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05000250/FIN-2012002-012012Q1Turkey PointEmergency lighting to auxiliary feedwater area disabledThe inspectors identified a non-cited violation of the Units 3 and 4 operating licenses condition 3.D, Fire Protection, when the licensee failed to provide emergency lighting in the common auxiliary feedwater (AFW) cage and other areas. The electrical panel that supported normal lighting in the area was taken out of service for maintenance thus placing the emergency lights on battery power until the batteries depleted and the areas became dark, impacting the ability of operators to complete manual actions in the area, if needed. The licensee documented the issue in the corrective action program (CAP) as AR 1738082. The inspectors determined that the failure to provide emergency lighting in areas requiring local manual actions to safely mitigate certain fire events, and the associated access/egress routes, was a performance deficiency. The issue was more than minor because the objective of the Mitigating System Cornerstone to ensure the availability of fire protection equipment was affected when emergency lighting was not provided. The inspectors assessed the finding using NRC Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process, and assigned a low degradation rating because of the reasonable likelihood that plant operators would obtain alternate lighting and complete the prescribed manual actions. The finding screened as having very low safety significance. The cross cutting aspect of Work Control Planning, (H.3(a)), was assigned because the licensee did not use risk insights, did not assess environmental conditions (lighting) that may have impacted human performance, and did not plan for contingencies nor compensatory actions when the normal lighting was removed from service leading to loss of emergency lighting
05000250/FIN-2012002-022012Q1Turkey PointControl power cables repeatedly submerged in ground water, contrary to designA self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified when FPL did not maintain safety-related power cables in the environment for which they were designed and tested. Specifically, 125 volt DC control power cables feeding various safety related components and cables supporting other risk significant equipment had been repeatedly submerged in ground water for extended periods of time and this submergence had the potential to affect the ability of the cables to perform safety related functions. The issue was entered into the licensees CAP as AR 1717619. Although predominantly Unit 3 cables were submerged, because equipment is shared, both units were affected. Allowing water accumulation in the manhole(s) after disabling of the sump pump without compensatory measures to keep the safety related and risk significant cables dry resulted in subjecting the cables to an environment for which they were not designed, and was a performance deficiency. The finding was more than minor because it challenged the reliability of systems that respond to initiating events to prevent undesirable consequences, which is an attribute of the Mitigating Systems cornerstone. The inspectors evaluated the finding in accordance with IMC 0609.04, Phase 1, Initial Screening and Characterization of Findings. The finding was of very low safety significance because it did not represent an actual loss of safety function or contribute to external event core damage sequences. The finding had a cross-cutting aspect in Problem Identification and Resolution, Corrective Action Program, (P.1(c)), because FPL did not thoroughly evaluate submerged cables such that the resolutions addressed causes and extent of conditions, including evaluating for operability.
05000250/FIN-2012002-032012Q1Turkey PointLicensee-Identified ViolationThe following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for disposition as an NCV. 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design and be approved by the organization that performed the original design unless the applicant designates another responsible organization. FPL implements this requirement, in part, with procedure ENG-QI 1.7, Quality Instruction Design Input/Verification, which states engineering methods employed shall ensure that design inputs are correctly translated into new designs and design changes, and that design verification activities are correctly performed. Contrary to the above, engineering methods employed did not ensure that design inputs were correctly translated into the A auxiliary feedwater pump design change nor were design verification activities correctly performed on engineering design change package PCM 2005-029. As a result, on February 3, 2012, during a design review while developing a modification package for the A auxiliary feedwater pump, FPL identified a design calculation error in the 2005 modification package for the A auxiliary feed water pump. The pump modification raised the pump power requirements. The revised design horsepower output specified for the turbine accounted for the increased pump power demand, but failed to account for recirculation flow, turbine lube oil coolers flow, and instrument uncertainties. When identified by FPL, a prompt operability determination was completed. FPL determined that although there was a reduction in margin, the required auxiliary feed water turbine horsepower remained bounded by vendors design limits. This issue was entered into the corrective action program as AR 1731117. The finding was screened as having very low safety significance (Green) using NRC Inspection Manual Chapter 0609 SDP Phase 1 screening because the finding did not result in an inoperable auxiliary feedwater pump, did not affect functionality of the system, and the design basis continued to be met.
05000259/FIN-2012007-012012Q1Browns FerryFailure to Follow NRC Commitment Management ProcedureThe inspectors identified a Green finding (FIN) for the licensees failure to follow procedure NPG-SPP-03.3, Rev.001, NRC Commitment Management. Specifically, the procedure states, in part, that each responsible organization ensures commitment implementation/completion occurs as scheduled. Contrary to this requirement, the licensees commitment to verify the accuracy and adequacy of completed Inspection Procedure (IP) 95002 corrective actions had not been performed adequately. The licensee entered this issue into the corrective action program as PERs 510126 and 510161. The performance deficiency (PD) associated with this finding was the failure of licensee personnel to follow procedures regarding managing NRC commitments. The finding is greater than minor because, if left uncorrected, the finding would have the potential to lead to a more significant safety concern. Specifically, the failure to assess the adequacy of corrective actions can lead to problems not being properly corrected. Using Manual Chapter 0609.04, Phase 1 Initial Screening and Characterization of Findings, the finding was determined to have a very low safety significance (Green) because the finding did not result in a loss of system safety function, an actual loss of safety function of a single train for greater than its Technical Specification allowed outage time, or screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. This finding has a cross cutting aspect in the area of Human Performance because the licensee did not ensure supervisory and management oversight of work activities associated with the commitments made to the NRC, which resulted in the commitments not be tracked or monitored to ensure completion.
05000259/FIN-2012007-022012Q1Browns FerryFailure to Establish Adequate Compensatory Measures for Non- Conforming Fire BarriersThe inspectors identified a Green NCV of Browns Ferry Operating License Conditions 2.C(13), 2.C(14) and 2.C(7), for Units 1, 2, and 3, respectively, for the licensees failure to establish adequate compensatory measures for non-conforming fire barriers, in accordance with the approved fire protection program (FPP). Specifically, the licensee failed to establish continuous fire watches for non-conforming fire barriers in the Intake Pumping Station (IPS), after discovering that the barriers were not credited in the sites approved FPP. The licensee initiated PER 509589 to document this condition and enter it into the corrective action program. The licensee also established a continuous fire watch, in accordance with the FPR. The licensees failure to establish adequate compensatory measures for non-conforming fire barriers, as required by their approved fire protection program, is a PD. The finding is more than minor because it is associated with the Reactor Safety Mitigating Systems cornerstone attribute of protection against external factors (i.e., fire) and it affects the cornerstone objective of ensuring the reliability and capability of systems that respond to initiating events. Using the guidance of IMC 0609, Appendix F, Fire Protection Significance Determination Process, inspectors determined that the PD represented a finding of very low safety significance (Green). Inspectors determined that the cause of this finding has a cross-cutting aspect in the Corrective Action Program component of the Problem Identification and Resolution (PI&R) area, in that it was directly related to the licensee not thoroughly evaluating problems, such that the problem was properly classified and evaluated for operability
05000259/FIN-2012007-032012Q1Browns FerryFailure to Implement Appropriate Safe Shutdown InstructionsThe inspectors identified an NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to establish procedures appropriate to the circumstances for combating plant fires. Specifically, four new Safe Shutdown Instruction (SSI) were established which contained multiple procedural deficiencies. The licensee entered this finding into the corrective action program (PER 507721) and adequate Safe Shutdown Instructions were restored following procedure revisions. This finding is more than minor because it is associated with the procedure quality attribute of the Mitigating Systems cornerstone and it affected the cornerstone objective of protection against external events such as fire to prevent undesirable consequences. The finding was assigned a Low degradation rating and screened as very low safety significance (Green) in step 1.3.1 of IMC 0609 Appendix F, attachment 1, Application of Fire Protection SDP Phase 1 Worksheet. The team determined the cause of this finding was directly related to the crosscutting aspect of Work Coordination in the Work Control component of the Human Performance area because the licensee did not adequately incorporate actions to address the impact of the work on different job activities and the need for work groups to maintain interfaces with offsite organizations, and communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure plant and human performance. This contributed to the failure to identify deficiencies with the new SSI procedures prior to procedure implementation.
