Similar Documents at Byron |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045A6941993-06-0404 June 1993 LER 93-003-00:on 930511,turbine Emergency Trip Oil Header Pressure Low Alert Received Followed by Reactor Trip & Turbine Trip Above P-8.Caused by Actuation of Overspeed Trip Relay.Faulty Power Supply Board replaced.W/930604 Ltr ML20024H2041991-05-22022 May 1991 LER 91-005-01:on 900817,preoutage Mod Work Initiated W/O Proper Operability Review Due to Programmatic Deficiencies. Daily Const Work Authorization Sheet formalized.W/910522 Ltr ML20029A6461991-02-20020 February 1991 LER 90-007-01:on 900612,main Steam Line Isolation Sys Declared Inoperable Due to Failure to Test Manual Initiation Handswitch.Caused by Deficiency in Procedure.Procedures reviewed.W/910219 Ltr ML18041A2251990-10-0303 October 1990 LER 90-006-00:on 900903,reactor Containment Fan Cooler 2C, Low Speed Fan Breaker Did Not Close,Resulting in Train a Safety Injection Signal.Caused by Miscommunication & Procedure Deficiency.Procedure revised.W/901003 Ltr ML20029A6901990-09-13013 September 1990 LER 90-011-01:on 900819,reactor Trip Occurred Due to Power Surge.Caused by Lightning Strike.Rod Drive Sys Will Be Modified W/New Model of Power Supply Less Likely to Cause Reactor trip.W/910221 Ltr ML20044B0991990-07-12012 July 1990 LER 90-007-00:on 900612,discovered That Steam Line Isolation Handswitch on Main Control Board Panel 1PM06J Not Tested During Past Refueling Outages.Caused by Deficient Procedure. All Similar Equipment Will Be reviewed.W/900712 Ltr ML20044A9871990-07-11011 July 1990 LER 89-005-01:on 890501,diesel Generator 1A Failed to Load to 5,500 Kw within 60 as Required.Caused by Max Fuel Setting on Fuel Control Sys Being Set Too Low.Vendor Instructions Added to Maint procedures.W/900629 Ltr ML20043D5841990-06-0101 June 1990 LER 90-006-00:on 900503,as Surveillance Underway All Indication on Digital electro-hydraulic Computer Panel Was Lost.Caused by Failure of Ampere Fuse Due to Short Circuit in Pushbutton.Lighting Circuit rewired.W/900530 Ltr ML20042G9121990-05-0808 May 1990 LER 87-012-01:on 870408,component Cooling Pump 1A Tripped When Surge Tank Level Dropped to Low Level Pump Trip Setpoint.Caused by Breakdown in Communication.Mod to Component Cooling Sys completed.W/900507 Ltr ML20042E1561990-04-0606 April 1990 LER 90-003-00:on 900307,individual Cell Voltage for Cell 53 Found to Be at 2.11 Volts,Contrary to Tech Spec Limit.Caused by Electrician Using Improper Acceptance Criteria Format & Inadequate Mgt Review of surveillance.W/900406 Ltr ML20006F7161990-02-16016 February 1990 LER 90-001-00:on 900118,determined That Containment Purge Isolation Sys Not Demonstrated Operable 100 H Prior to Start of Core Alterations.Caused by Cognitive Personnel Error. Task Force Formed to Review Tech Specs.W/900109 Ltr ML20006E1161990-02-0909 February 1990 LER 90-001-00:on 900118,during Functional Surveillance on Steam Generator Pressure Channel 526,channel 525 Spiked Low, Causing Reactor Trip & Safety Injection.Caused by Failure of Pressure Transmitter.Transmitter replaced.W/900126 Ltr ML20006D7401990-02-0505 February 1990 LER 87-004-01:on 870225,inadvertent Safety Injection Occurred During Maint Troubleshooting.Caused by Cognitive Personnel Error by Control Sys Technician Involved. Disciplinary Action Taken & Counseling done.W/900124 Ltr ML20005E2391989-12-26026 December 1989 LER 89-003-01:on 890227,area Radiation Monitor 2RT-AR012 Failed Automatic Checksource Test,Actuating Containment Ventilation Isolation Alarm.Caused by Faulty Detector. Detector Replaced & Monitor Returned to svc.W/891221 Ltr ML19327B9021989-11-0303 November 1989 LER 89-009-00:on 891005,conflicting Info Re Signals That Initiate Automatic Isolation of Steam Generator Blowdown Lines Found.Caused by Preservice Design Implementation Deficiency.Lines Isolated & Procedure changed.W/891103 Ltr ML19354D4681989-11-0101 November 1989 LER 89-008-01:on 890830,one Auxiliary Feedwater Suction Pressure Transmitter Calibr Not Head Corrected & Bases of Original Setpoints Not Questioned.Caused by Inadequate Procedures & Setpoint calculations.W/891101 Ltr 1993-06-04
[Table view] Category:RO)
