Similar Documents at Byron |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045A6941993-06-0404 June 1993 LER 93-003-00:on 930511,turbine Emergency Trip Oil Header Pressure Low Alert Received Followed by Reactor Trip & Turbine Trip Above P-8.Caused by Actuation of Overspeed Trip Relay.Faulty Power Supply Board replaced.W/930604 Ltr ML20024H2041991-05-22022 May 1991 LER 91-005-01:on 900817,preoutage Mod Work Initiated W/O Proper Operability Review Due to Programmatic Deficiencies. Daily Const Work Authorization Sheet formalized.W/910522 Ltr ML20029A6461991-02-20020 February 1991 LER 90-007-01:on 900612,main Steam Line Isolation Sys Declared Inoperable Due to Failure to Test Manual Initiation Handswitch.Caused by Deficiency in Procedure.Procedures reviewed.W/910219 Ltr ML18041A2251990-10-0303 October 1990 LER 90-006-00:on 900903,reactor Containment Fan Cooler 2C, Low Speed Fan Breaker Did Not Close,Resulting in Train a Safety Injection Signal.Caused by Miscommunication & Procedure Deficiency.Procedure revised.W/901003 Ltr ML20029A6901990-09-13013 September 1990 LER 90-011-01:on 900819,reactor Trip Occurred Due to Power Surge.Caused by Lightning Strike.Rod Drive Sys Will Be Modified W/New Model of Power Supply Less Likely to Cause Reactor trip.W/910221 Ltr ML20044B0991990-07-12012 July 1990 LER 90-007-00:on 900612,discovered That Steam Line Isolation Handswitch on Main Control Board Panel 1PM06J Not Tested During Past Refueling Outages.Caused by Deficient Procedure. All Similar Equipment Will Be reviewed.W/900712 Ltr ML20044A9871990-07-11011 July 1990 LER 89-005-01:on 890501,diesel Generator 1A Failed to Load to 5,500 Kw within 60 as Required.Caused by Max Fuel Setting on Fuel Control Sys Being Set Too Low.Vendor Instructions Added to Maint procedures.W/900629 Ltr ML20043D5841990-06-0101 June 1990 LER 90-006-00:on 900503,as Surveillance Underway All Indication on Digital electro-hydraulic Computer Panel Was Lost.Caused by Failure of Ampere Fuse Due to Short Circuit in Pushbutton.Lighting Circuit rewired.W/900530 Ltr ML20042G9121990-05-0808 May 1990 LER 87-012-01:on 870408,component Cooling Pump 1A Tripped When Surge Tank Level Dropped to Low Level Pump Trip Setpoint.Caused by Breakdown in Communication.Mod to Component Cooling Sys completed.W/900507 Ltr ML20042E1561990-04-0606 April 1990 LER 90-003-00:on 900307,individual Cell Voltage for Cell 53 Found to Be at 2.11 Volts,Contrary to Tech Spec Limit.Caused by Electrician Using Improper Acceptance Criteria Format & Inadequate Mgt Review of surveillance.W/900406 Ltr ML20006F7161990-02-16016 February 1990 LER 90-001-00:on 900118,determined That Containment Purge Isolation Sys Not Demonstrated Operable 100 H Prior to Start of Core Alterations.Caused by Cognitive Personnel Error. Task Force Formed to Review Tech Specs.W/900109 Ltr ML20006E1161990-02-0909 February 1990 LER 90-001-00:on 900118,during Functional Surveillance on Steam Generator Pressure Channel 526,channel 525 Spiked Low, Causing Reactor Trip & Safety Injection.Caused by Failure of Pressure Transmitter.Transmitter replaced.W/900126 Ltr ML20006D7401990-02-0505 February 1990 LER 87-004-01:on 870225,inadvertent Safety Injection Occurred During Maint Troubleshooting.Caused by Cognitive Personnel Error by Control Sys Technician Involved. Disciplinary Action Taken & Counseling done.W/900124 Ltr ML20005E2391989-12-26026 December 1989 LER 89-003-01:on 890227,area Radiation Monitor 2RT-AR012 Failed Automatic Checksource Test,Actuating Containment Ventilation Isolation Alarm.Caused by Faulty Detector. Detector Replaced & Monitor Returned to svc.W/891221 Ltr ML19327B9021989-11-0303 November 1989 LER 89-009-00:on 891005,conflicting Info Re Signals That Initiate Automatic Isolation of Steam Generator Blowdown Lines Found.Caused by Preservice Design Implementation Deficiency.Lines Isolated & Procedure changed.W/891103 Ltr ML19354D4681989-11-0101 November 1989 LER 89-008-01:on 890830,one Auxiliary Feedwater Suction Pressure Transmitter Calibr Not Head Corrected & Bases of Original Setpoints Not Questioned.Caused by Inadequate Procedures & Setpoint calculations.W/891101 Ltr 1993-06-04
[Table view] Category:RO)
