Transcript of 850613 Telcon Between Headquarters Operations Officer & Licensee Re 850609 Reactor TripML20129D980 |
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Davis Besse |
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Issue date: |
06/13/1985 |
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From: |
NRC |
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References |
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NUDOCS 8507300212 |
Download: ML20129D980 (38) |
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Category:LEGAL TRANSCRIPTS & ORDERS & PLEADINGS
MONTHYEARML20198L1911998-12-21021 December 1998 Submits Comments Re Proposed Rule to Revise 10CFR50.59, Changes,Tests & Experiments ML20198L1361998-12-15015 December 1998 Comment Opposing Proposed Rule 10CFR50.65 Re Requirements for Monitoring Effectiveness of Maint of NPP ML20217J2161998-03-27027 March 1998 Comment on Proposed Generic Communication Re Lab Testing of nuclear-grade Activated Charcoal ML20217F5361998-03-25025 March 1998 Comment Opposing Draft Regulatory Guide DG-1071, Std Format & Content for Post-Shutdown Decommissioning Activities Rept ML20199J4651998-01-22022 January 1998 Comment Opposing Draft RG-1070, Sampling Plans Used for Dedicating Simple Metallic Commercial Grade Items for Use in Npps. RG Unnecessary Based on Use of EPRI Guideline & Excellent Past History of Commercial Grade Items at DBNPS ML20148M6421997-06-17017 June 1997 Comment on Proposed NRC Bulletin 96-001,suppl 1 Re Control Rod Insertion Problems.Nrc Should Review Info Provided in Licensee 970130 Submittal & Remove Statements of Applicability to B&W Reactors from Suppl Before Final Form ML20134L3401997-01-22022 January 1997 Resolution 96-R-85, Resolution Supporting Merger of Centerior Energy Corp & Ohio Edison Under New Holding Co Called Firstenergy ML20133B6941996-12-18018 December 1996 Submits Ordinance 850-96 Re Approval of Merger of Centerior & Oh Edison Into Firstenergy ML20132A8461996-12-0202 December 1996 Resolution 20-1996 Supporting Merger of Ohio Edison & Centerior Corp Under New Holding Company Called Firstenergy ML20134M6191996-10-28028 October 1996 Proclamation of Support by City of Sandusky,Oh Re Merger of Ohio Edison and Centerior Energy Corp ML20108D9571996-05-0303 May 1996 CEI Response to City of Cleveland 2.206 Petition.Nrc Should Deny Petition ML20097G5731996-02-13013 February 1996 Comment Supporting Petition for Rulemaking PRM-50-63 Re Use of Potassium Iodide ML20097B8721996-01-23023 January 1996 Petition of City of Cleveland,Oh for Expedited Issuance of Nov,Enforcement of License Conditions & Imposition of Appropriate Fines,Per 10CFR2.201,2.202,2.205 & 2.206 ML20101B5841996-01-23023 January 1996 Motion of City of Cleveland,Oh for Partial Summary Judgement Or,In Alternative,For Severance of Issue & Expedited Hearing Procedures.W/Certificate of Svc ML20097B8911996-01-23023 January 1996 Motion of City of Cleveland,Oh for Partial Summary Judgement or in Alternative,For Severance of Issue & Expedited Hearing Procedures ML20096E9781996-01-0808 January 1996 Comment on Proposed Suppl to GL 83-11, Licensee Qualification for Performing Safety Analyses in Support of Licensing Actions ML20087J3611995-08-14014 August 1995 Comment Opposing Proposed Rule 10CFR2 Re Rev of NRC Enforcement Policy ML20086M8241995-06-29029 June 1995 Comment on Proposed Review of NRC Insp Rept Content,Format & Style ML20083M8701995-05-10010 May 1995 Comment on Proposed Rule 10CFR50 Re Primary Reactor Containment Leakage Testing for Water-Cooled Power Reactor ML20081C8841995-03-0303 March 1995 Comment Re NRC Proposed Generic Communication Suppl 5 to GL 88-20, IPEEE for Severe Accident Vulnerabilities. Util Ack NRC Efforts to Reduce Scope of GL 88-20,but Believes That Proposed Changes Still Overly Restrictive ML20077M5831995-01-0404 January 1995 Comment Opposing Proposed Rule 10CFR50 Re Shutdown & low-power Operations for Nuclear Power Reactors ML20072K3611994-08-16016 August 1994 Comment Opposing Proposed Rule 10CFR72 Re Plans for Storage of Sf at Davis Besse NPP ML20072K4411994-08-14014 August 1994 Comment Opposing Proposed Rule 10CFR72 Re Dry Storage of Nuclear Waste at Facility in Toledo,Oh ML20072K5261994-08-12012 August 1994 Comment Supporting Proposed Rule 10CFR72 Re Addition of Standardized NUHOMS Horizontal Modular Storage Sys to List of Approved Sf Storage Casks ML20072B1581994-08-0909 August 1994 Comment Opposing Proposed Rule 10CFR72 on List of Approved Spent Fuel Storage Casks:Addition ML20029D8221994-04-19019 April 1994 Comments on Proposed Rule 10CFR50 Re Codes & Stds for Nuclear Power Plants;Subsection IWE & Subsection Iwl ML20062M4011993-12-28028 December 1993 Comment Supporting Petition for Rulemaking PRM-21-2 Re Commercial Grade Item Dedication ML20046A9561993-07-19019 July 1993 Comment on Proposed Rules 10CFR170 & 171, FY91 & 92 Proposed Rule Implementing Us Court of Appeals Decision & Rev of Fee Schedules;100% Fee Recovery,FY93. ML20056C8951993-07-19019 July 1993 Order Extending Time within Which Commission May Rule on Petitions for Review of LBP-92-32.W/Certificate of Svc. Served on 930720 ML20045F8321993-06-22022 June 1993 Comment on Proposed Rule 10CFR26 Re Mods to fitness-for-duty Program Requirements.Concurs W/Proposed Rule in Reducing Random Testing Rate of Licensees to 50% & Disagrees W/ Maintaining Random Testing Rate of 100% for Vendors ML20044E2781993-05-13013 May 1993 Comment Supporting Petition for Rulemaking PRM-50-58 Re VEPCO Petition to Change Frequency of Emergency Planning Exercise from Annual to Biennial ML20044E1561993-04-29029 April 1993 Comment Supporting Petition for Rulemaking PRM-50-58 Re Frequency Change of Emergency Planning Exercises ML20127L8781993-01-19019 January 1993 Comment Supporting Comments Submitted by NUMARC Re Draft Reg Guide DG-1020 ML20127A6171993-01-0606 January 1993 Order.* Time within Which Commission May Rule on Petitions for Review of Board Order LBP-92-32,dtd 921118,extended Until 930208.W/Certificate of Svc.Served on 930106 ML20126D5801992-12-23023 December 1992 NRC Staff Answer in Response to Petitions for Review Filed by Oh Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & City of Cleveland.* W/Certificate of Svc ML20126F6501992-12-23023 December 1992 Answer of City of Cleveland,Oh,Intervenor,In Opposition to Petitions for Review of 921118 Decision of Aslb.* Petitioners Petitions for Review Should Be Denied. Certificate of Svc Encl ML20126D5171992-12-23023 December 1992 City of Brook Park Answer to Petitions for Review.* Opposes Applicants 921208 Petitions for Review Based on Fact That ASLB Decision in proceeding,LBP-92-32,adequately Addressed Issues Raised in Petitions.W/Certificate of Svc ML20126D5461992-12-23023 December 1992 Answer of Cleveland Electric Illuminating Co & Toledo Edison Co to Limited Petition for Review of City of Cleveland,Oh of 921118 Decision of Aslb.* Commission Should Deny City of Cleveland Petition.W/Certificate of Svc ML20126D5781992-12-23023 December 1992 Answer of American Municipal Power-OH,Inc in Opposition to Petitions for Review of Oh Edison Co & Cleveland Electric Illuminating Co/Toledo Edison Co.* W/Certificate of Svc ML20126D4761992-12-22022 December 1992 Alabama Electric Cooperative Answer to Applicants Petitions for Review.* Applicants 921208 Petitions for Review Should Be Denied.W/Certificate of Svc ML20126A5461992-12-10010 December 1992 Order.* Requests That Answers to Petition for Review Be Filed No Later than 921223.W/Certificate of Svc.Served on 921210 ML20126A5751992-12-0808 December 1992 Petition for Review.