05000259/FIN-2012007-042012Q1Browns FerryFailure to Identify and Correct Deficiencies Associated with Safe Shutdown InstructionsThe inspectors identified a Green non-cited violation of 10 CFR 50 Appendix B, Criteria XVI, Corrective Action, for the licensees failure to assure conditions adverse to quality associated with the establishment and implementation of four new Safe Shutdown Instructions (SSI) were promptly identified and corrected. Specifically, the inspectors identified instances where previously identified issues with SSIs were either not entered into the corrective action program, corrective actions were not implemented, or the corrective actions were ineffective in addressing the identified issue. The licensee entered this finding into the corrective action program (PER 505551) and adequate procedural guidance was restored following licensee procedure revisions, training and demonstration to inspectors that operators had acquired an adequate level of proficiency to implement the new SSIs. This finding is more than minor because it is associated with the procedure quality attribute of the Mitigating Systems cornerstone and it affected the cornerstone objective of protection against external events, such as fire, to prevent undesirable consequences. The finding was assigned a Low degradation rating and screened as very low safety significance (Green) in step 1.3.1 of IMC 0609 Appendix F, attachment 1, Application of Fire Protection SDP Phase 1 Worksheet. This finding was directly related to the cross-cutting aspect of Thorough Evaluation of Identified Problems in the Corrective Action Program component of the Problem Identification and Resolution area because the licensee did not thoroughly evaluate identified problems such that the resolutions addresses the causes and extent of conditions of the issues.
05000259/FIN-2012007-062012Q1Browns FerryLicensee-Identified Violation10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings states, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. BFN procedure NPG-SPP-03.1.9, Rev. 0002, which is a subset of the sites corrective action procedure NPG-SPP-03.1, Rev. 0002, stated, in part, that a PER cannot be closed that has identified a degraded or non-conforming condition until the corrective actions to resolve the degraded or non-conforming condition are completed. Contrary to the above, the licensee closed two PERs (177130, 243955) that were generated during the sites NFPA 805 transition process, based on the implementation of compensatory measures. The permanent corrective action for these nonconformances (transition to NFPA 805) has not been completed. Using IMC 0609, Attachment 4, Phase 1, Initial Screening and Characterization of Findings, inspectors determined the violation was of very low safety significance (Green) because it was not a design or qualification deficiency, did not result in the loss of any system safety function and was not risk significant due to seismic, flooding or severe weather. This violation was documented in the licensees corrective action program as PER 503024.
05000259/FIN-2012007-072012Q1Browns FerryLicensee-Identified Violation10 CFR 50.72(b)(3)(ii)(B) states, in part, the licensee shall notify the NRC as soon as practical and in all cases within eight hours of the occurrence of any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety. Additionally, 10 CFR 50.73(a)(2)(ii)(B) requires licensees to submit a Licensee Event Report (LER) within 60 days after discovery of any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety. Contrary to the above, on February 5, 2011, the licensee identified that they had failed to recognize that six unanalyzed conditions discovered during the sites NFPA 805 transition process were reportable conditions (see Section 4OA5 of this report). Consequently, the licensee failed to make an eight-hour report as required by 10 CFR 50.72, and submit LERs within 60 days, as required by 10 CFR 50.73. This finding was considered as traditional enforcement because it had the potential for impacting the NRCs ability to perform its regulatory function. The NRC has characterized this violation as a Severity Level IV NCV in accordance with Section 6.9 of the NRC Enforcement Policy. This violation was documented in the licensees corrective action program as PERs 505749, 505750, 505751, and 505752. Additionally, the licensee made an eight-hour report, and at the time of the exit, planned to submit LERs for the unanalyzed conditions.
05000269/FIN-2013005-012013Q4OconeeFailure to properly maintain a fire barrier penetration sealAn NRC-identified non-cited violation (NCV) of 10 CFR 50.48(c) and National Fire Protection Association Standard 805 (NFPA 805), Section 3.11.4, was identified for the licensees failure to comply with the fire barrier penetration sealing and inspection requirements of the approved fire protection program (FPP). The annular space between the fire barrier opening and the 2 conduit was not properly sealed. The licensee entered the issue in their CAP as PIP O-13-09104, initiated a work order to repair the seal, and implemented an hourly fire watch as required by Oconee Selected Licensee Commitment (SLC) 16.9.5. The licensees failure to comply with the fire barrier penetration sealing and inspection requirements of the approved fire protection program was a performance deficiency. This performance deficiency was determined to be more than minor because it was associated with the Mitigating Systems cornerstone attribute of protection against external factors (i.e., fire) and adversely affected the cornerstone in that the fire barrier could not be relied upon to fully perform its function. The finding was screened using NRC IMC 0609, Appendix F, Fire Protection Significance Determination Process, and determined to be of very low safety significance (Green) because safety significant equipment was located a sufficient distance from the degraded penetration and the reactors ability to reach and maintain a safe shutdown condition was not impacted. The cause of this finding was determined to have a cross-cutting aspect of H.2(c) in the Resources component of the Human Performance area because the licensee did not ensure that complete, accurate, and up-to-date design documentation and procedures were available because adequate guidance was not included in the maintenance inspection procedures to allow personnel to identify a degraded condition.
05000269/FIN-2013005-022013Q4OconeeLicensee-Identified Violation10 CFR 50, App. B, Criterion XVI, required in part that conditions adverse to quality, such as non-conformances, are promptly identified and corrected. NSD-203, Operability/Functionality, required entry into the operability determination process (ODP) upon the discovery of circumstances that call into question the operability of any TS SSC including degraded/non-conforming conditions. NSD-203 also requires that actions to confirm if the SSC is degraded or non-conforming should be completed in a timeframe that is commensurate with its safety significance. Contrary to the above, a potential non-conforming condition was identified on December 30, 2012; however, the ODP was not entered until November 26, 2013, and corrective actions generated to correct the non-conforming condition. The finding was not greater than Green because it did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components and did not involve an actual reduction of hydrogen igniters in containment. This violation was entered into the CAP as PIP O-13-14547.
05000269/FIN-2013007-022013Q3OconeeFailure to Identify Ignition Sources and Targets During Initial Fire Scenario DevelopmentAn NRC-identified Apparent Violation (AV) was identified for the licensees failure to comply with the requirements of 10 CFR 50.48(c) and National Fire Protection Association Standard 805 (NFPA 805). The Oconee fire probabilistic risk assessment (Fire PRA) failed to address the risk contributions associated with all potentially risk significant fire scenarios. This finding does not represent an immediate safety concern because the licensee entered the issue in the corrective action program as Problem Investigation Program (PIP) O-13-08059 and PIP O-13-08061 and implemented fire watches as compensatory measures. Failure to comply with the requirements of 10 CFR 50.48(c) and NFPA 805 to address the risk contributions associated with all potentially risk significant fire scenarios was a performance deficiency. This performance deficiency was determined to be more than minor because it was associated with the Mitigating Systems cornerstone objective of protection against external events (i.e., fire), and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was determined to be potentially greater than Green. Therefore, further analysis is required to assess the significance of the finding. The cause of this finding was determined to have a crosscutting aspect of H.4(c) in the Work Practices component of the Human Performance area because the licensee did not ensure supervisory and management oversight of work activities, including contractors, such that nuclear safety was supported.