MONTHYEARML20045A6941993-06-0404 June 1993 LER 93-003-00:on 930511,turbine Emergency Trip Oil Header Pressure Low Alert Received Followed by Reactor Trip & Turbine Trip Above P-8.Caused by Actuation of Overspeed Trip Relay.Faulty Power Supply Board replaced.W/930604 Ltr ML20024H2041991-05-22022 May 1991 LER 91-005-01:on 900817,preoutage Mod Work Initiated W/O Proper Operability Review Due to Programmatic Deficiencies. Daily Const Work Authorization Sheet formalized.W/910522 Ltr ML20029A6461991-02-20020 February 1991 LER 90-007-01:on 900612,main Steam Line Isolation Sys Declared Inoperable Due to Failure to Test Manual Initiation Handswitch.Caused by Deficiency in Procedure.Procedures reviewed.W/910219 Ltr ML18041A2251990-10-0303 October 1990 LER 90-006-00:on 900903,reactor Containment Fan Cooler 2C, Low Speed Fan Breaker Did Not Close,Resulting in Train a Safety Injection Signal.Caused by Miscommunication & Procedure Deficiency.Procedure revised.W/901003 Ltr ML20029A6901990-09-13013 September 1990 LER 90-011-01:on 900819,reactor Trip Occurred Due to Power Surge.Caused by Lightning Strike.Rod Drive Sys Will Be Modified W/New Model of Power Supply Less Likely to Cause Reactor trip.W/910221 Ltr ML20044B0991990-07-12012 July 1990 LER 90-007-00:on 900612,discovered That Steam Line Isolation Handswitch on Main Control Board Panel 1PM06J Not Tested During Past Refueling Outages.Caused by Deficient Procedure. All Similar Equipment Will Be reviewed.W/900712 Ltr ML20044A9871990-07-11011 July 1990 LER 89-005-01:on 890501,diesel Generator 1A Failed to Load to 5,500 Kw within 60 as Required.Caused by Max Fuel Setting on Fuel Control Sys Being Set Too Low.Vendor Instructions Added to Maint procedures.W/900629 Ltr ML20043D5841990-06-0101 June 1990 LER 90-006-00:on 900503,as Surveillance Underway All Indication on Digital electro-hydraulic Computer Panel Was Lost.Caused by Failure of Ampere Fuse Due to Short Circuit in Pushbutton.Lighting Circuit rewired.W/900530 Ltr ML20042G9121990-05-0808 May 1990 LER 87-012-01:on 870408,component Cooling Pump 1A Tripped When Surge Tank Level Dropped to Low Level Pump Trip Setpoint.Caused by Breakdown in Communication.Mod to Component Cooling Sys completed.W/900507 Ltr ML20042E1561990-04-0606 April 1990 LER 90-003-00:on 900307,individual Cell Voltage for Cell 53 Found to Be at 2.11 Volts,Contrary to Tech Spec Limit.Caused by Electrician Using Improper Acceptance Criteria Format & Inadequate Mgt Review of surveillance.W/900406 Ltr ML20006F7161990-02-16016 February 1990 LER 90-001-00:on 900118,determined That Containment Purge Isolation Sys Not Demonstrated Operable 100 H Prior to Start of Core Alterations.Caused by Cognitive Personnel Error. Task Force Formed to Review Tech Specs.W/900109 Ltr ML20006E1161990-02-0909 February 1990 LER 90-001-00:on 900118,during Functional Surveillance on Steam Generator Pressure Channel 526,channel 525 Spiked Low, Causing Reactor Trip & Safety Injection.Caused by Failure of Pressure Transmitter.Transmitter replaced.W/900126 Ltr ML20006D7401990-02-0505 February 1990 LER 87-004-01:on 870225,inadvertent Safety Injection Occurred During Maint Troubleshooting.Caused by Cognitive Personnel Error by Control Sys Technician Involved. Disciplinary Action Taken & Counseling done.W/900124 Ltr ML20005E2391989-12-26026 December 1989 LER 89-003-01:on 890227,area Radiation Monitor 2RT-AR012 Failed Automatic Checksource Test,Actuating Containment Ventilation Isolation Alarm.Caused by Faulty Detector. Detector Replaced & Monitor Returned to svc.W/891221 Ltr ML19327B9021989-11-0303 November 1989 LER 89-009-00:on 891005,conflicting Info Re Signals That Initiate Automatic Isolation of Steam Generator Blowdown Lines Found.Caused by Preservice Design Implementation Deficiency.Lines Isolated & Procedure changed.W/891103 Ltr ML19354D4681989-11-0101 November 1989 LER 89-008-01:on 890830,one Auxiliary Feedwater Suction Pressure Transmitter Calibr Not Head Corrected & Bases of Original Setpoints Not Questioned.Caused by Inadequate Procedures & Setpoint calculations.W/891101 Ltr 1993-06-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H5221999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Byron Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212B9261999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Byron Station,Units 1 & 2.With ML20210R3431999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Byron Station, Units 