* Requests That NRC Review LBP-92-32, 921118 Board Decision in Proceeding.Board Erroneously Interpreted Section 105(c) of AEA by Ignoring Fundamental Underpinning of Statute.W/Certificate of Svc ML20126A5871992-12-0808 December 1992 Petition for Review.* Requests That NRC Review ASLB 921118 decision,LBP-92-32.Board Erroneously Interpreted Section 105(c) of AEA by Ignoring Fundamental Underplanning of Statute.Certificate of Svc Encl ML20126A7651992-11-18018 November 1992 Limited Petition for Review of City of Cleveland,Oh of 921118 Decision of Aslb.* City of Cleveland Petition for Review Should Be Granted.W/Certificate of Svc ML20115E1771992-10-0808 October 1992 Comment Supporting Draft Mgt Directive 8.6,GL 92-05 ML20105C8971992-09-16016 September 1992 Comment Opposing Proposed Generic Communication Re Generic Ltr Concerning analog-to-digital Replacements Under 10CFR50.59 ML20114A8841992-08-17017 August 1992 Designation of City of Brook Park,Oh of Adopted Portions of Summary Disposition Pleadings.* Brook Park Not Advancing Any Addl Argument or Analysis in Connection W/Designation,Per 920806 Memorandum & Order.W/Certificate of Svc ML20099E1821992-07-28028 July 1992 Comment Supporting Proposed Rules 10CFR20 & 61 Re LLW Shipment Manifest Info & Reporting ML20099A4051992-07-17017 July 1992 Comment on Proposed Rules 10CFR20 & 50 Re Reducing Regulatory Burden on Nuclear Licensees.Supports Rules ML20101R4831992-07-0808 July 1992 Comment Supporting Proposed Rule 10CFR50 Re Receipt of Byproduct & Special Nuclear Matl 1998-03-27
[Table view] Category:TRANSCRIPTS
MONTHYEARML20101K2691992-06-29029 June 1992 City of Cleveland Proposed Corrections to Oral Argument Transcript of 920610.* W/Certificate of Svc & Svc List ML20214J0691986-11-21021 November 1986 Transcript of Commission 861121 Public Meeting in Washington,Dc Re Discussion/Possible Vote on Plant Restart. Pp 1-63.Supporting Documentation Encl ML20205C7691986-08-0707 August 1986 Transcript of 860807 Hearing in Sandusky,Oh.Pp 567-972. Supporting Documentation Encl ML20205C7801986-08-0606 August 1986 Transcript of 860806 Hearing in Sandusky,Oh.Pp 260-509. Supporting Documentation Encl ML20212F6431986-08-0606 August 1986 Transcript of 860806 Limited Appearances Session in Sandusky,Oh.Pp 510-566 ML20205C7931986-08-0505 August 1986 Transcript of 860805 Hearing in Sandusky,Oh.Pp 1-259. Supporting Documentation Encl ML20203K0651986-08-0101 August 1986 Prefiled Testimony of RM Bimber & D Gitlin Re Waste Disposal Permit for Facility.Related Correspondence ML20204E9961986-07-24024 July 1986 Transcript of Commission 860724 Status Briefing on Facility Restart in Washington,Dc.Pp 1-61.Supporting Documentation Encl ML20207F6381986-07-19019 July 1986 Testimony of D Briden,Gf Bennett,Js Bland,Dm Hendron, CE Herdendorf,R Hetherington,Wb Jackson & Re Linnemann Re Burial of Very Low Level Waste at Davis-Besse.Related Correspondence ML20207F3801986-07-17017 July 1986 Testimony of DE Guy,Rr Pavey,Jh Marshall & J Yoytek Supporting State of Oh Petition to Intervene in Proposed Waste Burial Plan.Related Info Encl.W/Certificate of Svc. Related Correspondence ML20206R7181986-06-27027 June 1986 Transcript of ACRS Subcommittee on Davis-Besse Restart 860627 Meeting in Washington,Dc.Pp 1-110.Supporting Documentation Encl ML20206J4891986-06-25025 June 1986 Testimony of D Gitlin to Be Presented on 860625 in Sandusky, Oh Requesting Rescission of NRC Approval of Proposed Sludge Disposal Project ML20206J4541986-06-14014 June 1986 Testimony of RM Bimber Requesting Rescission of Onsite Waste Disposal Permit &/Or Advance Approval of Release of Dumpsite for Unrestricted Use at Time of Decommissioning ML20151Y8351986-02-0606 February 1986 Transcript of ACRS Subcommittee on Davis-Besse Nuclear Station Unit 1 Restart 860206 Meeting in Washington,Dc. Pp 1-169.Supporting Documentation Encl ML20137T3141986-02-0606 February 1986 Statement Before Subcommittee on Energy & Environ, Committee on Interior & Insular Affairs,Us House of Representatives Re FY87 Budget ML20138Q0771985-12-18018 December 1985 Transcript of 851218 Briefing on Restart from 850609 Event in Washington,Dc.Pp 1-102.Supporting Documentation Encl ML20133F2361985-10-0404 October 1985 Transcript of ACRS Subcommittee on Davis-Besse 851004 Meeting in Oak Harbor,Oh Re Review of Course of Action Prior to Restart of Plant.Pp 1-117 ML20132A4241985-09-18018 September 1985 Transcript of 850918 Public Meeting in Washington,Dc Re Continuation of Briefing on Plant.Pp 1-80.Supporting Documentation Encl ML20132A4001985-09-17017 September 1985 Transcript of Commission 850917 Public Meeting in Washington,Dc to Continue 850724 Briefing on Davis-Besse 850609 Event.Pp 1-89.Viewgraphs Encl IA-86-787, Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC1985-09-0404 September 1985 Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC ML20215E1871985-09-0404 September 1985 Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC ML20129B8461985-07-12012 July 1985 Transcript of 850712 Closed Meeting in Oak Harbor,Oh Re Status Rept on Quarantined Equipment Resulting from 850609 Event.Pp 91-248.Related Documentation Encl ML20129B9411985-07-12012 July 1985 Transcript of 850712 Closed Meeting in Oak Harbor,Oh Re Status Rept on Quarantine Equipment Resulting from 850609 Event.Pp 1-90.Supporting Documentation Encl ML20129B6791985-07-11011 July 1985 Transcript of 850711 Closed Meeting Re Steam Feed Rupture Control Sys Equipment & Operations.Pp 1-72 ML20129B9121985-07-11011 July 1985 Transcript of 850711 Closed Meeting in Oak Harbor,Oh Re Steam & Feedwater Rupture Control Sys Training.Pp 1-20 ML20129B9071985-07-10010 July 1985 Transcript of NRC Fact-Finding Team 850710 Closed Meeting W/Util in Oak Harbor,Oh Re 850609 Sequence of Events. Pp 1-24 ML20129B0751985-07-10010 July 1985 Transcript of 850710 Closed Meeting W/Util in Oak Harbor,Oh Re Steam Feed Rupture Control Sys Actuated Equipment & Operations.Pp 1-37.Supporting Documentation Encl ML20129B8861985-07-0909 July 1985 Transcript of 850709 Closed Meeting in Oak Harbor,Oh Re Addl Info Request Concerning Serial 517 Ltr & Pump Capacities of Equipment Used to Mitigate Total Loss of Feed. Pp 1-24.Related Documentation Encl ML20129B1021985-07-0909 July 1985 Transcript of 850709 Meeting W/Util in Oak Harbor,Oh Re PORV Controls & Instrumentation.Pp 1-9.Supporting Documentation Encl ML20129B8221985-07-0909 July 1985 Transcript of 850709 Closed Meeting in Oak Harbor,Oh Re Steam & Feedwater Rupture Control Sys Operations & Action Plan to Troubleshoot 850609 Anomalies.Pp 1-69 ML20129B0801985-07-0909 July 1985 Transcript of 850709 Closed Meeting W/Util in Oak Harbor,Oh Re Procedures Concerning Startup Feed Pump & Main Feed Pump Following Steam Feed Rupture Control Sys Actuation.Pp 1-43. Supporting Documentation Encl ML20129C1051985-06-27027 June 1985 Transcript of Fact-Finding Task Force 850627 Closed Meeting in Bethesda,Md Re 850609 Event.Pp 1-33.Related Documentation Encl ML20129B5981985-06-21021 June 1985 Transcript of 850621 Interview of R Osburn in Oak Harbor,Oh Re 850609 Event.Pp 1-11 ML20129B6181985-06-21021 June 1985 Transcript of 850621 Meeting in Oak Harbor,Oh Re Results of Troubleshooting & Identification of Root Cause of 850609 Event.Pp 1-140 ML20129B1811985-06-21021 June 1985 Transcript of 850621 Joint Interview of Quennoz & W O'Connor in Oak Harbor,Oh Re 850609 Event.Pp 1-53 ML20129B5681985-06-21021 June 1985 Transcript