05000269/FIN-2013007-032013Q3OconeeFire Protection Program Change did not Meet Oconee License Condition Requirements for NFPA 805 Chapter ThreeAn NRC-identified Apparent Violation (AV) and associated traditional enforcement violation of Oconee Nuclear Station Renewed Facility Operating License Condition 3.D for Units 1, 2, and 3 was identified for the licensees failure to implement and maintain in effect all provisions of the approved fire protection program (FPP) that comply with 10 CFR 50.48(c), National Fire Protection Association Standard NFPA 805. The licensee made a change to the approved FPP involving control of combustible materials when the definition of transient fire loads was revised to exclude fire retardant scaffolding materials as transient fire loads, which would not require the licensee to track these items as combustible fire loads. The licensee also failed to submit the FPP change to the NRC for review and approval prior to implementation which impacted the ability of the NRC to perform its regulatory oversight function. The licensee entered this issue into the corrective action program as Problem Investigation Program O-13-08584. This finding did not represent an immediate safety concern because the licensee implemented compensatory measures in the form of combustible tracking impairments and fire watches in the high safety significant fire zones which contained the scaffolding. Failure to comply with Oconee Operating License Condition 3.D for a change to the approved FPP involving control of fire retardant scaffolding materials was a performance deficiency. This performance deficiency was determined to be more than minor because it was associated with the Mitigating Systems cornerstone attribute of protection against external events (i.e. fire), and it adversely affected the cornerstone objective in that the change to the FPP had the potential to adversely affect the ability to achieve and maintain safe and stable plant conditions due to the increased transient fire load in the affected fire zones. The finding was screened in accordance with NRC Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP), Attachment 4, Initial Characterization of Findings, which determined that an IMC 0609 Appendix F, Fire Protection Significance Determination Process, review was required as the finding affected fire prevention and administrative controls. The performance deficiency applied to most fire zones within the plant because the licensee stopped tracking the use of the fire retardant scaffolding materials. The team determined that a systematic plant-wide assessment effort was beyond the intended scope of the fire protection SDP. Therefore additional analysis is required to assess the significance of this finding. The cause of this finding was determined to have a cross-cutting aspect of H.1(b) in the Decision- Making component of the Human Performance area because the licensee used nonconservative assumptions in the decision making associated with this FPP change. Additionally, the licensees failure to submit the FPP change to the NRC was a traditional enforcement violation. The severity level of the traditional enforcement violation will be assigned based on the significance determination of the associated finding.
05000269/FIN-2013007-052013Q3OconeeNon-Compliance to License Condition Requiring Modifications to LPG Tank was not Identified During Transition to NFPA 805The team identified an unsecured 500 gallon (water capacity) LPG storage tank in the Transformer Yard adjacent to the CT1 transformer and the Unit 1 Turbine Building. The LPG storage tank sat on four concrete blocks and did not appear to have an excess flow control valve installed to prevent a large release of propane gas from a ruptured supply line to the Auxiliary Boiler. The licensee had previously identified these problems in PIPs O-06-01385, O-08-02163, O-11-10119 and O-13-03819. Initially, a work request was written to secure the tank but it was later closed without the work being performed. Subsequently, an engineering change request was initiated to address the issue but was never approved. In ONS License Amendment 64 for Unit Nos. 1 and 2 and License Amendment 61 for Unit 3, each units license was amended to state, in part, that The licensee is authorized to proceed and is required to complete modifications identified in Table 3.1 of the NRCs Fire Protection SER dated August 11, 1978. The modifications shall be completed on the schedule specified in Table 3.1. SER Section 3.1.7, states, Propane tanks located outside of the turbine building will be anchored and provided with excess flow valves. Table 3.1 states in part, The modification will be completed by the end of the first refuel outage for any unit which occurs after 6 months from the date of issuance of this Safety Evaluation. A letter from Duke Power Company to the NRC dated June 29, 1979 stated, in part that, The required modification had been completed. When questioned about the current configuration of the tank, the licensee stated that since the transition to their approved NPFA 805 FPP all prior FPP SERs and commitments have been superseded in their entirety by the revised license condition and that the tank was in compliance with the requirements of NFPA 805, Section 3.3.7.1 for the storage of flammable gases located outdoors. Offset distances from the tank to structures, systems or components were judged by the licensee to be sufficient to prevent adverse impact from fires or explosions. The team did not agree with this position and stated that the ONS April 14, 2010 License Amendment Request (LAR) did not address the tank or the non-compliance with the license amendment requirement of 1978. The NRC has requested additional information from the licensee to determine if a prior change to the license, made before the transition to NFPA 805, allowed the tank to remain in its current location without the originally required modifications; and, to determine if the tank had, at one time, been in compliance, but had been improperly relocated under a work order performed in 1986. This issue is unresolved pending NRC review of additional information requested to determine if the issue of concern constitutes a violation of NRC requirements. This issue is identified as URI 05000269, 270, 287/2013007-05, Non-Compliance to License Condition Requiring Modifications to LPG Tank was not Identified During Transition to NFPA 805.
05000269/FIN-2013501-012013Q3OconeeLicensee-Identified ViolationTechnical Specification 5.4.1(a), Procedures, required in part that written procedures be established, implemented, and maintained covering the applicable procedures in Regulatory Guide 1.33, Rev. 2, Appendix A, February 1978. Procedure OP/1/A/1102/008, Enclosure 4.35, On Line Valve Lineup for MOV Maintenance, Step 2.5, stated, in part, for the operator to cycle 1LP-22 (1B LPI BWST suction). Contrary to the above, on June 26, 2013, the licensee operator failed to follow written procedure when he closed 1LP-21 (1A LPI BWST suction) which isolated the operable LPI train from the BWST rendered Unit 1 LPI inoperable. The licensee restored the LPI A train to its proper alignment within thirteen minutes. The finding was determined not to be greater than Green because the loss of function of at least a single train did not exceed its TS allowed outage time. The licensee entered the issue into their CAP as PIP O-13-06879.
05000269/FIN-2013501-022013Q3OconeeLicensee-Identified ViolationTechnical Specification 5.4.1(a), Procedures, required in part that written procedures be established, implemented, and maintained covering the applicable procedures in Regulatory Guide 1.33, Rev. 2, Appendix A, February 1978. Procedure OP/0/A/1107/016, Enclosure 4.4, Removal and Restoration of 230KV Switchyard PCB, Step 2.2.4, stated, in part, Ensure locked closed PCB (27) Yellow (Red) Bus Side Disconnect. Contrary to the above, on October 22, 2012, the licensee failed to ensure PCB27 was locked closed. The licensee discovered and corrected this condition on April 24, 2013. The finding was determined to represent a loss of system and/or function which required a risk evaluation by a Senior Reactor Analyst (SRA). The SRA estimated the likelihood of faults that could lead to damage of the disconnect and multiplied these by the change in conditional core damage probability due to a loss of the transformer impacted. Dominant cutsets involved failure of one Keowee hydro unit in conjunction with LOOP sequences, operators failure to recover offsite power, or the Keowee faults within 4 hours, and failure of EFW. The risk impact was less than 1E-7 for the exposure period. In addition, the risk impact of seismic events was estimated not to be a major contributor to the change in risk. Because the risk impact was less than 1E-7, the finding was determined not to be greater than Green. Licensee personnel entered the issue into their corrective action program as PIP O-13-04503.