1 & 2.With ML20210E2251999-07-21021 July 1999 B1R09 ISI Summary Rept Spring 1999 Outage, 980309-990424 ML20209G1751999-07-0808 July 1999 SG Eddy Current Insp Rept,Cycle 9 Refueling Outage (B1R09) ML20207H7941999-06-30030 June 1999 Rev 0 to WCAP-15180, Commonwealth Edison Co Byron,Unit 2 Surveillance Program Credibility Evaluation ML20207H8071999-06-30030 June 1999 Rev 0 to WCAP-15178, Byron Unit 2 Heatup & Cooldowm Limit Curves for Normal Operations ML20207H7851999-06-30030 June 1999 Rev 0 to WCAP-15183, Commonwealth Edison Co Byron,Unit 1 Surveillance Program Credibility Evaluation ML20207H7771999-06-30030 June 1999 Rev 0 to WCAP-15177, Evaluation of Pressurized Thermal Shock for Byron,Unit 2 ML20209H3711999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Byron Station, Units 1 & 2.With ML20207H7561999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20207H7621999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20195J8001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Byron Station,Units 1 & 2.With ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206R6991999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Byron Station Units 1 & 2.With ML20195C7961999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) M980023, Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A)1999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) ML20205P7001999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Byron Station,Units 1 & 2.With ML20205B5091999-03-26026 March 1999 SER Accepting Relief Requests 12R-24,Rev 0 & 12R-34,Rev 0, Related to Second 10-year Interval Inservice Insp for Byron Station,Units 1 & 2 ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20204G3831999-03-19019 March 1999 Safety Evaluation Accepting Second 10-yr Interval ISI Request for Relief 12R-11 M990004, Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function1999-03-17017 March 1999 Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function ML20206A8831999-03-17017 March 1999 Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20204C7671999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Byron Station,Units 1 & 2.With ML20199G8271998-12-31031 December 1998 Rev 1 Comm Ed Byron Nuclear Power Station,Unit 1 Cycle 9 Startup Rept ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20202F6181998-12-31031 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20199E6371998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Byron Station,Units 1 & 2.With ML20202F6021998-12-31031 December 1998 Cycle 9 COLR in ITS Format & W(Z) Function ML20196K6731998-12-31031 December 1998 10CFR50.59 Summary Rept for 1998 ML20207H7731998-11-30030 November 1998 Rev 0 to WCAP-15125, Evaluation of Pressurized Thermal Shock for Byron,Unit 1 ML20207H8011998-11-30030 November 1998 Rev 0 to WCAP-15124, Byron Unit 1 Heatup & Cooldown Limit Curves for Normal Operation ML20198D1501998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195F8321998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Byron Nuclear Power Station,Units 1 & 2.With 05000454/LER-1998-018, Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a1998-10-0909 October 1998 Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154L5501998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20197C9051998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20151Z9651998-08-31031 August 1998 Revised MOR for Aug 1998 for Byron Nuclear Power Station. Rept Now Includes Page 9 Which Was Omitted from Previously Issued Rept ML20238F6551998-08-28028 August 1998 SE Authorizing Licensee Request for Relief NR-20,Rev 1 & NR-25,Rev 0 Re Relief from Examination Requirement of Applicable ASME BPV Code,Section XI for First ISI Interval Exams ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B3361998-08-14014 August 1998 B2R07 ISI Summary Rept,Spring 1998 Outage, 961005-980518 ML20237B4841998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Byron Nuclear Power Station Units 1 & 2 1999-09-30
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F N f) 4450 North61010 Byron,litinois G:rm.:n Church load January 24, 1990 Ltra BYRON 90-0130 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Dear Sir The enclosed Licensee Event Report from Byron Generating Station is being transmitted to you as a Supplemental Report.