MONTHYEARML20045A6941993-06-0404 June 1993 LER 93-003-00:on 930511,turbine Emergency Trip Oil Header Pressure Low Alert Received Followed by Reactor Trip & Turbine Trip Above P-8.Caused by Actuation of Overspeed Trip Relay.Faulty Power Supply Board replaced.W/930604 Ltr ML20024H2041991-05-22022 May 1991 LER 91-005-01:on 900817,preoutage Mod Work Initiated W/O Proper Operability Review Due to Programmatic Deficiencies. Daily Const Work Authorization Sheet formalized.W/910522 Ltr ML20029A6461991-02-20020 February 1991 LER 90-007-01:on 900612,main Steam Line Isolation Sys Declared Inoperable Due to Failure to Test Manual Initiation Handswitch.Caused by Deficiency in Procedure.Procedures reviewed.W/910219 Ltr ML18041A2251990-10-0303 October 1990 LER 90-006-00:on 900903,reactor Containment Fan Cooler 2C, Low Speed Fan Breaker Did Not Close,Resulting in Train a Safety Injection Signal.Caused by Miscommunication & Procedure Deficiency.Procedure revised.W/901003 Ltr ML20029A6901990-09-13013 September 1990 LER 90-011-01:on 900819,reactor Trip Occurred Due to Power Surge.Caused by Lightning Strike.Rod Drive Sys Will Be Modified W/New Model of Power Supply Less Likely to Cause Reactor trip.W/910221 Ltr ML20044B0991990-07-12012 July 1990 LER 90-007-00:on 900612,discovered That Steam Line Isolation Handswitch on Main Control Board Panel 1PM06J Not Tested During Past Refueling Outages.Caused by Deficient Procedure. All Similar Equipment Will Be reviewed.W/900712 Ltr ML20044A9871990-07-11011 July 1990 LER 89-005-01:on 890501,diesel Generator 1A Failed to Load to 5,500 Kw within 60 as Required.Caused by Max Fuel Setting on Fuel Control Sys Being Set Too Low.Vendor Instructions Added to Maint procedures.W/900629 Ltr ML20043D5841990-06-0101 June 1990 LER 90-006-00:on 900503,as Surveillance Underway All Indication on Digital electro-hydraulic Computer Panel Was Lost.Caused by Failure of Ampere Fuse Due to Short Circuit in Pushbutton.Lighting Circuit rewired.W/900530 Ltr ML20042G9121990-05-0808 May 1990 LER 87-012-01:on 870408,component Cooling Pump 1A Tripped When Surge Tank Level Dropped to Low Level Pump Trip Setpoint.Caused by Breakdown in Communication.Mod to Component Cooling Sys completed.W/900507 Ltr ML20042E1561990-04-0606 April 1990 LER 90-003-00:on 900307,individual Cell Voltage for Cell 53 Found to Be at 2.11 Volts,Contrary to Tech Spec Limit.Caused by Electrician Using Improper Acceptance Criteria Format & Inadequate Mgt Review of surveillance.W/900406 Ltr ML20006F7161990-02-16016 February 1990 LER 90-001-00:on 900118,determined That Containment Purge Isolation Sys Not Demonstrated Operable 100 H Prior to Start of Core Alterations.Caused by Cognitive Personnel Error. Task Force Formed to Review Tech Specs.W/900109 Ltr ML20006E1161990-02-0909 February 1990 LER 90-001-00:on 900118,during Functional Surveillance on Steam Generator Pressure Channel 526,channel 525 Spiked Low, Causing Reactor Trip & Safety Injection.Caused by Failure of Pressure Transmitter.Transmitter replaced.W/900126 Ltr ML20006D7401990-02-0505 February 1990 LER 87-004-01:on 870225,inadvertent Safety Injection Occurred During Maint Troubleshooting.Caused by Cognitive Personnel Error by Control Sys Technician Involved. Disciplinary Action Taken & Counseling done.W/900124 Ltr ML20005E2391989-12-26026 December 1989 LER 89-003-01:on 890227,area Radiation Monitor 2RT-AR012 Failed Automatic Checksource Test,Actuating Containment Ventilation Isolation Alarm.Caused by Faulty Detector. Detector Replaced & Monitor Returned to svc.W/891221 Ltr ML19327B9021989-11-0303 November 1989 LER 89-009-00:on 891005,conflicting Info Re Signals That Initiate Automatic Isolation of Steam Generator Blowdown Lines Found.Caused by Preservice Design Implementation Deficiency.Lines Isolated & Procedure changed.W/891103 Ltr ML19354D4681989-11-0101 November 1989 LER 89-008-01:on 890830,one Auxiliary Feedwater Suction Pressure Transmitter Calibr Not Head Corrected & Bases of Original Setpoints Not Questioned.Caused by Inadequate Procedures & Setpoint calculations.W/891101 Ltr 1993-06-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H5221999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Byron Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212B9261999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Byron