of 850621 Interview of W Rogers in Oak Harbor,Oh Re 850609 Event.Pp 1-17 ML20129B7751985-06-20020 June 1985 Transcript of 850620 Meeting in Oak Harbor,Oh Re Troubleshooting Action Plans for Auxiliary Feedwater Pumps Following 850609 Event.Pp 1-79 ML20129B4241985-06-20020 June 1985 Transcript of 850620 Interview of W Rogers in Oak Harbor,Oh Re 850609 Event.Pp 1-163 ML20129B4601985-06-19019 June 1985 Transcript of 850619 Meeting in Oak Harbor,Oh Re Action Plans for NI-1 Source Range Channel Following 850609 Event ML20129B5611985-06-19019 June 1985 Transcript of 850619 Joint Interview of T Lehman & Feasel in Oak Harbor,Oh Re 850609 Event.Pp 1-50 ML20129B7061985-06-19019 June 1985 Transcript of 850619 Meeting in Oak Harbor,Oh Re Action Plan on Turbine Bypass Valve Following 850609 Event.Pp 1-29 ML20129B5501985-06-18018 June 1985 Transcript of 850618 Meeting in Oak Harbor,Oh Re Action Plan for Main Feedwater Pump Control Sys Following 850609 Event. Pp 1-24 ML20129B0511985-06-18018 June 1985 Transcript of 850618 Interview of T Lang in Oak Harbor,Oh Re 850609 Event.Pp 1-49 ML20129B0461985-06-18018 June 1985 Transcript of 850618 Meeting in Oak Harbor,Oh Re Sequence of Events Discussion for 850609 Event.Pp 1-34.Supporting Documentation Encl ML20129D3761985-06-17017 June 1985 Transcript of 850617 Meeting W/Util in Bethesda,Md Re Auxiliary Feedwater Sys.Pp 1-50.Supporting Documentation Encl ML20129B0491985-06-17017 June 1985 Transcript of Interviews in Oak Harbor,Oh of Equipment Operators C Burns,J Meleg,M Klein & B Morrison Re 850609 Event.Pp 1-145.Supporting Documentation Encl ML20129B1271985-06-15015 June 1985 Transcript of 850615 Joint Interview of L Simon & SM Quennoz in Oak Harbor,Oh Re 850609 Event.Pp 1-78 ML20129C0591985-06-15015 June 1985 Transcript of Afternoon Session of 850615 Proceedings in Oak Harbor,Oh Re Guidelines for Troubleshooting or Performing Investigative Actions Into Root Causes Surrounding 850609 Event.Pp 1-15 ML20129B0661985-06-14014 June 1985 Transcript of 850614 Interview of R Walleman in Oak Harbor,Oh Re 850609 Event.Pp 1-114 ML20129B0841985-06-14014 June 1985 Transcript of 850614 Equipment Meeting in Oak Harbor,Oh Re 850609 Event.Pp 1-100.Supporting Documentation Encl 1992-06-29
[Table view] Category:DEPOSITIONS
MONTHYEARML20101K2691992-06-29029 June 1992 City of Cleveland Proposed Corrections to Oral Argument Transcript of 920610.* W/Certificate of Svc & Svc List ML20214J0691986-11-21021 November 1986 Transcript of Commission 861121 Public Meeting in Washington,Dc Re Discussion/Possible Vote on Plant Restart. Pp 1-63.Supporting Documentation Encl ML20205C7691986-08-0707 August 1986 Transcript of 860807 Hearing in Sandusky,Oh.Pp 567-972. Supporting Documentation Encl ML20205C7801986-08-0606 August 1986 Transcript of 860806 Hearing in Sandusky,Oh.Pp 260-509. Supporting Documentation Encl ML20212F6431986-08-0606 August 1986 Transcript of 860806 Limited Appearances Session in Sandusky,Oh.Pp 510-566 ML20205C7931986-08-0505 August 1986 Transcript of 860805 Hearing in Sandusky,Oh.Pp 1-259. Supporting Documentation Encl ML20203K0651986-08-0101 August 1986 Prefiled Testimony of RM Bimber & D Gitlin Re Waste Disposal Permit for Facility.Related Correspondence ML20204E9961986-07-24024 July 1986 Transcript of Commission 860724 Status Briefing on Facility Restart in Washington,Dc.Pp 1-61.Supporting Documentation Encl ML20207F6381986-07-19019 July 1986 Testimony of D Briden,Gf Bennett,Js Bland,Dm Hendron, CE Herdendorf,R Hetherington,Wb Jackson & Re Linnemann Re Burial of Very Low Level Waste at Davis-Besse.Related Correspondence ML20207F3801986-07-17017 July 1986 Testimony of DE Guy,Rr Pavey,Jh Marshall & J Yoytek Supporting State of Oh Petition to Intervene in Proposed Waste Burial Plan.Related Info Encl.W/Certificate of Svc. Related Correspondence ML20206R7181986-06-27027 June 1986 Transcript of ACRS Subcommittee on Davis-Besse Restart 860627 Meeting in Washington,Dc.Pp 1-110.Supporting Documentation Encl ML20206J4891986-06-25025 June 1986 Testimony of D Gitlin to Be Presented on 860625 in Sandusky, Oh Requesting Rescission of NRC Approval of Proposed Sludge Disposal Project ML20206J4541986-06-14014 June 1986 Testimony of RM Bimber Requesting Rescission of Onsite Waste Disposal Permit &/Or Advance Approval of Release of Dumpsite for Unrestricted Use at Time of Decommissioning ML20151Y8351986-02-0606 February 1986 Transcript of ACRS Subcommittee on Davis-Besse Nuclear Station Unit 1 Restart 860206 Meeting in Washington,Dc. Pp 1-169.Supporting Documentation Encl ML20137T3141986-02-0606 February 1986 Statement Before Subcommittee on Energy & Environ, Committee on Interior & Insular Affairs,Us House of Representatives Re FY87 Budget ML20138Q0771985-12-18018 December 1985 Transcript of 851218 Briefing on Restart from 850609 Event in Washington,Dc.Pp 1-102.Supporting Documentation Encl ML20133F2361985-10-0404 October 1985 Transcript of ACRS Subcommittee on Davis-Besse 851004 Meeting in Oak Harbor,Oh Re Review of Course of Action Prior to Restart of Plant.Pp 1-117 ML20132A4241985-09-18018 September 1985 Transcript of 850918 Public Meeting in Washington,Dc Re Continuation of Briefing on Plant.Pp 1-80.Supporting Documentation Encl ML20132A4001985-09-17017 September 1985 Transcript of Commission 850917 Public Meeting in Washington,Dc to Continue 850724 Briefing on Davis-Besse 850609 Event.Pp 1-89.Viewgraphs Encl IA-86-787, Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC1985-09-0404 September 1985 Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC ML20215E1871985-09-0404 September 1985 Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC ML20129B8461985-07-12012 July 1985 Transcript of 850712 Closed Meeting in Oak Harbor,Oh Re Status Rept on Quarantined Equipment Resulting from 850609 Event.Pp 91-248.Related Documentation Encl ML20129B9411985-07-12012 July 1985 Transcript of 850712 Closed Meeting in Oak Harbor,Oh Re Status Rept on Quarantine Equipment Resulting from 850609 Event.Pp 1-90.Supporting Documentation Encl ML20129B6791985-07-11011 July 1985 Transcript of 850711 Closed Meeting Re Steam Feed Rupture Control Sys Equipment & Operations.Pp 1-72 ML20129B9121985-07-11011 July 1985 Transcript of 850711 Closed Meeting in Oak Harbor,Oh Re Steam & Feedwater Rupture Control Sys Training.Pp 1-20 ML20129B9071985-07-10010 July 1985 Transcript of NRC Fact-Finding Team 850710 Closed Meeting W/Util in Oak Harbor,Oh Re 850609 Sequence of Events. Pp 1-24 ML20129B0751985-07-10010 July 1985 Transcript of 850710 Closed Meeting W/Util in Oak Harbor,Oh Re Steam Feed Rupture Control Sys Actuated Equipment & Operations.Pp 1-37.Supporting Documentation Encl ML20129B8861985-07-0909 July 1985 Transcript of 850709 Closed Meeting in Oak Harbor,Oh Re Addl Info Request Concerning Serial 517 Ltr & Pump Capacities of Equipment Used to Mitigate Total Loss of Feed. Pp 1-24.Related Documentation Encl ML20129B1021985-07-0909 July 1985 Transcript of 850709 Meeting W/Util in Oak Harbor,Oh Re PORV Controls & Instrumentation.Pp 1-9.Supporting Documentation Encl ML20129B8221985-07-0909 July 1985 Transcript of 850709 Closed Meeting in Oak Harbor,Oh Re Steam & Feedwater Rupture Control Sys Operations & Action Plan to Troubleshoot 850609 Anomalies.Pp 1-69 ML20129B0801985-07-0909 July 1985 Transcript of 850709 Closed Meeting W/Util in Oak Harbor,Oh Re Procedures Concerning Startup Feed Pump & Main Feed Pump Following Steam Feed Rupture Control Sys Actuation.Pp 1-43. Supporting Documentation Encl ML20129C1051985-06-27027 