05000269/FIN-2014002-012014Q1OconeeInadequate Procedure to Ensure Adequate Piping Weld InspectionsA NRC-identified potentially Greater than Green Apparent Violation (AV) of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified when the licensee failed to ensure that procedure NDE-995, Ultrasonic Examination of Small Diameter Piping Butt Welds and Base Material for Thermal Fatigue Damage, was adequate to achieve acceptable coverage for the ultrasonic (UT) examination of weld 1-RC- 201-205. NDE-995 did not contain the necessary steps to achieve acceptable coverage for UT examinations when limitations were encountered. The licensee entered this finding into their corrective action program as PIP O-13-13168. The failure to ensure that station procedure NDE-995 was adequate to achieve acceptable coverage for the UT examination of weld 1-RC-201-205 was more than minor because it affected the Design Control attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective in that an undetected crack resulted in reactor coolant system pressure boundary leakage and a forced shutdown of Unit 1. The inspectors determined that detailed risk analysis was required. There was no immediate safety concern because the crack was repaired. The inspectors determined this finding has a cross-cutting aspect of H.7 in the Documentation component of the Human Performance area because the licensee did not create and maintain complete, accurate, and up-to-date documentation in procedure NDE-995 to ensure acceptable coverage for UT examinations.
05000269/FIN-2014005-012014Q4OconeeFailure to Update FSAR for Mode 4 LOCAAn NRC identified Severity Level IV violation of 10 CFR 50.71(e), "Maintenance of Records, Making of Reports," was identified for the licensees failure to update the final safety analysis report (FSAR) after the licensee adopted the improved technical specifications (ITS). The licensee adoption of ITS introduced the possibility of a Mode 4 loss of cooling accident (LOCA), which was an accident of a different type than previously evaluated in the FSAR. The licensee initiated PIP O-15-00260 in order to determine future corrective actions. Continued non-compliance does not present an immediate safety concern because the inspectors assessed this as a very low safety significant issue. The licensees failure to update the FSAR as required by 10 CFR 50.71(e) was a performance deficiency. The performance deficiency impacted the ability of the NRC to perform its regulatory oversight function and was dispositioned using traditional enforcement. Specifically, a failure to update the UFSAR challenges the regulatory process because it serves as a reference document used, in part, for recurring safety analyses, evaluating license amendment requests, and in preparation for and conduct of inspection activities. This violation was determined to be a Severity Level IV violation per Section 6.1.d.3 of the NRC Enforcement Policy, revised July 9, 2013, because the lack of up-to-date information has not resulted in any unacceptable change to the facility or procedures. The NRC Enforcement Policy also requires disposition of findings in the significance determination process, which determined the finding was not more than minor. Since this issue was dispositioned using traditional enforcement, there was no cross-cutting aspect associated with this violation.
05000269/FIN-2014005-022014Q4OconeeKeowee Hydro Unit 2 Inoperable for Longer Than Allowed TS Outage TimeA self-revealing Green NCV of Oconee Nuclear Station Technical Specification (TS) 3.8.1, AC Sources Operating, was identified for Keowee Hydro Unit 2 being inoperable for longer than allowed TS outage time. The licensee modified Keowee Hydro Unit 2 electrical protection circuitry with a faster response relay which was susceptible to an existing degraded system condition and ultimately caused Keowee Hydro Unit 2 to be inoperable. The licensee implemented engineering change (EC111358) which moved the 86E2X relay to another cabinet which was not susceptible to the vibration from the governor oil system. The licensee entered this issue in their corrective action program (CAP) as PIP-O-13-09152. The licensees failure to properly evaluate a modification to the electrical control circuit of the governor oil system, which resulted in Keowee Hydro Unit 2 being inoperable for longer than allowed TS outage time, was a performance deficiency. The issue is more than minor because it was associated with the equipment performance attribute of the mitigating system cornerstone and it adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the modification of the governor oil system, including the addition of the 86E2X governor TXS catastrophic relay, resulted in Keowee Hydro Unit 2 being inoperable for longer than allowed TS outage time. The finding was screened in accordance with NRC IMC 0609, Significance Determination Process (SDP), Attachment 4 and Attachment A and determined to require a detailed risk evaluation. A regional Senior Reactor Analyst performed a risk analysis of the performance deficiency which was found to be Green (CDF < 1E-6/year). The dominant accident sequence was a loss of offsite power where Keowee Unit 1 fails independently and unrelated to the performance deficiency and power is not successfully restored by Oconee operators. The influential factors in the Green result were the limited exposure time (19 days) and the ability to quickly restore power to the unit via the Lee Station gas turbines via the Fant Line. This finding was determined to have a cross-cutting aspect in the problem identification and resolution cross cutting area because the licensees organization failed to take effective corrective actions to address the issue in a timely manner commensurate with its safety significance. Specifically, the licensee failed to take effective corrective actions to address system interactions (i.e. high vibrations) which ultimately had an adverse effect upon modifications to the governor oil system of the Keowee Hydro Unit 2.
05000269/FIN-2014007-052014Q2OconeePotential Unanalyzed Condition Associated with Emergency Power SystemDuring a review of Oconees engineered safeguards protection system (ESPS) emergency power start control for the KHUs, the team noted that the 125Vdc control cables for train A of the ESPS and cables for supervisory control of both KHUs were recently modified. The team also noted that these 125Vdc control cables were installed in the same underground concrete raceway systems as the 4160Vac auxiliary power cables, 13.8kVac power cables for both emergency power and protected service water (PSW), and were in close proximity to these power cables. The team was concerned that a short circuit (which the licensee considered outside their design basis) in the 13.8kVac cables could induce voltage and currents in the dc control system which could potentially impact the functionality of the emergency power system which is required to mitigate certain design basis events. A similar issue exists in Manhole 6 of the PSW underground raceway where the new power supply to the PSW (adjacent to the 125Vdc control emergency power system) could short circuit or fault to ground. The licensee had not performed an analysis to determine the effects of such failures on the ability of the emergency power system to perform its safety function, thus the team questioned whether the plant was in an unanalyzed condition. Although the licensee did not agree that these failures were part of their licensing basis, they reported this as an unanalyzed condition to the NRC in accordance with 10 CFR 50.73(a)(2)(ii)(B) in Licensee Event Report 269/2014-01. In response to the teams concerns, the licensee entered this issue into their corrective action program, and performed immediate and prompt determinations of operability in which they concluded a reasonable expectation of operability exists. The team has requested assistance from subject matter experts in the Office of Nuclear Reactor Regulation via a Task Interface Agreement1 to review the emergency power system licensing basis to determine the acceptability of the licensees design. If the design is found to be noncompliant with the licensing basis, the licensee will be required to implement corrective actions to restore compliance. This issue is being tracked as URI 05000269/2014007-05, 05000270/2014007-05, 05000287/2014007-05, Potential Unanalyzed Condition Associated with Emergency Power System.