Station,Units 1 & 2.With ML20210R3431999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Byron Station, Units 1 & 2.With ML20210E2251999-07-21021 July 1999 B1R09 ISI Summary Rept Spring 1999 Outage, 980309-990424 ML20209G1751999-07-0808 July 1999 SG Eddy Current Insp Rept,Cycle 9 Refueling Outage (B1R09) ML20207H7941999-06-30030 June 1999 Rev 0 to WCAP-15180, Commonwealth Edison Co Byron,Unit 2 Surveillance Program Credibility Evaluation ML20207H8071999-06-30030 June 1999 Rev 0 to WCAP-15178, Byron Unit 2 Heatup & Cooldowm Limit Curves for Normal Operations ML20207H7851999-06-30030 June 1999 Rev 0 to WCAP-15183, Commonwealth Edison Co Byron,Unit 1 Surveillance Program Credibility Evaluation ML20207H7771999-06-30030 June 1999 Rev 0 to WCAP-15177, Evaluation of Pressurized Thermal Shock for Byron,Unit 2 ML20209H3711999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Byron Station, Units 1 & 2.With ML20207H7561999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20207H7621999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20195J8001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Byron Station,Units 1 & 2.With ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206R6991999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Byron Station Units 1 & 2.With ML20195C7961999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) M980023, Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A)1999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) ML20205P7001999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Byron Station,Units 1 & 2.With ML20205B5091999-03-26026 March 1999 SER Accepting Relief Requests 12R-24,Rev 0 & 12R-34,Rev 0, Related to Second 10-year Interval Inservice Insp for Byron Station,Units 1 & 2 ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20204G3831999-03-19019 March 1999 Safety Evaluation Accepting Second 10-yr Interval ISI Request for Relief 12R-11 M990004, Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function1999-03-17017 March 1999 Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function ML20206A8831999-03-17017 March 1999 Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20204C7671999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Byron Station,Units 1 & 2.With ML20199G8271998-12-31031 December 1998 Rev 1 Comm Ed Byron Nuclear Power Station,Unit 1 Cycle 9 Startup Rept ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20202F6181998-12-31031 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20199E6371998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Byron Station,Units 1 & 2.With ML20202F6021998-12-31031 December 1998 Cycle 9 COLR in ITS Format & W(Z) Function ML20196K6731998-12-31031 December 1998 10CFR50.59 Summary Rept for 1998 ML20207H7731998-11-30030 November 1998 Rev 0 to WCAP-15125, Evaluation of Pressurized Thermal Shock for Byron,Unit 1 ML20207H8011998-11-30030 November 1998 Rev 0 to WCAP-15124, Byron Unit 1 Heatup & Cooldown Limit Curves for Normal Operation ML20198D1501998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195F8321998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Byron Nuclear Power Station,Units 1 & 2.With 05000454/LER-1998-018, Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a1998-10-0909 October 1998 Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154L5501998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20197C9051998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20151Z9651998-08-31031 August 1998 Revised MOR for Aug 1998 for Byron Nuclear Power Station. Rept Now Includes Page 9 Which Was Omitted from Previously Issued Rept ML20238F6551998-08-28028 August 1998 SE Authorizing Licensee Request for Relief NR-20,Rev 1 & NR-25,Rev 0 Re Relief from Examination Requirement of Applicable ASME BPV Code,Section XI for First ISI Interval Exams ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B3361998-08-14014 August 1998 B2R07 ISI Summary Rept,Spring 1998 Outage, 961005-980518 ML20237B4841998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Byron Nuclear Power Station Units 1 & 2 1999-09-30
[Table view] |
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fx Ctmmtnwealth
\ Byron Nuclear Station Edistn
/ ..