June 1985 Transcript of Fact-Finding Task Force 850627 Closed Meeting in Bethesda,Md Re 850609 Event.Pp 1-33.Related Documentation Encl ML20129B5981985-06-21021 June 1985 Transcript of 850621 Interview of R Osburn in Oak Harbor,Oh Re 850609 Event.Pp 1-11 ML20129B6181985-06-21021 June 1985 Transcript of 850621 Meeting in Oak Harbor,Oh Re Results of Troubleshooting & Identification of Root Cause of 850609 Event.Pp 1-140 ML20129B1811985-06-21021 June 1985 Transcript of 850621 Joint Interview of Quennoz & W O'Connor in Oak Harbor,Oh Re 850609 Event.Pp 1-53 ML20129B5681985-06-21021 June 1985 Transcript of 850621 Interview of W Rogers in Oak Harbor,Oh Re 850609 Event.Pp 1-17 ML20129B7751985-06-20020 June 1985 Transcript of 850620 Meeting in Oak Harbor,Oh Re Troubleshooting Action Plans for Auxiliary Feedwater Pumps Following 850609 Event.Pp 1-79 ML20129B4241985-06-20020 June 1985 Transcript of 850620 Interview of W Rogers in Oak Harbor,Oh Re 850609 Event.Pp 1-163 ML20129B4601985-06-19019 June 1985 Transcript of 850619 Meeting in Oak Harbor,Oh Re Action Plans for NI-1 Source Range Channel Following 850609 Event ML20129B5611985-06-19019 June 1985 Transcript of 850619 Joint Interview of T Lehman & Feasel in Oak Harbor,Oh Re 850609 Event.Pp 1-50 ML20129B7061985-06-19019 June 1985 Transcript of 850619 Meeting in Oak Harbor,Oh Re Action Plan on Turbine Bypass Valve Following 850609 Event.Pp 1-29 ML20129B5501985-06-18018 June 1985 Transcript of 850618 Meeting in Oak Harbor,Oh Re Action Plan for Main Feedwater Pump Control Sys Following 850609 Event. Pp 1-24 ML20129B0511985-06-18018 June 1985 Transcript of 850618 Interview of T Lang in Oak Harbor,Oh Re 850609 Event.Pp 1-49 ML20129B0461985-06-18018 June 1985 Transcript of 850618 Meeting in Oak Harbor,Oh Re Sequence of Events Discussion for 850609 Event.Pp 1-34.Supporting Documentation Encl ML20129D3761985-06-17017 June 1985 Transcript of 850617 Meeting W/Util in Bethesda,Md Re Auxiliary Feedwater Sys.Pp 1-50.Supporting Documentation Encl ML20129B0491985-06-17017 June 1985 Transcript of Interviews in Oak Harbor,Oh of Equipment Operators C Burns,J Meleg,M Klein & B Morrison Re 850609 Event.Pp 1-145.Supporting Documentation Encl ML20129B1271985-06-15015 June 1985 Transcript of 850615 Joint Interview of L Simon & SM Quennoz in Oak Harbor,Oh Re 850609 Event.Pp 1-78 ML20129C0591985-06-15015 June 1985 Transcript of Afternoon Session of 850615 Proceedings in Oak Harbor,Oh Re Guidelines for Troubleshooting or Performing Investigative Actions Into Root Causes Surrounding 850609 Event.Pp 1-15 ML20129B0661985-06-14014 June 1985 Transcript of 850614 Interview of R Walleman in Oak Harbor,Oh Re 850609 Event.Pp 1-114 ML20129B0841985-06-14014 June 1985 Transcript of 850614 Equipment Meeting in Oak Harbor,Oh Re 850609 Event.Pp 1-100.Supporting Documentation Encl 1992-06-29
[Table view] Category:NARRATIVE TESTIMONY
MONTHYEARML20101K2691992-06-29029 June 1992 City of Cleveland Proposed Corrections to Oral Argument Transcript of 920610.* W/Certificate of Svc & Svc List ML20214J0691986-11-21021 November 1986 Transcript of Commission 861121 Public Meeting in Washington,Dc Re Discussion/Possible Vote on Plant Restart. Pp 1-63.Supporting Documentation Encl ML20205C7691986-08-0707 August 1986 Transcript of 860807 Hearing in Sandusky,Oh.Pp 567-972. Supporting Documentation Encl ML20205C7801986-08-0606 August 1986 Transcript of 860806 Hearing in Sandusky,Oh.Pp 260-509. Supporting Documentation Encl ML20212F6431986-08-0606 August 1986 Transcript of 860806 Limited Appearances Session in Sandusky,Oh.Pp 510-566 ML20205C7931986-08-0505 August 1986 Transcript of 860805 Hearing in Sandusky,Oh.Pp 1-259. Supporting Documentation Encl ML20203K0651986-08-0101 August 1986 Prefiled Testimony of RM Bimber & D Gitlin Re Waste Disposal Permit for Facility.Related Correspondence ML20204E9961986-07-24024 July 1986 Transcript of Commission 860724 Status Briefing on Facility Restart in Washington,Dc.Pp 1-61.Supporting Documentation Encl ML20207F6381986-07-19019 July 1986 Testimony of D Briden,Gf Bennett,Js Bland,Dm Hendron, CE Herdendorf,R Hetherington,Wb Jackson & Re Linnemann Re Burial of Very Low Level Waste at Davis-Besse.Related Correspondence ML20207F3801986-07-17017 July 1986 Testimony of DE Guy,Rr Pavey,Jh Marshall & J Yoytek Supporting State of Oh Petition to Intervene in Proposed Waste Burial Plan.Related Info Encl.W/Certificate of Svc. Related Correspondence ML20206R7181986-06-27027 June 1986 Transcript of ACRS Subcommittee on Davis-Besse Restart 860627 Meeting in Washington,Dc.Pp 1-110.Supporting Documentation Encl ML20206J4891986-06-25025 June 1986 Testimony of D Gitlin to Be Presented on 860625 in Sandusky, Oh Requesting Rescission of NRC Approval of Proposed Sludge Disposal Project ML20206J4541986-06-14014 June 1986 Testimony of RM Bimber Requesting Rescission of Onsite Waste Disposal Permit &/Or Advance Approval of Release of Dumpsite for Unrestricted Use at Time of Decommissioning ML20151Y8351986-02-0606 February 1986 Transcript of ACRS Subcommittee on Davis-Besse Nuclear Station Unit 1 Restart 860206 Meeting in Washington,Dc. Pp 1-169.Supporting Documentation Encl ML20137T3141986-02-0606 February 1986 Statement Before Subcommittee on Energy & Environ, Committee on Interior & Insular Affairs,Us House of Representatives Re FY87 Budget ML20138Q0771985-12-18018 December 1985 Transcript of 851218 Briefing on Restart from 850609 Event in Washington,Dc.Pp 1-102.Supporting Documentation Encl ML20133F2361985-10-0404 October 1985 Transcript of ACRS Subcommittee on Davis-Besse 851004 Meeting in Oak Harbor,Oh Re Review of Course of Action Prior to Restart of Plant.Pp 1-117 ML20132A4241985-09-18018 September 1985 Transcript of 850918 Public Meeting in Washington,Dc Re Continuation of Briefing on Plant.Pp 1-80.Supporting Documentation Encl ML20132A4001985-09-17017 September 1985 Transcript of Commission 850917 Public Meeting in Washington,Dc to Continue 850724 Briefing on Davis-Besse 850609 Event.Pp 1-89.Viewgraphs Encl IA-86-787, Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC1985-09-0404 September 1985 Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC ML20215E1871985-09-0404 September 1985 Transcript of 850904 Meeting in Bethesda,Md Re Util Planned Action on 850609 Event.Pp 1-235.Supporting Documentation Encl,Incuding NRC 850828 Meeting Agenda & Viewgraphs of Util 850917 Presentation to NRC ML20129B8461985-07-12012 July 1985 Transcript of 850712 Closed Meeting in Oak Harbor,Oh Re Status Rept on Quarantined Equipment Resulting from 850609 Event.Pp 91-248.Related Documentation Encl ML20129B9411985-07-12012 July 1985 Transcript of 850712 Closed Meeting in Oak Harbor,Oh Re Status Rept on Quarantine Equipment Resulting from 850609 Event.Pp 1-90.Supporting Documentation Encl ML20129B6791985-07-11011 July 1985 Transcript of 850711 Closed Meeting Re Steam Feed Rupture Control Sys Equipment & Operations.Pp 1-72 ML20129B9121985-07-11011 July 1985 Transcript of 850711 Closed Meeting in Oak Harbor,Oh Re Steam & Feedwater Rupture Control Sys Training.Pp 1-20 ML20129B9071985-07-10010 July 1985 Transcript of NRC Fact-Finding Team 850710 Closed Meeting W/Util in Oak Harbor,Oh Re 850609 Sequence of Events. Pp 1-24 ML20129B0751985-07-10010 July 1985 Transcript of 850710 Closed Meeting W/Util in Oak Harbor,Oh Re Steam Feed Rupture Control Sys Actuated Equipment & Operations.Pp 1-37.Supporting Documentation Encl ML20129B8861985-07-0909 July 1985 Transcript of 850709 Closed Meeting in Oak Harbor,Oh