ENS 47988
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ENS Event | |
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06:39 Jun 3, 2012 | |
Title | Autostart of "B" Edg Due to Loss of Offsite Power Circuit 767 |
Event Description | At approximately 0239 hours0.00277 days <br />0.0664 hours <br />3.95172e-4 weeks <br />9.09395e-5 months <br /> on June 3, 2012 the 'B' Emergency Diesel Generator (EDG) automatically started when offsite power circuit 767 was de-energized. The EDG started and re-energized Safe Guards busses 16 and 17. The selected Service Water (SW) pump 'B' automatically started to supply cooling to the EDG.
The operators responded to the loss of circuit 767 using abnormal operating procedure AP-ELEC.1 'Loss of 12A and/or 12B Busses'. Offsite power was restored to 12B bus using ER-ELEC.1 'Restoration of Offsite Power' on circuit 7T at 0318 hours0.00368 days <br />0.0883 hours <br />5.257936e-4 weeks <br />1.20999e-4 months <br />. The 'B' EDG was shutdown at 0445 hours0.00515 days <br />0.124 hours <br />7.357804e-4 weeks <br />1.693225e-4 months <br />. The initial investigation of the loss of circuit 767 indicates that the likely cause was due to wildlife, e.g., raccoon. The licensee informed the NRC Resident Inspector. |
Where | |
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Ginna New York (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.53 h-0.0221 days <br />-0.00315 weeks <br />-7.25994e-4 months <br />) | |
Opened: | Craig Jones 06:07 Jun 3, 2012 |
NRC Officer: | Steve Sandin |
Last Updated: | Jun 3, 2012 |
47988 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 567902023-10-13T01:27:00013 October 2023 01:27:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 567312023-09-09T15:43:0009 September 2023 15:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 555042021-10-04T04:31:0004 October 2021 04:31:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid System Actuation ENS 536962018-10-26T04:00:00026 October 2018 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness Automatic Start of the Emergency Diesel Generator and Loss of Radiation Monitor ENS 517302016-02-12T04:05:00012 February 2016 04:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Auto-Started Due to the Loss of a Station Service Transformer ENS 492142013-07-24T18:19:00024 July 2013 18:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip from Full Power ENS 479882012-06-03T06:39:0003 June 2012 06:39:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Autostart of "B" Edg Due to Loss of Offsite Power Circuit 767 ENS 473382011-10-12T03:28:00012 October 2011 03:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Auto Stop Valve Closure ENS 469172011-06-03T04:39:0003 June 2011 04:39:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unexpected Emergency Diesel Generator Actuation ENS 432432007-03-17T02:09:00017 March 2007 02:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Caused by Safety Injection Signal ENS 431282007-01-28T01:40:00028 January 2007 01:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Load Transient Caused by Ehc Problem ENS 417652005-06-10T17:51:00010 June 2005 17:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Offsite Bus Due to a Lighting Strike with Actuation of Emergency Diesel Generator ENS 415582005-04-01T19:02:0001 April 2005 19:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Start Due to a Partial Loss of Offsite Power ENS 414142005-02-17T02:12:00017 February 2005 02:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Turbine Trip as a Result of Failed Power Supply ENS 403192003-11-13T14:54:00013 November 2003 14:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auto Start and Loading of the "B" Emergency Diesel Generator ENS 402482003-10-15T14:24:00015 October 2003 14:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation a Manual Reactor Trip from 1% Power as Per Abnormal Operating Procedures Occurred 2023-09-09T15:43:00 | |
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