ML20129H663

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Monthly Operating Rept for Mar 1985
ML20129H663
Person / Time
Site: Callaway 
Issue date: 03/31/1985
From: Goodenow R, Miltenberger S
UNION ELECTRIC CO.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
ULNRC-1077, NUDOCS 8506070631
Download: ML20129H663 (6)


Text

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MONTHLY OPERATING. REPORT DOCKET NO. 50-483 UNIT NAME CALLAWAY UNIT 1 DATE ApnTT a. loss COMPLs1su BY R. R COODENOW TELEPHONE (114)'676'-8460 -

PART A OPERATIONS

SUMMARY

MARCH 1985 Unit operated at full power for entire month except for a Reactor Trip on 3/3/85, as noted on Part E, and a scheduled shutdown on 3/29/85 due to a planned outage to remove startup strainers on main steam stops and control intercept valves.

During shutdown for the planned outage an Unusual Event was declared on 3/30/85 o due to a safety injection actuation on low steamline pressure on one of the four steamlines.

- PART B PORV AND SAFETY VALVE

SUMMARY

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None 8506070631 850331 PDR ADOCK 05000483 d 11 R PDR pF CA-#804 05/09/84

, QDP-ZZ-04204 Page 1 of 4

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Part C AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-483 -

UNIT Callaway DATE APRTT. 4. 1985 COMPLETED BY R. R. GOODENOW TELEPHONE (314) 676-8460 MONTH MARCH 19R5 a DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (MWe-Net)

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1 1108 17 1102 2 1112 gg 1098 1091 1097 3 3, ,

0 1096 4 3 21 1111 g 470 22 1108 1076 1101 7 23 8 1097 24 1109 1107 1108

, 3 10 1106 3 1104 33 1100 p 1091 g,

  • 1106 , 1064 13 1105 3 828 1099 y 0 14 1101 0 15 16 1034 CA-#804 05/09/64 Page 2 of 4 QDP-ZZ-04204

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Part D OPERATING DATA REPORT DOCKET NO.

50-483 UNIT Callaway DATE APRIL 4, 1985 R. R. COODENOW COMPLETED BY TELEPHONE (314) 676-8460 OPERATING STATUS MARCH 1985 gross MOURS IN REPORTING PERICO: 744

1. REPORTING PERIOO:
2. CURRENTLY AUTHORIZED POWER LEVEL (mwd: 3413 MAX. DEPENO. CAPACITY (m): Not vet known OEslGN ELECTRfCAL RATING IMWo.Noo: 1171* *At stretch reactor power level which is
o. not currently authorized under the operating license.
3. POWER LEVEL TO WHICM RESTRICTED (IP ANY) (MWo. Net)
4. REASONS FOR RESTRICTION llP ANYl:

THIS MONTH VR TO DATE CuMULATivt

. S.8. 2 2032.6 2335.1-

5. NUMSER OF HOURS REACTOR WAS CRITICAL .

0 0 0

s. REACTOR RESERVE SMuTOOWN MOURS . .
7. MOURS GENERATOR ON UNE . .

637.2 1976.5 2279.0 0 0 0 S. UNIT RESERVE SMUTDOWN MOURS .. .

. $.091.R19 5.916.689 6.918.214

9. GROSS TMERMAL ENERGY GENERATED IMWHI .

713,842 2,002,172 2.341,352 to. GROSS ELECTRICAL ENERGY GENERATED (MWM) . . . .

679.448 1,894.764 2.217.787

11. NET ELECTRICAL ENERGY GENERATED (MWM) . .

88.5% 94.1Y 94.87

12. REACTOR SERvlCE PACTOR . . . .... .

88.5% 94.1% 94.8%

13. REACTOR AvalLAstuTY PACTOR . . . ...

85.6% 91.5% 92.5%

14. UNI,7 SERVICE PACTOR . . . . ... . .

85.6% 91.5% 92.5%

i is. UNIT AvalLAeluTY PACTOR . .. . . . .

l NA NA NA

16. UNIT CAPACITY PACTOR (Umas MDCI .. .. . . .. .

l* 76.97*

78.0%* 74.9%*

17. UNIT CAPACITY P ACTOR IUmns Dw MWel . . . . . . . . .

f 8.4% 6.4% 5.6%

ts uMIT PORCEO OUTAGE MATE ..... . ... .. ... ..

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19. SMUTDOWNS SCHEDULED OVER NEXT S MONTMS ITYPE. DATE. AND OURATION OP EACMl: None 20.17 SMUT DOWN AT END OF REPORT PERICO. ESTIMATED DATE OP STARTUP: 4 /10/R 5 *
21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION): PORECAST ACHIEVEO INITIAL CRITICAuTy 10/2/84 f 10/24/84 INITI AL ELECTRICITY COMMERCIAL OPERATION
    • Unit fully operational. 12/19/84. Placed in commercial operation 4/9/85. CA-gqQ4 the date unit is reflected in rates charged to Missouri customers. 05/ vi84 Page 3 of 4 QDP-ZZ-04204

--- - --,v -y. , -- ..,,,,.:

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  • Part E DOCKET NO. 50-483 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Callaway APRIL 4, 1985 QATE COMPLETED BY R. R. GOODENOW MARCH 1985 TELEPHONE (314) 676-8460 REPORT MONTH METHOD OF TYPE SHUTTING DOtWe F: FORCED DURAYlON THE REACTOR OR NO. DATE S: SCHEDULED l HOURS) REASON REDUCING POWER CORRECTIVE ACTIONE/ COMMENTS 6 850303 Forced 58.3 A 3 Reactor Trip from 100% Power due to Pressurizer pressure. LER 85-016-00.

7 850329 Scheduled 48.5 B 1 Planned outage to remove startup strainers on main steam stops and control intercept valves.

SURAGARY:

i CA-f804

  • 05/09/84 Page 4 of 4 QDP-ZZ-04204

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UNION EtscTaic COMPANY CALLAWAY PLANT MAILING ADDRSSS:

P. O. BOX SSO FULTON. MO. SS2St April 9, 1985 Director, Resource'anagement M

U. S. Nuclear Regulatory Commission Washington, DC 20555 ULNRC-1077

Dear-Sir:

DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT 1 FACILITY OPERATING LICENSE NPF-30 MONTHLY OPERATING REPORT MARCH 1985 The enclosed Monthly Operating Report for March 1985 is

-submitted pursuant to section 6.9.1.8 of the Callaway Unit 1 Technical Specifications.

s .J S. E. Miltenberger Manager, Callaway Plant e n,

,/WRC/RRG/drs MET Enclosure cc: Distribution attached _...

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ec distribution for ULNRC-1077.

with' enclosures

, Mr.' James G. Keppler Regional Administrator Office of Inspection & Enforcement U. S.-Nuclear Regulatory Commission-

-Region III 799: Roosevelt Road Glen Ellyn, IL 60137

- Director Office of Inspection'& Enforcement U. S. Nuclear Regulatory Commission

- Washington, DC .20555

- NRC Resident Inspector

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