05000269/FIN-2014011-012014Q2OconeeFailure to Identify and Correct Weld Cracking in HPI NozzleA self-revealing potentially Greater than Green AV of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was identified when the licensee failed to identify a crack in a weld located in the Unit 1 High Pressure Injection (HPI) system. In 2004, a procedure was developed for augmented in-service inspection program ultrasonic examinations which effectively removed reasonable assurance that HPI nozzle component cracking would be identified and corrected. NDE-995, Ultrasonic Examination of Small Diameter Piping Butt Welds and Base Material for Thermal Fatigue Damage, did not contain the necessary steps to achieve acceptable coverage for UT examinations when limitations were encountered. The inspectors determined that the failure to ensure that station procedure NDE-995 was adequate to identify and correct cracking in weld 1-RC-201-105 was a performance deficiency. The inspectors determined that the performance deficiency was more than minor because it affected the Design Control attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective in that an unidentified crack resulted in reactor coolant system pressure boundary leakage and a forced shutdown of Unit 1. The finding was determined to require a detailed risk analysis because the condition could have resulted in a leak which exceeded the reactor coolant system leak rate for a small-break loss of coolant accident. There was no immediate safety concern because the crack was repaired. The inspectors determined this finding has a cross-cutting aspect of H.7 in the Documentation component of the Human Performance area because the licensee did not create and maintain complete, accurate, and up-to-date documentation in procedure NDE-995 to ensure acceptable coverage for UT examinations.
05000269/FIN-2015002-012015Q2OconeeInadequate Design Inputs for PSW Testing and Engineering EvaluationsThe NRC identified a finding for the licensees failure to verify the adequacy of design inputs used in protected service water (PSW) testing and engineering evaluations to validate that the PSW system could perform its design function with respect to Milestone 4 of order EA-13-010, in accordance with the Duke Energy Carolinas Topical Report, Quality Assurance Program. The licensee entered this issue into their corrective action program as problem investigation program reports (PIPs) O-15-03630, O-15-03527, O-15-03529, O-15- 03631, O-15-03530, NCR 01930521, NCR 01929161, and PIP 0-15-4544. The performance deficiency was more than minor because it was associated with the design control attribute and adversely affected the mitigating systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the errors identified in the hydraulic flow modeling software, Calculation OSC-9595, Protected Service Water (PSW) Hydraulic Model, Rev. 6, and supporting documentation required significant revision and reanalysis in order to determine that the PSW system was capable of meeting its design flow requirements for short term secondary heat removal capability. The inspectors determined the finding to be of very low safety significance (Green) because the finding was a deficiency affecting the design or qualification of a mitigating structure, system, or component (SSC), and the SSC maintained its operability or functionality. The inspectors determined the finding was indicative of present licensee performance and was associated with the cross-cutting aspect of avoid complacency within the human performance area. Specifically, the licensee failed to utilize standard human error prevention tools to ensure critical reviews were performed for the PSW testing and engineering evaluations supporting the completion of Milestone 4 of order EA-13-010 dated July 1, 2013.
05000269/FIN-2015002-022015Q2OconeeInadequate Acceptance Criteria for PSW Pump Surveillance TestingThe NRC identified a finding for the licensees failure to ensure that appropriate acceptance criteria was used during testing to verify PSW primary pump functionality in accordance with the Duke Energy Carolinas Topical Report, Quality Assurance Program. The licensee entered this issue into their corrective action program as PIP O-15-03190. The performance deficiency was more than minor because if left uncorrected, the performance deficiency had the potential to lead to a more significant safety concern. Specifically, PSW pump surveillance PT/0/A/0500/001, Protected Service Water Primary and Booster Pump Test, Rev. 0, did not incorporate acceptance limits established by design documents, and as a result, the licensee could unknowingly consider the PSW primary pump functional beyond seven percent pump degradation. The inspectors determined the finding to be of very low safety significance (Green) because the finding was a deficiency affecting the design or qualification of a mitigating SSC, and the SSC maintained its functionality. The inspectors determined the finding was indicative of present licensee performance and was associated with the cross-cutting aspect of avoid complacency within the human performance area. Specifically, the licensee failed to utilize standard human error prevention tools to ensure critical reviews were performed for PSW pump testing.
05000269/FIN-2015002-032015Q2OconeeFailure To Translate The Design Basis Into Procedures Used To Test The HPI Motor CoolersThe NRC identified a finding for the licensees failure to translate the design requirements of the high pressure injection (HPI) pump motor coolers into the procedure used to verify adequate flow from PSW, in accordance with the Duke Energy Carolinas Topical Report, Quality Assurance Program. Specifically, the licensee failed to incorporate the fouling factor assumed in Calculation OSC-2042, HPI Pump Motor Upper Bearing Cooling Report, Rev. 8, into Procedure TT/1/A/05000/008, High Pressure Injection Motor Cooler Flow Test from PSW, Rev. 2. The licensee entered this issue into their corrective action program as PIPs O-15-03608 and O-15-04544. The performance deficiency was more than minor because if left uncorrected, the performance deficiency had the potential to lead to a more significant safety concern. Specifically, the low pressure service water (LPSW) and PSW flow test acceptance criteria could have been met without ensuring adequate heat transfer could be provided from the HPI motor coolers to PSW. The inspectors determined the finding to be of very low safety significance (Green) because the finding was a deficiency affecting the design or qualification of a mitigating SSC, and the SSC maintained its operability or functionality. The inspectors determined the finding was indicative of present licensee performance and was associated with the cross-cutting aspect of teamwork within the human performance area. Specifically, the licensee failed to demonstrate a strong sense of collaboration and cooperation in connection with projects to ensure critical reviews were performed for the procedures used to test the HPI motor coolers.
05000269/FIN-2015004-012015Q4OconeeFailure to Adequately Maintain Controlled Procedures in Emergency Response FacilitiesThe inspectors identified a Green NCV of Title 10 of the Code of Federal Regulations (CFR), Part 50.47(b)(16), for the licensees failure to maintain the effectiveness of its emergency plan by ensuring procedures for use by the emergency response organization are maintained and up-to-date. Specifically, responsibilities for emergency plan implementing procedure distribution were not adequately maintained in multiple emergency response facilities because the procedures were not of the correct revision and may have been used had an emergency been declared. After the NRC inspectors informed the licensee of the discrepancy, the licensee entered the issue into their CAP as action request (AR) 01959550. The licensees immediate corrective actions were to perform an extent of condition review of all site EP procedures, including the corporate office and the other legacy Duke sites, and replace the procedures with the correct revision. The licensees failure to adequately maintain controlled procedures in the emergency response facilities was a performance deficiency. The inspectors determined that the performance deficiency was more than minor because the performance deficiency was associated with the procedure quality attribute of the emergency preparedness (EP) cornerstone and adversely affected the associated cornerstone objective. The finding was evaluated using the EP significance determination process and was identified as having very low safety significance because it was a failure to comply with NRC requirements and was not a loss of the planning standard function. The finding was associated with a cross-cutting aspect in the documentation component of the human performance area because the licensee failed to maintain complete, accurate, and up-to-date documentation.
05000269/FIN-2015004-032015Q4OconeeLicensee-Identified Violation10 CFR 50, Appendix B, Criteria III, Design Controls, requires in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in 10 CFR 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures and instructions. Contrary to the above, since May 11, 1992, the licensee failed to ensure that applicable regulatory requirements and design basis were correctly translated into specifications, drawings, procedures and instructions for the SSF. Specifically, the licensees initial analytical assumptions were inadequate to demonstrate that the SSF could meet design requirements under all required operating conditions. Additionally, on multiple occasions the licensee failed to properly evaluate emergent issues and design changes to ensure the SSF continued to meet design requirements under all required operating conditions. The performance deficiency was more than minor because it was associated with the equipment performance and protection against external factors attributes of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. An NRC Region II senior reactor analyst evaluated both internal events and external events (e.g. fire, turbine building flooding, tornado) and determined the risk significance was very low (Green). The dominant contributors to the low risk result were: 1) the limited exposure time per year that an individual Oconee unit would spend in the vulnerable time-window immediately following shutdown, and 2) the low frequency of the external events that would demand the SSF. The licensee entered this condition into their CAP as NCR 01905088 and NCR 01905183.