Re Addl Info Request Concerning Serial 517 Ltr & Pump Capacities of Equipment Used to Mitigate Total Loss of Feed. Pp 1-24.Related Documentation Encl ML20129B1021985-07-0909 July 1985 Transcript of 850709 Meeting W/Util in Oak Harbor,Oh Re PORV Controls & Instrumentation.Pp 1-9.Supporting Documentation Encl ML20129B8221985-07-0909 July 1985 Transcript of 850709 Closed Meeting in Oak Harbor,Oh Re Steam & Feedwater Rupture Control Sys Operations & Action Plan to Troubleshoot 850609 Anomalies.Pp 1-69 ML20129B0801985-07-0909 July 1985 Transcript of 850709 Closed Meeting W/Util in Oak Harbor,Oh Re Procedures Concerning Startup Feed Pump & Main Feed Pump Following Steam Feed Rupture Control Sys Actuation.Pp 1-43. Supporting Documentation Encl ML20129C1051985-06-27027 June 1985 Transcript of Fact-Finding Task Force 850627 Closed Meeting in Bethesda,Md Re 850609 Event.Pp 1-33.Related Documentation Encl ML20129B5981985-06-21021 June 1985 Transcript of 850621 Interview of R Osburn in Oak Harbor,Oh Re 850609 Event.Pp 1-11 ML20129B6181985-06-21021 June 1985 Transcript of 850621 Meeting in Oak Harbor,Oh Re Results of Troubleshooting & Identification of Root Cause of 850609 Event.Pp 1-140 ML20129B1811985-06-21021 June 1985 Transcript of 850621 Joint Interview of Quennoz & W O'Connor in Oak Harbor,Oh Re 850609 Event.Pp 1-53 ML20129B5681985-06-21021 June 1985 Transcript of 850621 Interview of W Rogers in Oak Harbor,Oh Re 850609 Event.Pp 1-17 ML20129B7751985-06-20020 June 1985 Transcript of 850620 Meeting in Oak Harbor,Oh Re Troubleshooting Action Plans for Auxiliary Feedwater Pumps Following 850609 Event.Pp 1-79 ML20129B4241985-06-20020 June 1985 Transcript of 850620 Interview of W Rogers in Oak Harbor,Oh Re 850609 Event.Pp 1-163 ML20129B4601985-06-19019 June 1985 Transcript of 850619 Meeting in Oak Harbor,Oh Re Action Plans for NI-1 Source Range Channel Following 850609 Event ML20129B5611985-06-19019 June 1985 Transcript of 850619 Joint Interview of T Lehman & Feasel in Oak Harbor,Oh Re 850609 Event.Pp 1-50 ML20129B7061985-06-19019 June 1985 Transcript of 850619 Meeting in Oak Harbor,Oh Re Action Plan on Turbine Bypass Valve Following 850609 Event.Pp 1-29 ML20129B5501985-06-18018 June 1985 Transcript of 850618 Meeting in Oak Harbor,Oh Re Action Plan for Main Feedwater Pump Control Sys Following 850609 Event. Pp 1-24 ML20129B0511985-06-18018 June 1985 Transcript of 850618 Interview of T Lang in Oak Harbor,Oh Re 850609 Event.Pp 1-49 ML20129B0461985-06-18018 June 1985 Transcript of 850618 Meeting in Oak Harbor,Oh Re Sequence of Events Discussion for 850609 Event.Pp 1-34.Supporting Documentation Encl ML20129D3761985-06-17017 June 1985 Transcript of 850617 Meeting W/Util in Bethesda,Md Re Auxiliary Feedwater Sys.Pp 1-50.Supporting Documentation Encl ML20129B0491985-06-17017 June 1985 Transcript of Interviews in Oak Harbor,Oh of Equipment Operators C Burns,J Meleg,M Klein & B Morrison Re 850609 Event.Pp 1-145.Supporting Documentation Encl ML20129B1271985-06-15015 June 1985 Transcript of 850615 Joint Interview of L Simon & SM Quennoz in Oak Harbor,Oh Re 850609 Event.Pp 1-78 ML20129C0591985-06-15015 June 1985 Transcript of Afternoon Session of 850615 Proceedings in Oak Harbor,Oh Re Guidelines for Troubleshooting or Performing Investigative Actions Into Root Causes Surrounding 850609 Event.Pp 1-15 ML20129B0661985-06-14014 June 1985 Transcript of 850614 Interview of R Walleman in Oak Harbor,Oh Re 850609 Event.Pp 1-114 ML20129B0841985-06-14014 June 1985 Transcript of 850614 Equipment Meeting in Oak Harbor,Oh Re 850609 Event.Pp 1-100.Supporting Documentation Encl 1992-06-29
[Table view] |
Text
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This is a transcript of the telephone conversations of the Headquarters Opera-tions Officer concerning the Davis Besse incident that took place on June 9, 1985. These conversations took place between the hours of 0211 through 0851.
Although every effort has been made to accurately transcribe the original taped conversations, this may not be a verbation text due to low volume, interfer-ence, or unintelligible recordings.
02:11:30 A = Headquarters Operations Officer B = Licensee (A) NRC. (Name deleted).
(B) This is (name deleted) at Davis Besse in Ohio.
(A) Yes.
(B) We just recently had a trip. We had a main feed pump trip; we had a com-plete aux feed pump trip. We've got the aux feed pumps back now and the plant appears to be stable.
(A) Yeah, what was the cause of the reactor trip?
(B) It's undetermined right now, but the MSIV's both closed and as far as I know that's... that's what we know as far as the initiating event, at the moment. The shift supervisor might know more; I don't.
(A) Okay, I'll need to know what would be the cause of the reactor trip once you determine it.
8507300212 850613 (B) Okay. (DR ADOCK 05000346 PDit 06/13/85 1 DAVIS BESSE INCIDENT
I
.. u (A) Do you have a time for the reactor trip?
(B) Hang on just a second. .. 0133.
(A) Okay; so you said that you: main feedwater pumps tripped?
(B) The main feedwater pumps tripped; the aux feedwater pumps either failed to initiate or tripped. At any rate, they weren't running when I came in.
(A) Okay, have you determined what the cause of that problem was?
(B) What's that?
(A) Have you determined what the cause of the aux feedwater pump trip is?
(B) No, we haven't.
(A) Okay, is that still under investigation?
(B) That's still under investigation. They seem to be, seem to be controlling okay right now though, manually, s0.....
(A) Okay. And what was the cause of the main feedwater pumps tripping? Do you know?
(B) That we don't know. We had been having trouble with them before and we have a whole lot of the instrumentation attached there. It will be hours before we get to investigating that, so... We also don't have, we broke condenser vacuum because of drop in steam header pressure while we were trying to get back off the aux feed pump.
(A) Anything else unusual or not understood?
(B) Not anything that I can really think of right now. I gotta get your name now.
06/13/85 2 -DAVIS BESSE INCIDENT
. Vw (A) My name is (name deleted).
(B) What was it?
-(A) (Name deleted). That's spelled (name deleted)...
'(B) (Name deleted)...
-(A) ...(namedeleted)...
(B) ...I didn't...
(A) Okay, that's (name deleted). (Namedeleted).
(B) All right. (Name deleted)... I just can't hear you real well. (Name deleted)...
(A) ...(name deleted). (Name deleted). (Namedeleted).
(B) Okay.-
(A) Okay, what was the power prior to the trip?
(B) What was the power at the time of the trip?-
(A) Right.
(B) I believe about 90%.
(A) 90%. And you're in Mode 3 right now?
(B) Ah...
.(A) Hot shutdown?
06/13/85 3 DAVIS BESSE INCIDENT
V
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(B) Yeah, I believe so.
(A) Okay. And you're calling this under a notification of 50.72?
(B) I don't know what the notification number would be.
(A) Yeah, I'll need to know that. I need why you're calling this in.
(B) Uh, that's uh, that I don't know. You're talking about CFR numbers?
(A) I need to know why you're notifying me. Are you declaring an Unusual Event?
(B) Yeah. We.'do have an unusual event.
(A) Okay, that is very important, I need to know that. Okay, what time did you declare this an unusual Event?
(B) What's that? (Note: He appears to be talking to control room personnel).
(A) What time did you declare this--
(B) Hold.that. We haven't declared an Unusual Event. We are just in the pro-cess of evaluating it.
(A) Okay, so you are not, did not declare an unusual event.
