys B.Caused by Operational Amplifiers Saturating When First Energized.Amplifiers Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000331/LER-1985-035, :on 850904,RCIC Sys Declared Inoperable When RCIC Turbine Tripped During Manual Start.Caused by Worn Mechanical Overspeed Trip Linkage Sys.New Turbine Governor Control Box Ordered |
- on 850904,RCIC Sys Declared Inoperable When RCIC Turbine Tripped During Manual Start.Caused by Worn Mechanical Overspeed Trip Linkage Sys.New Turbine Governor Control Box Ordered
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| 05000331/LER-1985-036, :on 850828,emergency Diesel Generators Declared Inoperable Per Tech Spec 3.5.G.1.Caused by Determination That Existing Electrical Lineup Could Defeat Load Sequencing Logic of Emergency Diesel Generators |
- on 850828,emergency Diesel Generators Declared Inoperable Per Tech Spec 3.5.G.1.Caused by Determination That Existing Electrical Lineup Could Defeat Load Sequencing Logic of Emergency Diesel Generators
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000331/LER-1985-037, :on 850731,too Few APRM Downscale Trip Channels Discovered.Util & GE Currently Determining Purpose of Reactor Protection Sys Logic Channel Trip & Feasibility of Elimination |
- on 850731,too Few APRM Downscale Trip Channels Discovered.Util & GE Currently Determining Purpose of Reactor Protection Sys Logic Channel Trip & Feasibility of Elimination
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| 05000331/LER-1985-038, :on 850906,both Doors of Airlock Between Reactor & Turbine Bldgs Inadvertently Opened Simultaneously, Resulting in Secondary Containment Violations.Caused by Personnel Error.Door Interlocks Repaired |
- on 850906,both Doors of Airlock Between Reactor & Turbine Bldgs Inadvertently Opened Simultaneously, Resulting in Secondary Containment Violations.Caused by Personnel Error.Door Interlocks Repaired
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| 05000331/LER-1985-039, :on 850918,RCIC-to-vessel Inject Valve BN-20-2512 Failed to Open on Demand.Possibly Caused by Unnecessarily High Setting of Valve Torque Switch.Switch Placed at Lower Setting |
- on 850918,RCIC-to-vessel Inject Valve BN-20-2512 Failed to Open on Demand.Possibly Caused by Unnecessarily High Setting of Valve Torque Switch.Switch Placed at Lower Setting
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000331/LER-1985-040, :on 851010,unintentional Momentary Violation of Secondary Containment Occurred When Both Airlock Doors Simultaneously Opened.Caused by Loose Wire on Solenoid.Wire Repaired.Amend to Tech Specs Requested |
- on 851010,unintentional Momentary Violation of Secondary Containment Occurred When Both Airlock Doors Simultaneously Opened.Caused by Loose Wire on Solenoid.Wire Repaired.Amend to Tech Specs Requested
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| 05000331/LER-1985-041, :on 851007 & 28,maint Activities on Isolation & Downstream Valves Required Voluntary Realignment of Fire Suppression Sys from Normal to Backup Water Supply.Sys Returned to Normal Status |
- on 851007 & 28,maint Activities on Isolation & Downstream Valves Required Voluntary Realignment of Fire Suppression Sys from Normal to Backup Water Supply.Sys Returned to Normal Status
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| 05000331/LER-1985-042, :on 851005,two Drywell Equipment Drain Sump Timers Found Inoperable.Caused by Corrosion/Pitting on Internal Motor Power Contacts & Increased Resistance Across Contacts at Low Voltage.Timers Replaced |
- on 851005,two Drywell Equipment Drain Sump Timers Found Inoperable.Caused by Corrosion/Pitting on Internal Motor Power Contacts & Increased Resistance Across Contacts at Low Voltage.Timers Replaced
| 10 CFR 50.73(a)(2)(1) |
| 05000331/LER-1985-043, :on 851104,HPCI Sys Taken Inoperable to Work on Packing Leak on Outboard Steam Supply Isolation Valve.Valve Repaired & Sys Declared Operable.Further Valve Repair Will Be Performed in Near Future |
- on 851104,HPCI Sys Taken Inoperable to Work on Packing Leak on Outboard Steam Supply Isolation Valve.Valve Repaired & Sys Declared Operable.Further Valve Repair Will Be Performed in Near Future
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000331/LER-1985-044, :on 851105,RCIC Taken Out of Svc to Modify RCIC-to-vessel Inject Valve Circuitry.Repair Completed.On 851107,RCIC Tripped on Electrical Overspeed.Caused by Setpoint Drift on Overspeed Trip Monitor |
- on 851105,RCIC Taken Out of Svc to Modify RCIC-to-vessel Inject Valve Circuitry.Repair Completed.On 851107,RCIC Tripped on Electrical Overspeed.Caused by Setpoint Drift on Overspeed Trip Monitor
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000331/LER-1985-045, :on 851116 & 22,momentary Inadvertent Violations of Secondary Containment Occurred.Caused by Defective Door Interlock Mechanisms.New Mechanisms Installed |
- on 851116 & 22,momentary Inadvertent Violations of Secondary Containment Occurred.Caused by Defective Door Interlock Mechanisms.New Mechanisms Installed
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| 05000331/LER-1985-046, :on 851120,electric Fire Pump Out of Svc for More than 7 Days & Maint Not Completed.Caused by Increased Scope of Work & Delay in Procurement of Parts.Electric Pump Returned to Svc & Pump Tested |
- on 851120,electric Fire Pump Out of Svc for More than 7 Days & Maint Not Completed.Caused by Increased Scope of Work & Delay in Procurement of Parts.Electric Pump Returned to Svc & Pump Tested
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