05000269/FIN-2016002-022016Q2OconeeFailure to Properly Control Transient Combustible Materials in the Oconee Main Control RoomsAn NRC-identified Green non-cited violation (NCV) of Oconee Nuclear Station Units 1, 2, and 3 Renewed Facility Operating License Condition 3.D, Fire Protection, was identified for the licensees failure to adequately implement the requirements of the transient combustible material program. Specifically, the licensee failed to control the storage of transient combustible material in the Oconee main control rooms with the proper evaluation in accordance with procedure AD-EG-ALL-1520, Transient Combustible Control, Attachment 3, Allowed Combustible Materials in Level B and Level C Areas. The licensee removed the stored items from each of the main control rooms and entered this issue into their corrective program as nuclear condition reports (NCRs) 02012091, 02012290, and 02013990. The licensees failure to control the storage of transient combustible material in the Oconee main control rooms with the proper evaluation in accordance with procedure AD-EG-ALL-1520 was a performance deficiency. The performance deficiency was more than minor because it was associated with the protection against external factors attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, uncontrolled transient combustibles challenge the habitability requirements of the main control room in the event of a fire and the ability of licensed operators to respond to events using the systems designed to prevent undesirable consequences. The finding was screened in accordance with IMC 0609, Significance Determination Process, Attachment 4, Initial Characterization of Findings and IMC 0609 Appendix F, Fire Protection Significance Determination Process Task 1.3.1, and determined to be of very low safety significance (Green) because the finding did not prevent the reactor from reaching and maintaining a safe shutdown condition. The finding was determined to have a cross-cutting aspect of procedure adherence in the human performance cross-cutting area because the licensee failed to implement the requirements of station procedure AD-EG-ALL-1520, Transient Combustible Control.
05000269/FIN-2016003-012016Q3OconeeFailure to Translate Design Requirements to Prevent the Effects of WaterhammerThe NRC identified a finding for the licensees failure to translate the limiting flow rate design requirement into station procedures used to start and operate the alternate reactor building cooling (RBC) system, in accordance with the Duke Energy Carolinas Topical Report, Quality Assurance Plan (QAP). Specifically, the licensee failed to translate the limiting flow rate of 170 gallons per minute (gpm) into Procedure AP/0/A/1700/051, Alternate Reactor Building Cooling, Revision (Rev.) 2, to ensure prevention of waterhammer on the A reactor building cooling unit (RBCU) or connecting low pressure service water (LPSW) lines when starting the RBCU Hale pump. The licensee entered this issue into their corrective action program as Action Request (AR) 02049903 and revised Procedure AP/0/A/1700/051 to limit the RBCU Hale pump discharge flow to each affected unit to an initial fill rate of 120 gpm or less. The performance deficiency was determined to be more than minor because it adversely affected the protection against external factors attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, opening the RBCU Hale pump discharge valve four turns, as specified in the procedure, would have resulted in filling the alternate RBC system at approximately 600-700 gpm and exceeding the design flow rate of 170 gpm established to prevent equipment and piping damage as a result of waterhammer. This provided a reasonable doubt that the alternate RBC system had the capability to reliably perform its intended safety function and, in turn, that the protected service water (PSW) system had the capability to meet its 30-day mission time during a turbine building fire that resulted in a loss of offsite power. The finding was determined to be of very low safety significance (Green) because the finding would not have resulted in a fire that caused secondary fires outside of the originating fire area due to circuit issues and did not affect the ability to reach and maintain a stable plant condition within the first 24-hours of a fire event. The inspectors determined the finding was indicative of present licensee performance and was associated with the cross-cutting aspect of design margin, in the area of human performance. Specifically, the licensee failed to operate and maintain the alternate RBC system equipment within design margins when they did not translate design requirements from Engineering Change (EC) 110008 and Calculation OSC-8107 into station procedures.
05000269/FIN-2016004-012016Q4OconeeFailure to Perform Appropriate Evaluation of Motor Operated Valve Actuator Output CapabilityGreen. The NRC identified a non-cited violation (NCV) of Title 10 Code of Federal Regulations (10 CFR) 50, Appendix B, Criterion III, Design Control, for the licensees failure to correctly determine the bounding degraded voltage to be assumed in the determination of motor operated valve (MOV) actuator output capability. Specifically, the licensee did not use appropriate transient voltages as input into the evaluation of the capability of the MOVs that are required to reposition in response to an accident signal. In response, the licensee entered the issue into their corrective action program as nuclear condition report (NCR) 2056895 and planned to formally revise their calculations to reflect the current plant configuration. This performance deficiency was more than minor because it was associated with the design control attribute of the mitigating systems cornerstone, and adversely impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, Oconees programmatic failure to use bounding terminal voltage values in the evaluation of their automatically actuated, safety-related MOVs did not ensure they would be capable of mitigating accidents when powered from sources other than the 230kV switchyard, thus resulting in doubt on their capability to perform their intended safety function. The finding was determined to be of very low safety significance (Green) because the finding was a deficiency affecting the design or qualification of a mitigating structure, system, or component (SSC), and the SSC maintained its operability or functionality. No cross-cutting aspect was assigned because the inspectors determined that the finding was not indicative of current licensee performance, because the most recent transient analysis that was performed for the sources other than the 230kV switchyard was performed in 2012.
05000269/FIN-2016004-022016Q4OconeeInappropriate Voltage Band in Lee Combustion Turbine Unit Operating ProcedureGreen. The NRC identified a NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to identify appropriate procedural updates that were needed to ensure the Lee combustion turbine (LCT) procedures were appropriate for the circumstances and maintained current. Specifically, the licensee did not include appropriate operational limitations in procedures associated with the LCTs. In response, the licensee generated NCR 2058763, verified the LCT automatic voltage regulator setpoint was, and had been, 13.8kV, and generated a corrective action to revise the affected procedures limits to 13.78kV, a value bounded by station analyses. This performance deficiency was more than minor because it was associated with the procedure quality attribute of the mitigating systems cornerstone, and adversely impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, Oconees failure to limit the operating voltage band of the LCTs to an amount that was demonstrated as acceptable by analysis resulted in doubt on their capability to provide power to safety-related equipment during an accident. The finding was determined to be of very low safety significance (Green) because the finding was a deficiency affecting the design or qualification of a mitigating SSC, and the SSC maintained its operability or functionality. No cross-cutting aspect was assigned because the inspectors determined that the finding was not indicative of current licensee performance, because the update to the procedures occurred in January and October 2007, after replacement of the LCTs.