(B) Yeah.
(A) Okay, so you're saying the plant is stable right now?
(B) The plant appears to be stable right now. I'll get back to you as soon as I find a little more on this.
(A) Okay. Thanks a lot.
06/13/85 4 DAVIS BESSE INCIDENT
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-(B) Uh-huh.
(A) Goodbye. ,
(A) Wait, hold it for a minute there! You called the resident inspector on this?
(B) Uh, I don't know about that yet. I.can, I'll inquire and if we haven't I'll make sure he's notified. t (A) Okay, good enough. Thank you.
(B) Uh-huh,
[ENDOFCONVERSATION]
1 02:15:37 i
s 06/13/85 5 DAVIS BESSE INCIDENT'
e 's n I
The next telephone conversation occurs at 02:17:00 and is a notification by the Operations Officer to the Regional Outy Officer. This conversation is inter-rupted at 0218 by a call back from the Licensee A = Headquarters Operations Officer B = Licensee C = Regional Duty Officer (C) Hello.
(A) (Name deleted), this is (name deleted), Headquarters.
(C) Yes.
(A) Davis Besse took a reactor trip at 0133.
(C) Okay, let me get to the other phone so I can take this information down, okay?
(A) Okay.
[There is a pause on the tape here]
(C) That okay? '
(A) Okay. They took a reactor trip, the cause is still unknown. #
(C) Okay.
P (A) Okay. The main feedwater pump tripped on them, cause unknown. The aux feedwater pump tripped on them, cause unknown.
(C) The aux feedwater?
(A) Yes.
06/13/85- 6 DAVIS BESSE INCIDENT
,ui (C) That's interesting.
(A) It is. Could you hold on for a minute please?
(C) Sure can.
(A)-They'recallingmeback.
(C) All right.
[CONVERSATIONisinterrupted]
02:18:29 (A) NRC,(namedeleted).
(B) Yes, (Name deleted), this is (name deleted) again.
(A) Yes, (name deleted).
(B) Uh, the initiating event was a main feed pump one trip.
(A) Okay.
(B) And exactly what happened after that I still can't tell you too good. .
We're just working on figuring everything else out.
(A)-Okay. And so, could you give me a call back once you have, determined the cause of the feedwater pump trip? And also we're interested in the aux feedwater pump trips also.
(B) Yeah, like I said. I'm not sure whether that was a trip or a failure to initiate, but at any rate they wanted to--it didn't come on by itself, s0.....
06/13/85 7 DAVIS BESSE INCIDENT
. Ls (A) Okay, so if you, once you determine that information you could pass it on to me we would appreciate it.
(B) Yeah, do you want to hold the line or anything?
(A) Oh, no, that's not necessary but, and also I need to know your evert classification.
(B) I know, I've been trying to get them to declare but we haven't yet, so...
(A) Okay. Keep me in touch, please.
(B) Okay.
(A) Okay, thanks.
(B) Bye.
[END OF CONVERSATION, CONTINUATION OF ORIGINAL CONVERSATION WITH THE REGIONAL DUTYOFFICER]
02:19:25 (A) Hello?
(C) Hello,(namedeleted)?
(A) Okay, the cause of the reactor trip appears to be the main feedwater pump No. I tripped.
(C) Did they just call you back?
(A) Yes, they did. Evidently the person who was talking to me is real disori-ented. In fact, they know very little about this event it seemed like.
However, the plart is stable. Okay, for the aux feedwater pump they're 06/13/85 8 DAVIS BESSE INCIDENT
. 6 L e, not sure whether the pump initiated, and tripped, or it failed to initi-ate. But in any case the aux feedwater pumps, they are operating right
.now, and they're operating normally.
(C) So they tripped and then they restarted them evidently.
(A) Well, this person appears did not know the information.
(C) Did they trip? Do we know that for sure?
(A) No, we don't.
(C) Okay. I'll just put down ' tripped?' for right now then.
(A) Right and once that guy gets back to me, apparently they're scurring around to see what's going on with this, but I will have a good nice talk to him once he calls me back again. Make sure we get all these questions
. cleared up.
(C) Okay.
(A) Evidently this person must have been the operator, STA, or something talk-ing to me; you know the other people are busy.
(C) Okay, so the cause was a feedwater problem, then.
(A) Right.
(C) Okay, say that their main steamline isolation valve closed on 'em...
(A) Okay.
(C) Other than that, that's about all I know about_at this point. The reactor was tripped from 90% power, now it's in Hot Shutdown; stable.
06/13/85 9 DAVIS BESSE INCIDENT
. ._ .- -. . . - - - . - . - . .- .. ~_ - . .. . -
. t. o '
(A) Okay. How about giving me some times? L
- (C) Okay, the reactor tripped at 0133. [
] (A) That Central?
i
-(C) Let's see. That'll be Eastern, s
3 (A) Okay.
(C) And they called me up at 0211...
T i
(A) Okay.
(C) And at this time the individual said he wasn't sure whether the resident j inspector was notif!ed but was going to make sure he will be notified.
1 l (A) Okay.
1
! (C) And also the individual will get back to me with their event classifica-tion. He is not familiar with the 50.72.
(A) I'm not surprised.
1 I
(C) Okay.
I i
l (A) I'll give you a call back once I.get the rest of the information from them.
l ,
(C) Okay. Very good. Anything'else?
f 4
- (A)'That' sit.
{ (C). Okay. Thank's a lot.
06/13/85 10 DAVIS BESSE INCIDENT
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(A) All right.
(C) Bye.
[ENDOFCONVERSATION]
02:21:57 06/13/85 11 DAVIS BESSE INCIDENT
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l The next conversation occurs at 02:26:24 and is the plant calling the Opera-l tions Officer to declare an Unusual Event.
i A = Headquarters Operations Officer B = Licensee (A) NRC; (name deleted).
(B) Yeah, (name deleted) this is (name deleted) again.
(A) Yes, (name deleted).
l (B) We do have an Unusual Event at least now. At 0225.
l (A) Okay, 0225. Okay, and repeat, is the plant stable?
(B) What's that?
(A) Plant stable right now?
(B) Yes, we're stable right now.
(A) Okay. What's the reason why you declared an unusual Event?
(B) Basically, I guess, we would have declared earlier on an Alert based on loss of--a Site Area Emergency based on the loss of all feedwater, but since it was quickly restored before we could--within a few minutes before we could get into the emergency plan, we're not really in any obvious sec-tion of the emergency plan, but since we're uncertain as to what the cause l of the loss of initiation or the lack of initiation of aux feedwater was, and since the main feedpumps are tripped still, the Shift Supervisor's a little uneasy about things and that's why he wants some emergency plan activation.
l (A) Right. Okay, it sounds good. So you'll keep ne posted?
l 06/13/85 12- DAVIS BESSE INCIDENT l
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(B) Oh-huh.
(A) Okay. Thanks a lot.
(B) Yeah.
[ENDOFCONVERSA',10N]
02:27:39 06/13/85 13 DAVIS BESSE INCIDENT
.. c ..
I The next conversation occurs at 0233 and is the Headquarters Operations Officer notifying the Regional Duty Officer of the notification of Unusual Event.
A = Headquarters Operations Officer C = Regional Duty Officer (A) Hello.
~
I (C)'0kay. (Name deleted), this is (name deleted) again.
(A) Yes.
(C) Okay, I just got a call back from Davis Besse and they have declared an Unusual Event.
(A) Okay.
(C) Okay, due to the questionable operation of the aux feedwater pump.
(A) Okay.
(C) Okay. Other than that the plant is still stable,'and they're still inves-tigating the cause of the... either the pump tripped or failed to start.
(A) Either it tripped or it failed to start.
(C) .Right.
(A) Okay, very good.
(C) Okay, I'll keep you posted.
(A) Okay, thanks.
l 06/13/85 14- DAVIS BESSE INCIDENT .I l
_ _ _ _ _ _ _ _ _ ___________i
I o 4 o (C) Okay, bye.
[ENDOFCONVERSATION]
02:33:50 06/13/85 15 DAVIS BESSE INCIDENT
.. 4 a The next conversation occurs at 02:39:40 and is the Operations Officer notify-ing the Emergency Officer.
A = Headquarters Operations Officer D = Errergency Officer (D) Hello.
(A) Yes, (name deleted). Thisis(namedeleted), Headquarters.
(D) Yes.
(A) Okay, Davis Besse declared an Unusual Event due to a reactor trip and a bunch of weird things happened after the reactor tripped. The reactor trip was caused by a main feedwater pump tripping, which then isolated the main steam isolation valve. The problem arises'when the aux feedwater pump failed to--either failed to start or---
(D) Whoa, whoa, whoa, hold on. The main feed pump tripped and that isolated the main steam isolation valve?
(A) Pardon me?