This report is number 87-004; Docket No. 50-454.
Sincerely,
-a ?M '
.d R. Pleniewic %.
s Station Manager Byron Nuclear PowQ Station
.RP/dm Enclosures Licensee Event Report No.87-004 1
cci A. Bert Davis, NRC Region III Administrator W. Kropp, NR,C Senior Resident Inspector INPO Record' Center CECO Distribution List (0512R/0059R) fgg2]ggy Q 4 /
-S
, , Li(EN5(E [V[Ni R[ PORT (L(R) facility Name (1) Dock +,t Number (2) ,fane (3) tvron. Unit 1 01 El 01 01 01 41 El 4 1lef!0l4 11tle (4) ,
1%l!y[]LIENT SAFETY IN){LilQtlilVRING MAINTENAN(LlRQU$1LitDQllNG_CAViED BY A PERjQyNEL ERROR
-_11tnLE41tj5) LER Numbitjj) Rgggfl ptle (7) Other Facilitit1Jaralttd (8)
Month Day Year Year fj//j Sequential /jj//
/
f Revisto.. Month Day Year 13tility Names DolitLNumktris )
/// Numb.gr Uf,_Nightr.
NONE O!510101Of I l
~ ~
.pl_iL215 81 7 BJ7 01014 01 1 _Q l 2 01.5 Jl 0 01 51 01 01 01 l l_
OtfRATING gggt g9, lihtik one or mate of the fellowing) (111 5 20.402(b) _ 20.40$(c) .1 50.73(a)(2)(iv) 73.7)(b) :
POWER ,_ 20.405(a)(1)(1) 50.36(c)(1) _ 50.73(a)(2Hv) 73.71(c)
LEvil g g __ 20.40$(a)(1)(II) 50.36( c H 2) __ 50.73(a)(2Hvil) Other ($pecify 1101- _A i 0I Q_._ _ 20.405(e)(1)(lit) _ 50.73(a)(2HI) __ 50.73(a HCHviii)( A) in Abstract
/ /////////// ///// _ 20.405(aH1)(lv) 50.73(a)(2)(li) _ 50.73(a)(2)(viii)(B) below and in
/ ///////////
///// _ 20.40$(a)(1)(v) 50.73(a)(2 Hill) _ 50.73(a)(2Hx) Tent)
LICLN1LLLONIACT FOR THIS LER (12)
Name IELLl't9SLNVMi1LR -
ARLA C000 H. $n0 _Et9W3A LREL811 W C &fli t_IUPR EY110 P E111.2260 B l 1 1 5_ L_j4 l -l_11 41 4lj COMELLIE ONE LINE FOR EACH COM ONEN FAILygLDESCRibED IN THIS REPORT f13)
CAUSE SY$ TEM COMPONENT MANUFAC- REPORTABLE CAU$t $Y$ttM COMPONENT MANUTAC- REPORTABLE J UEER TO NPRDS . _ ,,IllRER 10 NPRDS l l !j !I I l __l l l I- I l-l l 1 [ l l I I I l l i I l l .