05000269/FIN-2016007-012016Q1OconeePressure Boundary of Motor Operated Valves Could be Breached Due to Fire- Induced Hot ShortAn unresolved item was identified regarding the licensees evaluation of certain motor operated valves (MOVs) in the NSCA. Specifically, based on the conclusions in the licensees NSCA, as well as subsequent evaluations, MOVs that are subject to a hot short that bypasses the torque or limit switch could result in damage to the valve that causes an unmitigated loss of reactor coolant system (RCS) inventory due to leakage through the damaged valves pressure boundary or the valves associated sealing components. Information Notice 92-18, Potential for Loss of Remote Shutdown Capability During a Control Room Fire, stated that fire damage could cause an electrical hot short that bypasses thermal overload protection for MOVs, and that this hot short could result in damage to the valve. As a part of the licensees transition to NFPA 805, the licensee identified a number of MOVs that could be susceptible to IN 92-18 type damage. These valves were classified as non-compliant components or variances from deterministic requirements (VFDRs). The subsequent evaluation of these valves by the licensees Fire PRA group determined that these VFDRs met the acceptance criteria of the Fire Risk Evaluation, as documented in OSC-9314, as being acceptable "as-is" and that no further action was required. These VFDRs and their FPRA dispositions were communicated to the NRC in the April 2010 Oconee NFPA 805 license amendment request (LAR). Subsequent to NRCs issuance of the SER, Oconee Valve Engineering determined that, due to the size of the installed motor/gearbox, 10 MOVs could potentially suffer IN 92-18 damage to the extent that the integrity of the valve body or bonnet could be compromised. Loss of valve integrity of the valve pressure boundary was not an assumption used in the FPRA evaluation. The licensee documented this condition in AR 01906086. After further evaluation, the licensee documented in AR 01999309 that 9 of the original 10 valves identified could potentially suffer IN 92-18 damage to the extent that the integrity of the valve body or bonnet could be compromised. For the 9 affected valves, the licensee has undertaken additional evaluations to determine whether some portion of the valve would fail before the valves pressure boundary is compromised, or that any possible leakage that may result can be bounded by the credited RCS make-up sourcein this case, the reactor coolant make-up pump. Inspectors determined that no immediate safety concern existed with this item because the licensee had implemented compensatory measures in accordance with the sites approved FPP. This item is unresolved pending inspector receipt and review of the licensees evaluation.
05000269/FIN-2016008-012015Q4OconeePotential lack of adequacy of the licensees maintenance program to detect substantial degradation of cables and their connections used on Oconee large oil filled stationary transformersAn URI was identified to determine if a performance deficiency exists regarding the adequacy of the licensees maintenance program to detect substantial degradation of cables and their connections used on the stations large oil filled stationary transformers. Description The inspectors developed an issue of concern related to the adequacy of the licensees maintenance program to detect substantial degradation of cables and their connections used on the stations large oil filled stationary transformers. The inspectors noted that all inspections required by the licensees surveillance and preventative maintenance programs used unaided visual inspections of bushings, surge arrestors, cable connections, T-connections, and cables on the stations large oil filled stationary transformers. The inspectors noted that the licensees metallurgical report associated with the failed power cable from the Unit 3 startup transformer identified degradation which likely occurred over a lengthy period of time. The inspectors determined that the following inspection activities should be pursued to determine if a performance deficiency exists: Review of the licensees completed cause determination Review of any additional testing and metallurgical reports Review of any license event report submitted by the licensee Review of requirements associated with emergency AC power paths and associated transformers This issue is identified as URI 05000269, 287/2016008-01, Potential lack of adequacy of the licensees maintenance program to detect substantial degradation of cables and their connections used on Oconee large oil filled stationary transformers.
05000269/FIN-2017001-012017Q1OconeeFailure to Comply with 10 CFR 55.49Green: A Green NRC-identified non-cited violation (NCV) of 10 CFR 55.49, Integrity of Examinations and Tests, was identified because the licensee engaged in an activity that compromised the integrity of examinations. Specifically, the licensee failed to ensure that current week simulator scenarios could not be predicted based on the previous weeks simulator scenarios during the annual operating exams required by 10 CFR 55.59, Requalification. While inspecting the annual operating examination schedules for the required simulator examinations for 2016 and 2017, the inspectors identified that one of the two scenarios that were administered during a single week of the annual exam cycle could be predicted for administration the following week. The licensee did not implement any immediate corrective actions because the exams were completed and there was no evidence of compromise. The licensee documented the issue in nuclear condition report (NCR) 2114313. This performance deficiency was more than minor because it was associated with the human performance attribute of the mitigating systems cornerstone, and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, using predictable exam development and administration techniques adversely affected the integrity of the administration of the operating exams, which test licensed operator performance in order to ensure timely and correct mitigating actions during an event. Using the Licensed Operator Requalification Significance Determination Process, this finding was determined to be of very low safety significance (Green) because no known compromise of the examinations occurred. The inspectors determined the finding had a cross-cutting aspect of resources in the cross-cutting area of human performance because the licensee failed to ensure that adequate training procedures were available to meet industry standards and ensure that the potential for the compromise of regulatory examinations did not exist. (H.1)
05000269/FIN-2017001-022017Q1OconeeLicensee-Identified ViolationTechnical Specification 3.3.8, PAM Instrumentation, requires CHRRMs, RIA-57 and RIA-58, to be operable in Modes 1, 2, or 3. Contrary to the above, from 1998 to October 2016, the licensee failed to maintain operability of the CHRRMs for all three units when they failed to provide reasonable assurance that the CHRRMs would provide accurate measurement of containment radiation levels during a HELB event in the east penetration room of the affected unit(s). The CHRRMs are utilized in the Oconee site emergency plan and implementing procedures to support assessment of the severity of an accident. The performance deficiency was determined to be more than minor because it was associated with the facilities and equipment attribute of the emergency preparedness cornerstone and adversely affected the cornerstone objective to ensure the licensees capability to implement adequate measures to protect the health and safety of the public in the event of a radiological emergency. The inspectors used IMC 0609, Att. 4, Initial Characterization of Findings, issued June 19, 2012, and IMC 0609, Appendix B, Emergency Preparedness Significance Determination Process, issued September 22, 2015, and determined the finding was of very low safety significance (Green) because no planning standard function failure occurred due to the availability of other parameters that could be used to validate the indications from the CHRRMs. The licensee has entered this issue into their corrective action program as NCRs 02069527 and 02077587.
05000269/FIN-2017001-032017Q1OconeeLicensee-Identified ViolationOconee Nuclear Station Technical Specification 3.0.4 requires that when a limiting condition of operation is not met, entry into a mode or other specified condition in the applicability shall not be made except when the associated actions to be entered permit continued operation in the mode or other specified condition in the applicability for an unlimited period of time. Oconee Nuclear Station Technical Specification 3.3.7, Engineered Safeguards Protective System (ESPS) Automatic Actuation Output Logic Channels, requires eight ESPS automatic actuation output logic channels to be operable in Modes 1 and 2 and Modes 3 and 4 when associated ES equipment is required to the operable. Contrary to the above, Oconee Nuclear Station Unit 1 entered Mode 4 on November 24, 2016 with ES protective system voters 1 and 2 in an abnormal configuration (bypassed) for the plant mode of operation. Operations shift personnel discovered this abnormal configuration on November 25, 2016 and restored voters 1 and 2 to an operate condition which met Technical Specification 3.3.7. This failure to maintain ESPS channels in the correct mode of operation for the required mode of applicability was a performance deficiency and was determined to be more than minor. The issue is more than minor because it was associated with the configuration control attribute of the mitigating system cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the issue challenged the configuration control attribute of ensuring operating equipment was available to respond to initiating events. The inspectors used IMC 0609, Att. 4, Initial Characterization of Findings, issued October 07, 2016, and IMC 0609, Appendix A, Significance Determination Process for Findings at Power, issued June 19, 2012, and determined the finding was of very low safety significance (Green) because the finding did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time or two separate safety systems out-of-service for greater than its technical specification allowed outage time. The licensee has entered this issue into their corrective action program as NCR 02081523.