(D) The feedwater pump tripped and you said that automatically isolated the main steam isolation--
(A) Hey, I didn't say 'automatica11y'. That's what they told me.- I still--
that's one question I gntta ask them. Probably it...it's usually designed to isolate with less than 600 lbs of steam pressure.
(D) Right, it's a safety va'.ve.
(A) And so, if you trip a pump.
06/13/85 16 DAVIS BESSE. INCIDENT-
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(D) If you trip a pump the pressure goes up. Alright, go ahead. What else?
(A) Anyway, the problem arose when the aux feedwater pump either failed to start or it imediately tripped.off after starting. But it had to be ini-tially manually initiated. Okay. And that occurred for about 5 minutes and they started their pumps up. And so the plant is stable, everything is normal right now. The aux feedwater pump is still operating as normal but the cause of the problem on the aux feed pump is still undetermined at this time.
(D) And so the plant is' stable.
(A) Uh, yes.
(D) Okay. And does the Region III Duty Officer know?
(A) Uh, yes he does.
(D) Okay, fine. Okay, thanks for calling, (name deleted).
(A) Okay, good'enough.
3 (D) Bye.
.[ENDOFCONVERSATION]
02:41:20 l-06/13/85 17 DAVIS BESSE INCIDENT
.. % 0 The next conversation occurs at 02:53:38 and is a call from RIII Staff to the Operations Officer for an update. (Region III) is very difficult to understand on the tape.
A = Headquarters Operations Officer E = Region III Staff (A) NRC, (name deleted).
(E) Yes. Hi. (Name deleted) from RIII. I just got a call from my resident at Davis Besse...
(A) Yes.
(E) That they've had a trip.
(A) Right.
(E) And, that he was going to go out and see what the devil was going on. He didn't get any details, but they'd gotten themselves in a tight fix.
(A) Yes.
(B) What did the licensee tell you?
(A) Okay, now who's this speaking, please?
(E) This is (name deleted). I'm a section chief...
(A) Okay, (name deleted). They called me up on a reactor trip.
(E) Right.
06/13/85 18 DAVIS BESSE INCIDENT
~.
. 4 .
(A) Let me get my sheet out. Okay, the cause of the trip, which they told me on the second phone call, was due to main feedwater pump No. I tripping.
(E) Right, and they had the problem with the auxiliary feed pumps.
(A) Right. And they also had a main steam isolation valve isolation. The biggest problem was the aux feedwater pump had to be manually started be-cause it either failed, or failed to start, or tripped. And that cause is still under investigation.
(E) Did they declare .it an Unusual Event?
t (A) Yes, they did. This was after I questioned the fact that the person who was talking to me knew very little information, and it took a third phone call.in order to declare an Unusual Event. I asked him what the event 3
classification was, and he said at that time he didn't know.
02:55:00 (E) I was just looking in our NRC book and it says that one of the initiating conditions for notification of an Unusual Event would be loss of engi-neered safety feature or fire protection system function requiring shut-down by technical specification. I would say that any danger of losing auxiliary feedwater would automatically qualify as an Unusual Event.
(A) Right. But in their emergency plan the loss of the aux feedwater system is declared a site area emergency.
(E) Oh? But did they say they declared a site area emergency?
(A) No, they didn't. Okay, within a couple minutes they' started the pumps, and by that time they weren't even in their emergency plan.
(E) Is the plant stable?
06/13/85 19 DAVIS BESSE INCIDENT
. .. - 4 s (A) Yes. The plant is stable and the aux feedwater system was operating prop-erly within, I think, five minutes, they mentioned, after the reactor trip.
(E) Well, anyway I thought I'd call to let you know that (name deleted) and (name deleted) both probably be there within a half hour to forty five minutes.
(A) That's probably a good idea because the person I talked to knew very lit-tie information, and they seemed pretty disoriented when I talked to him on the phone.
(E) Right, I think, did you tell the Region III Duty Officer.....
(A) Yes, I did.
1 (E) When did you call him? At Home?
1 (A) Pardon me?-
(E) When did you call him? We need to follow up. I'd like to suggest you call him back when I hang up.
(A) Okay. I called him about 15 minutes ago.
(E) Oh, woke him up to take the call?
(A) Right.
(E) Okay, thanks very much.
1 N
ll 06/13/85 20 DAVIS BESSE INCIDENT
. *o (A) Okay. Thanks for the info.
(E) Okay. Bye.
[ENDOFCONVERSATION]
02:57:02 06/13/85 21 DAVIS BESSE INCIDENT
. 9 .
i l The next conversation occurs at 03:06:16 and is a call from the plant to the Operations Officer reporting an update on their status.
A = Headquarters Operations Officer i B = Licensee (A) NRC, (name deleted).
(B) Yes sir. This is (name deleted), shift supervisor at Davis Besse.
(A) Yes, (name deleted).
(B) Can you give me your name again, please?
i (A) My name is (name deleted).
(B) Okay. Uh, it's the same one we talked to earlier. Do you have any ques-tions for me?
I (A) I sure do.
(B) Okay.
(A) What was the cause of the isolation of your main steam isolation valves?
, (B) I'do not know.
(A) It's still under investigation?
(B) There were...we had no~ conditions at the time that would have caused those to close.
(A) Okay. Have you determined the cause of your main or ' aux feedwater from tripping?
06/13/85 22 . DAVIS BESSE' INCIDENT
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3 (B) The main feed. pump? ,
(A) Yes.
(B) Are you talking about the initial feedpump trip?
p
, (A) Yes.
k (B)' No, i
. (A) Okay.
1
-(B) I do not know what the cause of that.
(A) Okay, and have you determined the cause of the aux feedwater pump for not
. starting or tripping after start?
(B) No, not really. '
j- (A) 0kay.
1 i
(B)- It's still un' der investigation but we do have good control now.
j (A) Okay.
(B) No problem that way. 'We are stable on the secondary side 'and we're stable j on the primary side.
i.
I (A)- Okay, then I' guess that's 'all'I needed to'know. However, when you have.
determined the cause of your main . steam-isolation valves and your aux feedwater, and your main feedwater from tripping, could-you give me a call-back, please?
(B) We certainly.will, sir.
.06/13/85 23 DAVIS BESSE INCIDENT-
____. = . __ -. . .- - .- . . - . . - _ . - . - - . - , - - - . - . .-
0, e s.
(A) Okay. I also got word from Region III that both your resident inspectors are on their way.
(B) Okay. I did call one of them myself and talk to him.
(A) You should expect them within 20 minutes or so.
(B) Okay, sir.
(A) Okay. Thanks for the call.
(B) Thank you.
(A) Thanks, bye.
[END OF C0 VERSATION]
03:07:53 06/13/85 '24 DAVIS BESSE INCIDENT
., 'u e The next conversation occurs at 0511 when the Operations Officer calls the plant for the routine morning status report.
A = Headquarters Operations Officer B = Licensee (B) Hello, Davis Besse.
(A) Yes, good morning, your status.
(B) Okay. Right now we have the startup feed pump running and it's supplying
- feedwater to both steam generators. We have both aux pumps, feedwater pumps available but not pumping water. Right now we're in the process of reestablishing vacuum in the condenser and normal post-trip lineup.
, (A) Okay. Any new news on all the trips?
(B) All what trips?
(A) Oh, the cause of the main feedwater...
(B) Oh, okay. No, there's no... we've got some chart recorders that have data on them. We're analyzing it. The feed pump did trip and appeara to be on a... well, we've got indication that it may have been on overspeed.
(A) Okay.
(B) We have no... we do understand we had a what we call a steam and feedwater rupture control system trip concurrent with the feed pump trip. And that was what isolated... did the isolation and secured the other main feed 4
pump.
(A) Oh, okay.
06/13/85 25 DAVIS BESSE INCIDENT
. . .. s
'1 (B) And then both aux feedwater pumps started but tripped due to problems with their trip throttle valve.
. (A) 0kay. So you're telling me the trip throttled this valve?
i (B) We originally thought it was overspeed because that's the only thing that
. really trips them but we're, we're thinking, we're having problems with
- the trip throttle valve. And once they were ...the trip throttle valves were reset they've been running. We've had one system that has not, one auxiliary feedwater system that we've declared inoperable, although it's available; we just don't have the proper control.
(A) Okay. You still in your Unusual Event?
! (B) Be're still on the unusual event. We could get out of it, but we'd like to stay in it until we get vacuum restored and get off of our safety systems.
(A) Okay. It sounds pretty good.
(B) Okay.
4 (A) Thanks for the info.
- (B) All right. Thank you.
[ENDOFCONVERSATION]
05:13:38 i
a 4
06/13/85 26 DAVIS BESSE INCIDENT
e 4 a The next two conversations occur at 07:49:32 and 0753, respectively. One to the Region III duty officer and the second one to the emergency officer for an update.
A = Headquarters Operations Officer C = Region III Duty Officer D = Emergency Officer (C) Hello.