$UPPLLt4 ENTAL REPORT EXPECTED (14) Expected bortthl Day 1.lfA.C Submis: Ion Date (15) '
_llta 11 Lyt 140mpitie EXPLCILQJUBM131LDtLDAIE) X l NQ l l l I' l AB$fRACT (Limit to 1400 spaces, i.e, approximately fifteen single-space typewritten lines) (16)
On February 2$. 1907, Unit I was in Mode 5, Cold Shutdown, in preparation for refueling. Instrument Maintenance (IM) personnel were troubleshooting a problem with the Process Instrumentation and Control System. During this troubleshooting activity, an IM Control $ystem Technician (C$i), not cognizant of all the consequences of the action re-positioned a Solid State Protection System " Memory" switch. The repositioning of the switch unb.ocked an existing Main Steamline Low Pressure Safety Injection signal. A
$afety injection occurred at 1614 on February 25. 1987. The root cause of the event was a cognitive personnel error by the C$i involved and procedural personnel errors by all IM's involved in the troubleshooting by not initiating the proper troubleshooting paperwork. All safety systems functioned as designated and the unit was properly recovered without incident. Corrective Actions include disciplinary action against the C$i and counseling all individualt involved. There were two similar previous occurrences reported in LER's 454-05-34 and 85-97.
(0512R/0059R)
o ,
LICENitt EVENT REPORT (Ltki TEXT CONTINUATION Fe.1n Rev 21 I FACILITY NAME (1) DOCKET NUSER (2) _ LtR NLNelR f 61 Page (31 ,
/// Sequential
. Year // Revision
/// Nua6er j//j/
/
f Number _ ,
1 3rren. .Un1 L 1 ILilj 01010 141 $14 s17 - 01014 - 0 11 QLL E_ JLo '
T[XT [nergy Industry Identification System (Il!$) codes are identified in the text as (XX)
I A. PLANT CONDITIONS PRIOR.10 EVERI:
]
Unit 1 was in Mode $ (Cold shutdown) in preparation for refueling. RC$ (AB) was less than 200*f and de-pressurised. The $teamline Low Pressure Safety injection ($1)(BA) signal was blocked and the Pressuriser low Pressure $1 signal was blocked. Train B of Solid State Protection System ($$PS) (JE) was out-of-service for maintenance. The Main Control Board Trip Status Light Board (T$LB) was dark and the $$PS Demultiplexer (DEMUX) feeding the TSLB was de-energized. ;
i B. DL1Cl LIE 11QN 0F EVENT:
1 On February 2$. 1987 the Instrument Maintenance (IM) Department was asked to aid the Operating Department in taking channel 3, of the Process Instrumentation and Control System (JL), cabinet IPA 03J.
out-of-service. This out-of-service wet needed to install a wiring modification under Modification
]
M6-1-Bd 0246. Operating personnel on shift requested that channel 3 not be taken out-of-service until -
indications on the T$LB had been restored so that possible trips from other channels could be identified, i With $$P$ Train B out-of-service the main control board DCMUX had been deenerglaed to remove the "f alse" Train B indications f rom the T$LB. It was determined that to restore the T$LB indications, the OEMUX had to be powered up and the comununication links between Train A and Train B had to be interrupted.
l In an attempt to accomplish this, three I.M. personnel, two foremen and one Control System Technician (C$f) 1 (All non-Itcensed), determined that two cables between Train A and Train B needed to be disconnected. This '
l discussion was taken to the Operating $hift personnel and concurrence was given to remove the cables.
Disconnecting these cables, however, did not allow the TSLB to operate as desired. At this time, the I.M.
personnel returned to the I.M. shop to consult wiring diagrams. While they were in the shop, another C$T ;
who is a system expert, reported for work and offered his assistance in solving the problem. Convinced 1 that the consnvnication links between Train A and Train B had been severed, the two 1.M. foremen and the "new" C$T returned to the Auxiliary Electric Room. In the course of troubleshooting, the three people i proceeded to the Train A (IPA 09J) logic test panel to determine if some mispositioned switch could be ,
causing the problem. No mispositioned switches were found. The cabinet, IPA 093 contains three General l Warning Ilghts which indicate if there is a problem with either of the two $$PS Trains. An inconsistency ;
in the status of these lights, prompted the CST to suspect a " light" problem. Knowing that repositioning any switch in the cabinet would cause a General Warning, the C$f, on an impulse, then reached up and )
without further discussion repositioned the MEMORY $ witch. The repositioning of this switch unblocked the entsting $teamline ($8] Low Pressure $1 and the Pressurlier Low Pressure $1 signals, and initiated the l Sofety injection. '
l I l The Safety Injection occurred at 1614 on February 25. 1987. Water was injected into the Reactor vessel and Reactor Coolant pressure inceased to 80 psig. No over-pressure protection component was actuated nor I required. 1 Byron Emergency Operating Procedure BEP-0, " Reactor Trip or $afety Injection" was entered, and the Operators proceeded with the designated actions. All safety systems operated as designed. Following the steps. outlined in BEP-0. the $afety injection was reset and the two $1 signals were re-blocked within seven minutes from the inception of the event.
l t I (0512R/0059R)
FarnLRer l a.