..o; i / 4450 North German Church Road Byron. lilinois 61010 February 21, 1991 Ltra BYRON 91-0110 U. S. Nuclear Regulatory Commission Document Cont.rol Desk Washington, D.C. 20555 Dear Sir The enclosed supplemental Licensee Event Report from Byron Generating Station in being transmitted t.o you in a ;ordance with the requirement.s of 10CTR50.73(a)(2)(iv).
This report is number 90-011; Docket tio. 50-454.
Sincerely, s
/ / &
R. Pleniewicz Station Manager Byron Nuclear Power ?tation RP/DK/mw Enclosure Licensee Event Report No.90-011 cci A. Dort Davis, NRC Region III uministrator W. Kropp, NRC Senior Resident Inspector INPO Record Center CECO Distribution List (0716R/0081R) 9103010259 900913
{DR ADOCK 03000454 FDR 1I\ {
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SUPFLEMENT TO DVR DVR NO.
0 01 - 90 - 109 STA UNIT YEAR NO.
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PART 1 lillLQ{_(yD{l Q[(MRELQ High Negative Flux Rate Reactor Trip due to Loss 08/19/10 0425 of Control Rod Drive Power Supplies during DATE 11 t't Lightning Strike BfA10tLIDi.3VffLEMENTAL P,EEQE1
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ACEPTANCEBYSTAi!0NREVIEW/ M ;L2 /
DATE h6 / 3 /N)
SUPPLEMENTAL REPORT APPROVED AND AUTHORIZED FOR DISTRIBUTION s I///-rL . /
/ /-
bA/
' STATIbH b hAbE / dad w
- (0716R/0081R-1)
LICENSEE EVENT REPORT (LER) 9 Fact,llty Namt (1) Docket Number (2) lagtj ] _ _ _
8yrrn. Unit 1 0.L51_0LOLollLil 4 L L or1 0 i_ 4 Title,(4) High Negative Flux Rate Reactvr Trip due to Eoss of Control Rod Drive Power Supplies during LI 2hin.ifg.1LE1).t-lten_LRaledh) . LI!LUnitidt) RepotLpejtllL _ Qlhtr_[AE111t i t1Jnt9hicl0L_
Month Day Year Year Sequential // Revision Month Day Year _ [A111tLyleinti loittLitumj2ttilL._.
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LIL LLL.UO_ .9 JO LI 1 11 0 l .1 LLL LlL LlL lillollllLLJ_
OPERATING LCh'ALIAIIt_ng.E e f the fo1Igwlna)_(l11 MODE (9) 1 20.402(b) __ 20.405(c) .JL 50.73(a)(2)(iv) _ 73.71(b)
POWER _ 20.405(a)(1)(1) _ 50.36(c)(l) __ 50.73(a)(2)(v) _ 73.71(c)
LEVEL , , _ _ _ 20.405(a)(1)(ii) _ 50.36(c)(2) ___ 50.73(a)(2)(vil) _ Other (Specif y (101 17 i L _._ 20.405(a)(1)(lii) _
50,73(a)(2)(t) _ 50.73(a)(2)(viii)(A) in Abstract
////////////////////////// _,_ 20.405(a)(1)(iv) _ 50.73(a)(2)(ii) _. 50.73(a)(2)(viii)(B) below and in
////////////////////////// _ 20.405(a)(1)(v) _ 50.73's)(2)(lii) _ 50.73(a)(2)(x) Text)
LICENSEE CONTACT FQR THIS LER (11)
Name TELLPHQULttyMECR AREA CODE J. Schros L Qgeratin.gJnalater Exten11gnl216 8l 1 l5 21314 l -l ILaLilJ COMPLETE ONE LIME FOR EACH CQM ONEN FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE' SYSTEM COMPONENT MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT MANUFAL. REPORTABLE /
TURER lQJP10L. TURER _103{PRQL. j/
I i l l I L_j l I I l l l 1 '/
l 1 I I I i l l I I 1 i Ll }
SUPfL(tiENTAL REPORT EEEECTED (14) Expected t!ontb._j.la.y llent Submission lyes (If ves. (QLnnit.ttJ)(PECTEDlVQdi$1]ON DATE) X l NO ABSTRACT (Limit to 1400 spaces, i.e, approximately fifteen single-space typewritten lines) (16) 8 l ll lI _
At 0425 on August 19, 1990, with severe lightning activity near Byron Station, a Unit I reactor trip occurred from 78% power. A lightning strike induced a voltage surge that activated nine out of ten over-voltage protection devices installed on power supplies in the rod drive (RO) ( AA) power cabinets. Inis activation released twelve out of fifteen rod control cluster assembly groups into the core and resulted in a high negative flux rate reactor trip.
