05000237/FIN-2009005-10
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Finding | |
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Title | Electro-Hydraulic Control (EHC) Fluid Leaking From Stop Valve 3-5699-MSV4-FA Resulting in Forced Outage D3F49 |
Description | The inspectors identified an unresolved item regarding the regulatory requirements associated with the circumstances surrounding the Unit 3 turbine trip on On November 5, 2009, at 8:53 p.m., Unit 3 Control Room received the following alarm: 903-7 B-6, EHC [electro-hydraulic control] RESERVOIR LVL HI/LO (reference IR 989641) indicating a rate of change in the EHC reservoir at 1.3 in 100 hrs or greater. A non-licensed operator (NLO) was dispatched to stage a barrel of EHC fluid for addition. Preparations were made for a heater bay entry to look for leaks. A Unit 3 heater bay entry was made and it was determined that the Unit 3 Main Turbine Stop Valve (MSV) # 4 had an EHC leak from the fast-acting solenoid valve (3-5699-MSV4-FA). The leak was determined to be approximately 4-5 gallons of fluid per hour. A report from the field was that reservoir level had dropped about 1.1 in the last 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Between 12:50 a.m. and 3:43 a.m. on November 6, 2009, the licensee added two barrels of EHC fluid to the EHC reservoir. On November 6, 2009, between 9:00 a.m. and 2:00 p.m., licensee management conducted meetings regarding the repair of the leak on MSV #4. The plan called for starting to down power Unit 3 to 650 Mwe for a planned 3:00 p.m. entry into the heater bay to repair the valve. The decision to go to 650 Mwe was to reduce the dose rate in the area and extend stay time for the repair. At approximately 3:00 p.m., while staging for entry to repair the leak, Operations personnel informed the NLO, staged to isolate the oil supply to the leaking valve, that level in the EHC reservoir was dropping quickly, and requested the NLO to enter the pipeway as soon as possible. At approximately 3:05 p.m., the NLO observed oil spraying profusely from the bottom area of #4 Main Stop Valve and the area of the solenoid that was going to be changed out. The NLO immediately contacted the control room to report what was observed and a decision was made to take the turbine offline. At 3:32 p.m., the Unit 3 Turbine was tripped. The licensee had not completed their root cause investigation by the end of the inspection period. The inspectors planned to review the root cause investigation to determine if there were any violations of NRC requirements and that appropriate corrective actions were applied. (URI 05000249/2009005-10 |
Site: | Dresden |
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Report | IR 05000237/2009005 Section 4OA3 |
Date counted | Dec 31, 2009 (2009Q4) |
Type: | URI: |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | R Jickling C Moore C Phillips D Melendez Colon D Sand F Ramirez J Benjamin J Draper J Mcghee L Kozak M Holmberg M Mitchell M Ringc Phillipsd Melendez-Colon E Coffman J Draper M Ring R Krsek R Russell W Slawinski |
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Finding - Dresden - IR 05000237/2009005 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Dresden) @ 2009Q4
Self-Identified List (Dresden)
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