_ LICLnLL iVLNT REPORT (LER) f tKT COM11M)6110N DOCKET NU$tR (2) Ltk NupetR (6) Pane (31 l tACitlTY NAMt (1)
Year /j/jj/ Sequential /jj f
// Revision
* /// Nysthgr uf . Hgight.t_
.htmJnit 1 015 l 9101(L1.Albl 4 8I7 -
_A l 0 1 4_ - O l1 QL1_QL _0L4 itX1 Energy Industry Identification System ([11$) codes are identified in the tent as (XX) x C. CMLDLLYCM1:
The root causes of the event were a tegnitive personnel error by the C$T (non licensed) and procedural personnel errors by the I.M. Foremen involved for not initiating the proper troubleshooting paperwork. Had the proper paperwork been initiated, to delineste the systematic documentation of actions tc troubleshoot this problem, the safety injection actuation would probably have been prevented.
Contributing factors to this event are:
The General Warning Ilghts in Cabinet IPA 09J were not working due to an unusual system status because the Reactor Trip breakers were racked out for another work activity.
The reduced risk of Reactor Trip /$af eguard actuations while the plant is in Cold $hutdown led to a slightly reduced level of alertness.
D. $ArtTY A%LY.$1$1 This event did not affect plant or public safety. All safety systems worked as designed, and all operator actions progressed as anticipated. In addition, the unit was in Cold Shutdown which is a non-applicable mode for Emergency Core Cooling System to be operable. This type of work activity would only be performed with the reactor in a shutdown mode.
E. CORELCILYL .*n110N$:
Appropriate disciplinary action was taken against the CST involved.
Other Instrument Maintenance personnel involved were counseled to re-emphastae the need for proper documentation and pre-planning when performing troubleshooting activities on plant equipment. Also discussed was the constant alertness needed when working on plant equipment, especially safety related equipment in all modes of operation.
This report was disseminated to Station Departments to be discussed with their respective personnel.
A long tonn solution to modify the $$P$ $ystem to be paced in TEST during an outage was investigated.
However, installing a modification of this type would not have prevented a similar event occurring in Modes 1 thru 4. or while in Mode $ with the $$PS cabinets in normal (as required to thange from Mode 5 to Mode 4). In addition, this type of event has not occurred since this event. On-Site Review 89-197 determined the Modification would not be beneficial. BVP 600-3 Placing Both Trains of $$PS In fest While in Mode 5 and 6, was in place for Refueling Outage BIR03. Action Item Record 45$.225-90 01200 will track the completion of the procedure for Unit Two. The procedure will then be available f or f uture use during outages as deemed necessary by the Operating Engineer.
(0512R/00$9R)
i i e . .
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- LittWi[[ ty[NT ktPORT (Ltti itKT CONTINUATION FernLRev 2.0 FACit!TY NAME (1) DOCKET NUSER (2) Ltk MuMata (6) Pane (3)
Year 5equential Revision j
' //{
ff
/// Number
//
,/{
f
// Nunea r _
l A ren. Unit 1 0 l 5 1 0 l 0 1 0 l 41 51 4 8I7 - 0l0l4 - 0 l1 01 4 0F OL4 ftKT Energy Industry identification System (E!!b) codes are identified in the text as (XXI
- f. RLtuRRINfi_EYLt0S SLAkCH AND ANALYSl$:
LLR.NuteLR 111LE 454-85-34 Manual Safety injection 454-85-97 Inadvertent $afety injection During Surveillance Test G. LQ!i'QNENT FAILURE DATA a) tnNUFACTURLR tiQtCNCLATURE tjQDEL. NUPSLR HrG PART NUtBER No components f ailed b) RLSulis or NPRDS STARCH:
Not Appitcable
-(0512R/0059R)
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