Due to several Commonwealth Edison and industry wide lightning induced reactor trips, several modifications have previously been made to both the containment lightning protection system and the rod drive over voltage protectors.
The Rod Drive System will be further modi' led with a new model of power supply that is less likely to cause a reactor trip after a transient caused by lightning.
This event is reportable pursuant to 10CFR50.73 (a)(2)(iv) as a result of the automatic actuation of the Reactor Protection System.
(0716R/0081R-2)
-.---._---._.--_-_i
((. j LICEN$tE EVENT pEPORT (LER) TEXT Cot {lltiUATION Form Rev 2.Q_ ,
3- i fACl)!TY #4AME (1) DOCKET NUMDER (2) .MfLJNttDL! Lib) P Agt_.13 L._ l Year j/// $equential /j//j Revision 4 ff f
/// Number /// Number.;
Jyron; Unit' 1 0 1 5 l Q_l__QJ_Q l 4111 4 9i0 - 0 l 1 1._ l ' -
Q l1 0 12_ 0F Q,.lt TEXT Energy Industry Identification System (EMS) codes are identified in the text as (XX) "
A'.' PLANT CONQITIONS PRIOR TO EVEN{t Event Date/fime 08-19-90. / 0425 Unit 1 MODE 1 - 02ERL2 PEAL [pn Rx Power 181_ RCS ( AB) . Temperature / Pressure _gtmjLggnaling.
Unit 2 MODE I _P0rtI._QF t.tElian__ Rx Power.301_. RCS (AB]' Temperature / Pressure _ngts L gptraling_.
+
B; QL M IP_ TION OF EVEN1:
AT 0425 on August 19, 1990, with severe lightning activity near Byron Station, a Unit I reactor trip occurred. f rom 78% power due to Fower range (IG) high . negative flux rate. As expected after the trip, both Auxillary Feedwater pumps (AF) (BA) automatically started on $ team Generator to+2 level. The Unit was
- stabilized and recovered in accordance with Station emergency procedures with the reactor core temperature
' being controlled by main condenser steam dumps and steam generator. level maintaleed by both the 1A Auxiliary Feedwater Pump and the Unit One Startup Feedwater Pump. The Unit was maintained in Mode 3 (Hot
' Standby). Mode 1-(power operations) was entered following a reactor startup on 8-20-90 at=1225.
-i
- No systems or components were inoperable at the beginning of this event which contributed to this event.
Operator actions aided in restoring stable plant conditions af ter the event.
The NRC Operations Center w as notified 'of the event at 0525 on 8-19-90, pursuant to 10CFR50.72(b)(2)(ii), i An actuation of the Reactor Protection System is reportable pursuant to 10CFR50.73(a)(2)(lv).
C. 'CAUSE OF__ EVENT .
The Unit I five Rod Drive-(RO) (AA) power cabinets each contain two Lambda (model LME-24) 44 Volt direct current (VDC) power supplies and two Lambda-(model LCS-A24-6795) -24VDC power supplies. A unique feature-common._to the positive. supplies are the Over-Voltage Protection :(OVP)-devices (Lambda model LHOV-3)
. designed to protect the power cahinet's internal circuitry. If the sensed output of a positive power ,
supply excee$s +28VDC, the'0VP device will activate. This activation will short the associated power 7
-supply =and. force the;r W *i ct pnet s@ ply to pick up the cabinet load through auctioneering. Once the
.0VP device is " tripped". It can only be_ reset by de-energizing the shorted supply. Loss.of both positive !
. power supplies in a power cabinet through OVP activation will cause all the power cabinet's Rod Control Cluster' Assemblies (RCCAs) to fall into the core and . result in a reactor high-negative flux rate trip.
Innediately prior to.the reactor trip of this event,' a lightning = strike in the vicinity of.0yron Station induced a voltage surge that activated nine out of ten Over-Voltage Protection devices installed on the. ,
- positive 24 VOC power supplies in the Unit One' RD power cabinets. - This activation released twelve RCCA j groups out of the total fif teen into the corei These groups the caused the Negative Higk fluw Rate trip )
which then released the remaining three RCCA groups held t , the 2AC cabinet. l
- The most probable-root cause of the OvP activations sas lightning induced volteges on the RD system . !
cabling, Due to the elusive nature of lightning and the unkenwn location of-the lightning strikef the -
Induced voltage carrier is unknown. The ground cables and lightning rods were e ffied intact on both units.
