ML20129H663

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Monthly Operating Rept for Mar 1985
ML20129H663
Person / Time
Site: Callaway 
Issue date: 03/31/1985
From: Goodenow R, Miltenberger S
UNION ELECTRIC CO.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
ULNRC-1077, NUDOCS 8506070631
Download: ML20129H663 (6)


Text

- _ - ___ _____

MONTHLY OPERATING. REPORT DOCKET NO.

50-483 UNIT NAME CALLAWAY UNIT 1 DATE ApnTT a. loss COMPLs1su BY R.

R COODENOW TELEPHONE (114)'676'-8460 PART A OPERATIONS

SUMMARY

MARCH 1985 Unit operated at full power for entire month except for a Reactor Trip on 3/3/85, as noted on Part E, and a scheduled shutdown on 3/29/85 due to a planned outage to remove startup strainers on main steam stops and control intercept valves.

During shutdown for the planned outage an Unusual Event was declared on 3/30/85 o

due to a safety injection actuation on low steamline pressure on one of the four steamlines.

PART B PORV AND SAFETY VALVE

SUMMARY

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None 8506070631 850331 d

PDR ADOCK 05000483 11 R

PDR pF CA-#804 05/09/84 QDP-ZZ-04204 Page 1 of 4

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Part C AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-483 UNIT Callaway DATE APRTT. 4. 1985 COMPLETED BY R. R. GOODENOW TELEPHONE (314) 676-8460 MONTH MARCH 19R5 a

DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)

(MWe-Net)

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1 1108 17 1102 1112 1098 2

gg 1091 1097 3

3,,

0 1096 4

3 21 1111 470 1108

  • g 22 1076 1101 7

23 1097 1109 8

24 1107 1108 3

1104 1106 3

10 1100 1091 33 p

  • 1106 1064 g,

828 13 1105 3

1099 0

14 y

1101 0

15 1034 16 CA-#804 05/09/64 Page 2 of 4 QDP-ZZ-04204 r---

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l Part D OPERATING DATA REPORT 50-483 DOCKET NO.

UNIT Callaway APRIL 4, 1985 DATE R. R. COODENOW COMPLETED BY (314) 676-8460 TELEPHONE OPERATING STATUS 744 MARCH 1985 gross MOURS IN REPORTING PERICO:

1. REPORTING PERIOO:

3413 MAX. DEPENO. CAPACITY (m): Not vet known

2. CURRENTLY AUTHORIZED POWER LEVEL (mwd:

OEslGN ELECTRfCAL RATING IMWo.Noo:

1171*

  • At stretch reactor power level which is o.

not currently authorized under the operating license.

3. POWER LEVEL TO WHICM RESTRICTED (IP ANY) (MWo. Net)
4. REASONS FOR RESTRICTION llP ANYl:

THIS MONTH VR TO DATE CuMULATivt

. S.8. 2 2032.6 2335.1-

5. NUMSER OF HOURS REACTOR WAS CRITICAL 0

0 0

s. REACTOR RESERVE SMuTOOWN MOURS 637.2 1976.5 2279.0
7. MOURS GENERATOR ON UNE 0

0 0

S. UNIT RESERVE SMUTDOWN MOURS

. $.091.R19 5.916.689 6.918.214

9. GROSS TMERMAL ENERGY GENERATED IMWHI 713,842 2,002,172 2.341,352 to. GROSS ELECTRICAL ENERGY GENERATED (MWM)..

679.448 1,894.764 2.217.787

11. NET ELECTRICAL ENERGY GENERATED (MWM) 88.5%

94.1Y 94.87

12. REACTOR SERvlCE PACTOR 88.5%

94.1%

94.8%

13. REACTOR AvalLAstuTY PACTOR 85.6%

91.5%

92.5%

14. UNI,7 SERVICE PACTOR 85.6%

91.5%

92.5%

i is. UNIT AvalLAeluTY PACTOR l

NA NA NA l*

16. UNIT CAPACITY PACTOR (Umas MDCI 78.0%*

74.9%*

76.97*

f

17. UNIT CAPACITY P ACTOR IUmns Dw MWel..

8.4%

6.4%

5.6%

ts uMIT PORCEO OUTAGE MATE

19. SMUTDOWNS SCHEDULED OVER NEXT S MONTMS ITYPE. DATE. AND OURATION OP EACMl: None l

20.17 SMUT DOWN AT END OF REPORT PERICO. ESTIMATED DATE OP STARTUP:

4 /10/R 5

21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

PORECAST ACHIEVEO 10/2/84 f

INITIAL CRITICAuTy 10/24/84 INITI AL ELECTRICITY COMMERCIAL OPERATION

    • Unit fully operational. 12/19/84. Placed in commercial operation 4/9/85.

CA-gqQ4 05/ vi84 the date unit is reflected in rates charged to Missouri customers.

Page 3 of 4 QDP-ZZ-04204

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o Part E DOCKET NO.

50-483 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Callaway QATE APRIL 4, 1985 R. R. GOODENOW COMPLETED BY REPORT MONTH MARCH 1985 TELEPHONE (314) 676-8460 METHOD OF TYPE SHUTTING DOtWe F: FORCED DURAYlON THE REACTOR OR NO.

DATE S: SCHEDULED l HOURS)

REASON REDUCING POWER CORRECTIVE ACTIONE/ COMMENTS 6

850303 Forced 58.3 A

3 Reactor Trip from 100% Power due to Pressurizer pressure. LER 85-016-00.

7 850329 Scheduled 48.5 B

1 Planned outage to remove startup strainers on main steam stops and control intercept valves.

SURAGARY:

i CA-f804

  • 05/09/84 Page 4 of 4 QDP-ZZ-04204

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UNION EtscTaic COMPANY CALLAWAY PLANT MAILING ADDRSSS:

P. O. BOX SSO FULTON. MO. SS2St April 9, 1985 Director, Resource'anagement M

U. S. Nuclear Regulatory Commission Washington, DC 20555 ULNRC-1077

Dear-Sir:

DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT 1 FACILITY OPERATING LICENSE NPF-30 MONTHLY OPERATING REPORT MARCH 1985 The enclosed Monthly Operating Report for March 1985 is

-submitted pursuant to section 6.9.1.8 of the Callaway Unit 1 Technical Specifications.

s.J S. E. Miltenberger Manager, Callaway Plant e n,

,/WRC/RRG/drs MET Enclosure cc: Distribution attached

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f:[

cw p

3 ;.,

ec distribution for ULNRC-1077.

with' enclosures Mr.' James G. Keppler Regional Administrator Office of Inspection & Enforcement U. S.-Nuclear Regulatory Commission-

-Region III 799: Roosevelt Road Glen Ellyn, IL 60137

'- Director Office of Inspection'& Enforcement U. S. Nuclear Regulatory Commission

- Washington, DC.20555

- NRC Resident Inspector

- 1 h

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