ML20138M594
| ML20138M594 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 11/30/1985 |
| From: | Krieger K, Otoole J CONSOLIDATED EDISON CO. OF NEW YORK, INC. |
| To: | Taylor J NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| NUDOCS 8512230055 | |
| Download: ML20138M594 (7) | |
Text
. o OPERATING DATA REPORT
- DOCKET NO. 50-247 DATE 12-5-85 COMPLETED BY K. Krieger TELEPHONE 914-526-5155 OPERATING STATUS Indian Point Unit #2 Notes
- 1. Unit Name:
For the year to date, gross
- 2. Reporting Period: November 1985 2758 electrical generation has
- 3. Licensed Thermal Power (MWt): exceeded that for the pre-
'4. Nameplate Rating (Gross MWe): 1013 vious record full year (1983)
- 5. Design Electrical Rating (Net MWe):873
- 6. Maximum Dependable Capacity (Gross MWe): 900
- 7. Maximum Dependable Capacity (Net MWe): 864
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
None
- 9. Power Level To Which Restricted,If Any (Net MWe): None
- 10. Reasons For Restrictions,if Any: No ne This Month Yr.-to-Date Cumulative 720 8016 100105
- 11. Hours In Reporting Period
- 12. Number Of Hours Reactor Was Critical 720 7787.36 68453.08
- 13. Reactor Reserve Shutdown Hours 0 152.67 3398.37
- 14. Hours Generator On-Line 720 7677.41 AAA?7 ni
- 15. Unit Reserve Shutdown Hours 0 0 n
- 16. Gross Thermal Energy Generated (MWH) 1855601 20181onn 1799nsus -
- 17. Gross Electrical Energy Generated (MWH) 572230 _,
6322110 53630726
- 18. Net Electrical Energy Generated (MWH) 550751 6077638 51191545
- 19. Unit Service Factor 100 95.8 '66.4
- 20. Unit Availability Factor 100 95.8 66.4
- 21. Unit Capacity Factor (Using MDC Net) 88,5 88.6 59.5
- 22. Unit Capacity Factor (Using DER Net) 87.6 86.8 58.6
- 23. Unit Forced Outage Rate 0 3.4 o.n
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each):
Cycle 7/8 Refueling and Maintenance Outare, scheduled for 1-15-86 nnd n f n 60 day duration
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
/A
- 26. Units in Test Status (Prior to Commercial Operation): Forecast Achieved
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INITIAL CRITICALITY INITIAL ELECTRICITY / N/A [
COMMERCIAL OPERATION / /
B512230055 851130 7
/ / <hS y-DR ADOCK 0500
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-247 UNIT IP #2 DATE 12-5-85 E
COMPLETED BY
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TELEPHONE November 1985 .
MONTH f DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 1MWe-Net) y 840 g7 548 841 805 2 g 3 844 838 19 4 844 833 20 5
843 748 21 6
845 718 22 7
839 836 23 643 841 8 24 827 838 9 25 10 834 209 26 gg 824 146.
27 0lI 12 28 797 804 835 13 29 818 g4 30 834 827 -
15 31 _
16 838 l
INSTRUCTIONS On this format, list the aserage daily unit power level in MWe Net for each day in the reporting inonth. Compute to the nearest whole megawatt.
l (9/77) ,
1 L
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SU MARY OF OPERATING EXPERIENCE
, November 1985 Unit No. 2 operated at 100% reactor power until Friday, November 8,1985, when load .was reduced to approximately 200 We to facilitate visual
. verification of.a suspected reactor coolant leak at the gasketed cover plate joint on check valve 897D. This particular valve is in the
' discharge line tram No.'24 Safety Injection System Accumulator and is located immediately off the loop cold leg. After confirmation that the
<1eak was at the gasketed joint, load was returned to full power conditions.
With the following exceptions, the unit operated at full load for the remainder of the month:
o On November 12th reactor power was reduced to 90% as a result of higher than normal Steam Generator Chlorides. Power was returned to 100% on November 13th.
c,-- s o On November 17th reactor power was reduced to 64% to allow the cleaning of the tubes'in #23 Condenser.
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o On November 21st reactor power was reduced to 74% to allow -
shutdown of 22 MBFP (Main Boiler Feed Pump) to replace a leaking.
s hose in the high pressure control oil system. Power was returned to 100% on November 22nd.
o On November 26th reactor power was reduced to 15% to reduce radiation fields within containment to allow verification of qualified electrical equipment. Power was returned to 100% on November 28th.
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U 50-247 DOCKET NO.
UNITSHUTDOWNS AND POWER REDUCTIONS IP #2 UNIT NAME DATE 19 4 95 November 1985 COMPLETED BY v vh a ea >-
REPORT MONTH TELEPHONE 914-990siss
_ 5 E
- .{ g 3 j .E h Licensee ,Eg . Cause & Corrective No. Date g 'd g % yss Event g7 {"?
gU Action to H
f5 5 j;gg Report 2r. mo g Prevent Recurrence d5 N/A 85 11 08 S 0 H N/A N/A SD Valvex B Controlled load reduction to verify source of increased RCS leakage N/A 85 11 17 S 0 H N/A N/A HC IITexch D Condenser cleaning N/A 85 11 26 S 0 B N/A N/A IE SLECON Controlled load reduction to facilitat 2 verification of qualified electrical 8"
' equipment within vapor containment 85 11 27 building i 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F-Adininistrative 5 G-Operational Error (Explain) Exhibit I - Same Source 19/77) II-Ott er (Explain)
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MAJOR SAFEIT-RELATED CORRECTIVE MAINTENANCE November 1985 WR NO. SYSTEM COMPONENT DATE WORK PEPSORMED 23042 RVLIS Level Transmitters 11/27/85 Replaced existing LT-1311, 1312, 1321 transmitters with 1322 qualified transmitters 20278- ELEC Terminal Blocks, 11/30/85 Replaced terminal "T" Drains, blocks with qual-Terminal Box ified blocks, Seals and' Drains Installed "T" Drains on valve motor operators and installed terminal block box cover seals and drains 5
s-
- - J:hn D. O'Toob
%ce Presx1ent Consolidated Ed: son Company of New Ycrk. loc.
4 Irying Piace, New York, NY 10003 Telephone (212) 460 2533 December 16, 1985 Re: Indian Point Unit No. 2 Docket No. 50-247 Mr. James M. Taylor, Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Washington, D.-C. 20555 ATIN: Document Control Desk
Dear Sir:
Enclosed are twelve copies of the Monthly Operatirg Report for Indian Point Unit No. 2 for the month of November 1985.
Ver[ truly youys, jL , ff(C_
Encl.
cc: Dr. Thomas E. Murley, Regional Administrator Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pa. 19406 Senior Resident Inspector U. S. Nuclear Regulatory Commission P. O. Box 38 Buchanan, New York 10511
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