The positive power supplies themselves may have allowed passage of the voltage transient and contributed to this event. The RO power cabinet negative power supplies. which are not over-voltage protected, did not contribute to the cause of this event.
!~
(0716R/0081R-3)
LECK$LLEYEHLREP9RLIMRLJEXI._MNIINVAI19N _. _ LettnattlaQ_
s FACI,tITY NA'ME (1) DOCKET NUMBER (2) _LLILtM10LR {6)-
Page R L,__
Year /
pp/ Sequential j//g/ Revision llL,/ httL- LLL hntL
.anobatt i LLLULLLLLL4L.5LL_LLO -
DJ i 1 1
- -- LLL_LIL .0L Lit TEXT Energy Industry Identification System (E!!$) codes are Identified in the tent as (XX)
D. $AFETY A%LY.113:
There were no adverse safety consequences as a result of this event, the health and safety of the public was at no time endangered. Other equipment important to safety was not affected by the storm.
E. CDELC11YLAtllMS:
After a similar event in 1985, several corrective actions were implemented to prevent recurrence.
Hodification M6-1-85-0516 improved the containment lightning protection by bypassing the containment liner in the lightning protection system and routing directly to the ground grid. This modification seems to have abated lightning influences beyond the Rod Drive system.
After the 1987 successive Unit One lightning trips, Modification M6-1-87-105 changed Unit One Rod Drive grounding such that cabinets were not separately grounded but grounded only at two points. This groundir.g scheme reduced circulating currents and is consistent with the Unit Two configuration.
Additionally, per Commonwealth Edison Engineering and Westlughouse recomendations, surge protection has been added to the RO over-voltage protectors and the trip setpoints increased on both Units. On 04-15-88, 2200 pr capacitors were installed across the base to emitter of transistor Q1 within the OVP devices on Unit One. This installation is equivalent to Lambda model LHOV-3 "$-option" and should relieve tow energy high frequency transients without activating the OVP device. On 2-16-90, Unit One OVP setpoints were changed from 26.5 Vdc to 28 Vdc.
On 10/21/90, Byron Nuclear Work Requests B80213 - 880222 were written to replace the Lambda LME-24 (+) 24 Vdc power supplies with Acopian model A24H1200 supplies. The Acoplan supplies will prevent unwarranted reactor trips with an automatic " reset" function. Upon activation of an OVP device, the Acopian supplies will cut out and re-energize in 50mS. The Acopian supplies will then provide control power to the still stationary RCCAs if the initiating over voltage condition no longer exists.
The Acoplan supplies are presently installed on the Unit Two Rod Drive System from the latest Unit Two refueling outage 02R02. The Unit One Acoplan power supply changeout will occur prior t; the completion of the the upcoming Unit One refueling outage BIR04. AIR
- 91-030 tracks completion of this activity.
i
- r. ERLY10VSJCCVERENCISI Since 1985, the OVP devices on the power cabinet positive power suoplies have tripped Unit One four times during thunderstorms. Below 15 a list of the events:
- OVP QAII UN11 ACIMA110NS LER 07-13-85 1 02 LER 85-068 07-29-87 1 09 LER 87-017 07-31-87 1 03 LER 87-017 08-19-90 1 09 LER 90-011 l
In all the above events, lightning caused a voltage surge sensed by the OVP devices which lead to their activation. Only the 1985 event caused additional damage beyond the Rod Drive system. Note also Unit Two has not experienced lightning induced reactor trips.
I (0716R/0081R-4) l
' ~' \
I L1RERELLyJHLIEPML EltRL. TEXT CANTINILAJlpN F QIm_@&y.,LL i FACDifY HAME (1) DOCKET NUMBER (2) JfLEVdDERJ6) __Past L3L__
Year /// Sequential //
,j/p Revision (pppR BunktL-. lR HunktL
,J,yrok. Uni t 1 0 1 5 1 0 1 0 1 0 i d1 Sl_4 910 -
0 l_1 11 - 0l t Ljd 0F Llt TEXT Energy Industry Identification System iEIIS) codes are identified in the text as (XX)
In addition, similar events have occurred at Zion and Braidwood and throughout the industry. IE Inf ormation Notice 85-86, " lightning Strikes at Nuclear Power Generating Stations," included events at Zion and Byron and the corrective actions as a result of the 7-13-85 trip, G- CEf0NLMT FAILVELDAIA:
Component failure did not initiete this event, nor did any failures result from this event, l
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