(A) Hey,(namedeleted). This is (name deleted), Headquarters.
(C) Okay. Let me get down to my other phone.
(A) Okay.
[ PAUSE, WHILE PHONES ARE SWITCHED]
(C) Okay.
(A) Okay. I called back Davis Besse during the morning status calls, and they cleared some information for me. Okay, the aux _feedwater pumps apparently had problems with the trip throttle valve.
(C) Say that again?
(A) The aux feedwater pump...
(C) Okay, aux feedwater pump...
(A) Right. Apparently had some problems with the trip throttle valve.
(C) Okay. Problems with trip throttle valves.
l i
06/13/85 27 DAVIS BESSE INCIDENT.
1
.-~ - . . . , , ..
.- o .
(A). Right. And they suspect that to be the problem of why it tripped off. But
~
they're still investigating.
(C) Okay.
(A) Okay, the MSIV closure, OK, is still a mystery. But, apparently it was actuated by the feed steam leak isolation system.
(C) Say that again, now?
(A) Okay, the cause of the main steam isolation closure was a result of the signal from the feedwater main steam leak isolation system.
(C) You're breaking up a little bit, I'm sorry. Try again.
(A) Okay. The reason why the main steam isolation valve closed was due to apparent signal from the feedwater steam main steam isolation signal.
(C) Okay.
(A) But it's still a mystery why it actually actuated.
(C) Okay.
(A) Okay,-that resulted in a tripping of the other main feedwater pump. So therefore they lost all main feedwater. Remember that the whole event initiated from the tripping of the No.1 main feedwater pump...
(C).0kay.
~
-(A) ...cause 'still unknown. At the same time the main steam isolation valve closed on 'em.
-(C) All right.
06/13/85 28 DAVIS BESSE INCIDENT i
.. o g (A) It is still under Unusual Event when I talked to them a couple hours ago; they will remain'so until they regain condenser vacuum.
(C) Okay.
(A)' Let me see. Other than that, that's about all I have for the Davis Besse event.
(C) Okay. The supervisor told me, after we talked, he and I talked, and he sent both .the resident and senior resident to the site. As soon as they get out there and get this thing sorted out, he told me-after he got a complete update a little later on this morning, probably around 8:00 o' clock our time, he's going to call me and give me a complete rundown.
(A)- Okay, sounds good.
(C) Okay?
(A) Okay, thanks.
(C) ' Bye.
[ENDOFFIRSTCONVERSATION]
07:53:05 07:53:53 (D) Hello?
(A)' Hello,.(name delete)? This is-(name delete), Headquarters?
(D) Yes.
06/13/85 29 DAVIS BESSE INCIDENT
.o o (A) Okay, let me give you an update on these two unusual events. Quad Cities terminated around midnight.
(D) Okay.
, (A) No problems. At Davis Besse, they're still in an Unusual Event and will remain so until they restore condenser vacuum.
l (D) Okay. They're still working on aux feed.
j (A) Right. And they suspect--
I f (D) I didn't realize they had lost condenser vacuum. Oh, but they had the main steam lines isolated.
(A) Right. And the cause of that's still unknown. But it happened at the same time when they lost the No. 1 main feedwater pump that started the a
whole show.
- (D) Okay, so they're still cooling with aux feed.
(A) Right.
(D) Are they dumping to.....?
(A) Hold on, (name deleted), no they're not cooling with aux feed. They se-cured aux feed; they restored feedwater pump. The start up feedwater pump.
i (D) Okay, but then they still have to dump the main conder.ser or--
-(A) Yeah, yeah, they're dumping that in the atmosphere, of course.
(D) They're~ dumping in the atmosphere.
1 06/13/85 30 DAVIS BESSE INCIDENT
.. s- a (A) Right.
(D) All this time. Wowl (A) So, other than that, they suspect the problem was the trip throttle valve for the aux feedwater.
(D) ..is why they had trouble starting them?
(A) Right. They thought it was overspeed but that's the only thing that can trip th'ese things, but they're lo'oking at it a little closely, and they think that it could be a problem with the trip throttle valve. But when they reset it, everything was fine.
(D) Okay. Why? What was the problem with the condenser vacuum that they didn't get the main steam isolation valve open?
(A)- It takes some time to pump these things out. This was about an hour and a half ago during morning status, about 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> ago, when I talked to them.
(D) Oh, ekay.
(A) So, other than that'everything is normal.
(D) Okay, and you say Quad cities has ended their event?
(A) Yeah.
(D) Okay, thank you.
(A) Okay, good enough.
(D)_ Bye.
(A) Bye.
06/13/85 31- DAVIS BESSE INCIDENT
. o o
[END OF CONVERSATION]
07:56:00 06/13/85 32 DAVIS BESSE INCIDENT
/ 4' %
The following call occurred at 08:45:20 with the plant calling the Headquarters Operations Officer to notify him that they had terminated the Unusual Event.
A = Headquarters Operations Officer B = Licensee (A) NRC, (name deleted).
(B) Yeah, this is (name deleted), the shift supervisor at Davis Besse.
(A) Yes.
(B) I'm calling to inform you that we have downgraded out of the Unusual Event. We are no longer in our emergency plan.
(A) Okay. Phat time did you terminate the Unusual Event?
(B) 0840.
(A) Okay. Now what is the plant's condition right now? !
(B) We're in stable, normal, post-trip condition.
(A) Okay, is that Hot Shutdown?
(B) Hot Shutdown, Mode 3. No, Hot Standby, I'm sorry. Hot Standby, Mode 3.
(A) What are your plans of action right now?
(B) They are going to remain in Hot Standby and -investigate the cause of the various problems that occurred during the transient.
(A) Okay. You had mentioned a couple hours ago that you have one train of your aux feedwater system inoperable?
8 06/13/85 33 DAVIS BESSE INCIDENT
T~
o = a (B) Yes, that is true.
(A) Okay. Are you in any LC0 Action e,.atement?
(B) Yes, we're in an Action Statement for that. A 72-hour action statement.
(A) Okay, 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> to Cold Shutdown?
(B) To Hot Shutdown.
(A) Okay, anything else?
(B) No. That's all.
(A) Okay, your name please?
(B) (Name deleted). (Name deleted). I'll need your name, too.
(A) Okay. My name is (name deleted). That's spelled (name deleted).
(B) Okay. Thank you.
(A) Okay. Thanks for the call.
(B) Thank you.
(A) Bye.
08:47:06 08:48:15 (A) Hello, this is (name deleted).
06/13/85 34 DAVIS BESSE INCIDENT
r
..o si (B) ' Hey, (name deleted), this is (name deleted) again. I forgot to ask you what is the cause of the' aux feedwater system being out of service?
(A) The' turbine governor is malfunctioned. '.t would not control turbine speed correctly.
(B) Okay.- Thanks a lot.
(A) You're welcome. Thank you.
[ENDOFCONVERSATION]
- 06/13/85 35 DAVIS BESSE INCIDENT
~
. ba These last two calls were made by the Headquarters Operations Officer to the Region III Duty Officer (08:49:47) and Emergency Officer (08:51:40).
A = Headquarters Operations Officer C = Region III Duty Officer D = Emergency Officer (C) Hello.
(A) (Name deleted)?
(C) Yes.
(A) Thisis(namedeleted), Headquarters.
(C) Okay.
(A) Davis Besse terminated Unusual Event at 0840.
(C) Okay.
(A) Okay, they're stable in Hot Standby, Mode 3. Their plans are to stay in Mode 3 while they're investigating the reasons for the various malfunctions.
(C) 0kay.
(A)~ Okay, they're currently in a 72-hour-to-llot-Shutfnwn LC0 action statement because they had to take one of the trains of the aux feedwater system inoperable due to a turbine governor malfunction.
(C) Okay, they determined that that was the cause of the problem?
(A) 'Well, for one of the problems.
06/13/85 36 DAVIS BESSE INCIDENT a
.3 . '
f~ .
,3..
V _ o:c. b.,
- .(C) .One of the problems, okay.
'(A) Okay, so that's about it.
1 (C) Okay.
(A) Okay?-
(C) Very' good. Thanks.
)
[ENDOFCONVERSATION]
}
08:51:40
! -- (D) Hello.
I j -(A) Yes, (name deleted), this is (name deleted), Headquarters?
I
[ (D) Yeah.-
I j; .
j (A) = Davis Besse-terminated Unusual Event at 8:40.
- (D) Okay.
i (A) -0kay?
l .
(D) All right.
(A) Thank you, i
.(D) Bye p
', [ENDOFCONVERSATION]
i-
-06/13/85 ,- 37 : DAVIS BESSE INCIDENT .
2
7 s
08:52:00 This concludes the initial conversations taped during the Davis Besse incident on June 9, 1985.
06/13/85 38 DAVIS BESSE INCIDENT