ML19347C826

From kanterella
Revision as of 21:11, 2 January 2020 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
AO 73-21:on 730908,during Plant shutdown,21 Hydraulic Shock & Sway Arrestors in Piping Sys in Drywell Found Failed. Caused by Loss of Hydraulic Fluid.Failed Snubbers Replaced W/Snubbers Rebuilt w/Bergen-Paterson Seal Kits
ML19347C826
Person / Time
Site: Oyster Creek
Issue date: 09/10/1973
From: Rone A
JERSEY CENTRAL POWER & LIGHT CO.
To:
References
AO-73-21, NUDOCS 8103040989
Download: ML19347C826 (2)


Text

.

  • Date: 9/10/73

. ,

Time: 3:00 a.m.

.- o .

.

/ ABNORMAL OCCURRENCE REPORT NO. 73-21

.

SUBJECT:

Failure of 21 Ilydraulic Shock and Sway Arrestors on piping systems in the Drywell, including units on both Core Spray and both

'

Isolation Condenser loops.

.

This event is considered to be an abnormal occurrence as defined in the Technical Specifications, paragraph 1.15.D. Notification of this event as required by the Technical Specifications, para-

. grap:16.6.2.a, was made to AEC Region I, Directorate of Regulatory

,

.

Operations, by telephone on Monday, September 10, 1973, at 12:45 p.m., and personally to Mr. E. Greeman on Monday, September 10, 1973.

.

SITUATION: The plant was shutdown on September 8,1973 for the purpose of inspecting the flydraulic Shock and Sway Arrestors located on

~ ~

piping systems throughout the Drfwell.

CAUSE: The snubbers were made inoperable due to a loss of hydraulic fluid.

REMEDIAL ACTION:

The failed liydraulit Shock and Sway Arrestors were replaced using

,

snubbers ' rebuilt with seal kits supplied by the Bergen Paterson Pipe Support Company. The new' seals are of'a different type, which according to Bergen Paterson, will provide a longer seal life.

.

p

-

.

.

O: 4

,

'

.- .

b~

AbnoEnal Occurrence .

September 10, 1973 - -

Report No. 73-21 ,

.

.

SAFETY SIGNIFICANCE:

<

The loss of snubber operability resulted in a reduction in the ability of the plant to safely survive a design bases earthquake.

The failures were such that they affected both Core Spray and

.

e both Emergency Condenser Systems, e

, o e

,

e a I

  • e e

0 e

e o e

%

.

e 0

.

.

6 -.

.

e

- - , e c ---