ENS 41246
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ENS Event | |
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02:35 Dec 6, 2004 | |
Title | Automatic Turbine Trip/Reactor Trip Due to Moisture Separator Reheater (Msr) High Level Trip Signal. |
Event Description | Reactor Trip caused by Turbine trip. Turbine trip caused by a Moisture Separator Reheater 1B high level. Maintenance personnel were working in vicinity of level switches at time of trip. Root cause investigation in progress. All systems operated as designed on Reactor trip.
Maintenance personnel working in the vicinity of Moisture Separator Reheater 1B were setting up radiography equipment when the MSR 1B high level trip was generated. All rods fully inserted. Both Motor Driven Auxiliary Feedwater pumps actuated as expected. All Emergency Core Cooling Systems and the Emergency Diesel Generators are fully operable if needed. Catawba Unit 2 is operating at 100% power and the electrical grid is stable. The NRC Resident Inspector was notified of this event by the licensee. |
Where | |
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Catawba South Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-2.3 h-0.0958 days <br />-0.0137 weeks <br />-0.00315 months <br />) | |
Opened: | Jeff Nieberding 00:17 Dec 6, 2004 |
NRC Officer: | John Mackinnon |
Last Updated: | Dec 6, 2004 |
41246 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Catawba with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 573442024-09-27T11:46:00027 September 2024 11:46:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Condenser Vacuum ENS 570262024-03-13T01:11:00013 March 2024 01:11:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Power to Containment Radiation Monitors ENS 561772022-10-24T12:57:00024 October 2022 12:57:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 558562022-04-23T06:24:00023 April 2022 06:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Control Rod Testing ENS 555492021-10-27T18:29:00027 October 2021 18:29:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of the 1B EDG Load Sequencer on Bus Undervoltage Condition ENS 552292021-05-01T11:55:0001 May 2021 11:55:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Actuation of the Auxiliary Feedwater System ENS 548882020-09-08T13:25:0008 September 2020 13:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip on Over Power Delta Temperature ENS 545232020-02-12T23:00:00012 February 2020 23:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Due to Main Turbine Trip ENS 543072019-10-02T08:15:0002 October 2019 08:15:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Containment Spray System ENS 532712018-03-19T07:29:00019 March 2018 07:29:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Actuation of Auxiliary Feedwater System During Maintenance ENS 467802011-04-23T13:21:00023 April 2011 13:21:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Auxiliary Feedwater Pump Start While Cooling Down Reactor ENS 435972007-08-25T14:58:00025 August 2007 14:58:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Autostart of All Emergency Diesel Generators Due to a Grid Disturbance ENS 412462004-12-06T02:35:0006 December 2004 02:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Turbine Trip/Reactor Trip Due to Moisture Separator Reheater (Msr) High Level Trip Signal. ENS 411542004-10-28T04:52:00028 October 2004 04:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip After Shutdown Bank Dropped Into Core ENS 405382004-02-22T22:30:00022 February 2004 22:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Manually Tripped After the "B" Sg Feedwater Isolation Valve Failed Closed ENS 401142003-08-29T06:03:00029 August 2003 06:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Catawba Unit 1 Automatic Reactor Trip Due to Reactor Protection System Actuation 2024-09-27T11:46:00 | |
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