05000269/FIN-2017004-012017Q4OconeeFailure to Identify Sensitive Equipment During Modification Results in Loss of Safety FunctionA self-revealing Green non-cited violation (NCV) of Oconee Nuclear Station Technical Specification (TS), Section 5.4, Procedures, was identified for the licensees failure to identify sensitive equipment in a work area that warranted implementation of compensatory measures as required by station procedure AD-EG-ALL-1180, Engineering Change (EC) Walkdowns. During the design and planning phase of a station modification, the licensee failed to identify sensitive components located in the subject work area and subsequently failed to implement adequate protective measures as defined in station procedures to prevent plant impacts during modification installation. The licensee entered this issue into their corrective action program (CAP) as nuclear condition report (NCR)02131608 and implemented corrective actions to identify other positionable components required for emergency power source operability that would require the use of protective measures, as defined by AD-OP-ALL-0204, Plant Status Control, in order to prevent inadvertent operation. The licensee created a formal Engineering department communication which included lessons learned from the event and familiarization with the EC walkdown checklist. The signs on the governor actuator cabinets were also revised to emphasize the sensitive nature of the equipment. The licensees failure to properly identify sensitive equipment and implement compensatory measures to prevent plant impacts as required by station procedure AD-EG-ALL-1180 was a performance deficiency. The performance deficiency was determined to be more than minor because it was associated with the human performance attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in the loss of the emergency AC power path function for 11 hours and 31 minutes. The finding was assessed using IMC 0609, Attachment 4 and IMC 0609, Appendix A. Inspection Manual Chapter 0609, Appendix A required a detailed risk evaluation because the finding represented a loss of system and/or function. A regional senior reactor analyst (SRA) performed the detailed risk evaluation using SAPHIRE Version 8.1.6 and a modified Version 8.50 of the SPAR Model for Oconee. The SRA developed two change sets to model the total exposure time for the finding. The first simulated a common cause failure of both Keowee units with an exposure time of 7 hours. The second simulated the failure of both Keowee units while the standby buses were energized by the Lee Station for 5 hours. The result was less than 1E-6 for each Oconee unit, which would be a finding of very low significance (Green). The inspectors utilized IMC 0310, Aspects Within the Cross-Cutting Areas, dated December 4, 2014, and determined the finding had a cross-cutting aspect of work management in the area of human performance, in that the organization failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process failed to include the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. (H.5)
05000269/FIN-2018002-022018Q2OconeeFailure to Coordinate a No-later-than Arrival Time for the Shipment of a Category 2 Quantity of Radioactive MaterialThe inspectors identified aSeverity Level IV NCV of 10 CFR 37.75(b) when the licensee failed to coordinate a no-later-than arrival time for a Category 2 shipment of radioactive material. Specifically, the licensee failed to recognize that a package of primary resin contained a Category 2 quantity of Cobalt-60 prior to shipment, and therefore failed to arrange a no-later-than arrival time with the receiving licensee.
05000270/FIN-2014004-012014Q3OconeeReview of FOD 50.59 EvaluationAn Unresolved Item (URI) was identified to review the licensees re-evaluation of the initial 50.59 evaluation for the Flood Outlet Device to determine if the performance deficiency is more than minor. In November 1998, the licensee identified that a HELB induced flood in the EPR could spread to other components in the Auxiliary Building (AB) and affect the ability of various safe shut down (S/D) equipment to perform its safety-related function as described in the Final Safety Analysis Report (FSAR). The licensee developed a modification package in April 2006, to install a Flood Outlet Device (FOD) which required a 50.59 evaluation. An initial 50.59 screening determined that the FOD modification did not require a detailed 50.59 evaluation. On August 21, 2006, the licensee conducted a review of the 50.59 screening and, as documented in PIP O-06-05726, ...were not able to conclusively determine if the correct conclusion had been made. A corrective action was identified in the corrective action document to perform an in-depth 50.59 screening and evaluation. The inspectors determined, through personnel interviews and review of documentation, that the licensee failed to perform this corrective action for a condition adverse to quality. The licensee is performing a revised 50.59 screening. The inspectors will evaluate the results of the screening to determine if a performance deficiency exists. This is identified as URI 05000270/2014004-01, Review of FOD 50.59 Evaluation.
05000270/FIN-2015004-022015Q4OconeeFailure to Accomplish Activities Affecting Quality in Accordance With Station Instructions and Procedures Which Resulted in a Valid AFIS ActuationA Green self-revealing non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified for the failure to accomplish activities affecting quality in accordance with instructions and procedures established by the licensee. Specifically, the failure of station personnel to correctly close the Weidmuiller links on the feedwater control valves, in accordance with procedure PT/2/A/0152/020, AFIS Circuitry Test, Enclosure 13.2, AFIS Circuitry Verification and Valves Stroked on Refueling Frequency During FDW System Shutdown, Steps 1.22 and 1.23, caused feedwater flow oscillations. The feedwater flow oscillations resulted in a valid automatic feedwater isolation signal (AFIS) initialization. The licensee entered this issue into their corrective action program (CAP) as nuclear condition report (NCR) 01939072. The licensee verified all AFIS links on all units were closed and modified station procedures to include additional detail on ensuring that the links are fully closed. The licensees failure to follow procedure PT/2/A/0152/020, AFIS Circuitry Test, during the last AFIS circuitry testing on November 17, 2013 was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance and human performance attributes of the mitigating systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the failure of station personnel to correctly close the Weidmuiller links on the feedwater control valves caused feedwater flow oscillations resulting in a valid AFIS initialization. Using NRC IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 2 Mitigating System Screening Questions Part B, dated July 1, 2012, the inspectors determined the finding to be of very low safety significance (Green) since the finding did not result in the loss of equipment specifically designed to mitigate a loss of feedwater flow. Specifically, the AFIS initiation was a valid actuation and as such, there was no loss of safety function. The finding had a cross-cutting aspect of procedure adherence in the area of human performance, because the licensee did not adequately follow processes, procedures, and work instructions.
05000287/FIN-2016002-012016Q2OconeeFailure to Perform ISI General Visual Examinations of Containment Moisture BarrierAn NRC-identified Green NCV of 10 CFR Part 50.55a, Codes and Standards, was identified for the licensees failure to conduct 100 percent general visual examinations of the moisture barriers to the containment liner in accordance with Subsection IWE of American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code, Section XI. Specifically, the licensee failed to conduct visual examinations of the sealant applied to interior expansion joint locations in containment. In response, the licensee repaired the identified moisture barriers and confirmed the operability of the containment liner with the satisfactory results of the containment integrated leak rate test. The licensee entered this issue into their corrective action program as NCR 02027086. The failure to conduct a general visual examination of 100 percent of the moisture barriers intended to prevent intrusion of moisture against inaccessible areas of the containment liner was a performance deficiency. The performance deficiency was determined to be more than minor because it was associated with the design control attribute of the barrier integrity cornerstone and adversely affected the cornerstone objective of providing reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, the inspectors determined that this finding was of more than minor significance because the failure to conduct required visual examinations and identify the degraded moisture barriers, which could allow the intrusion of water, if left uncorrected, had the potential to lead to a more significant concern. The inspectors used IMC-0609, Appendix A, The Significance Determination Process (SDP) For Findings At-Power, Exhibit 3 Barrier Integrity Screening Questions, and determined that the finding was of very low safety significance (Green) because it did not represent an actual open pathway in the physical integrity of the reactor containment and did not involve an actual reduction in function of hydrogen igniters in the reactor containment. The inspectors determined no cross-cutting aspect was associated with this finding because the finding was not reflective of present licensee performance.
05000287/FIN-2016002-032016Q2OconeeDegraded power cables result in inoperable startup transformer and loss of Unit 3 safety functionA self-revealing Green violation of Oconee Technical Specification 5.4, Procedures, was identified for the licensees failure to establish adequate procedures to detect degradation of the startup transformer power cables. Station procedure IP/0/A/2400/002, Substation Insulators, Lighting Arrestors, CCVT, Transformer Drop Down Line, Bus Inspection and Maintenance, lacked sufficient detail for maintenance personnel to properly inspect power cables for cracks and fraying. This allowed undetected degradation of the Oconee startup transformer power cables to develop causing the Unit 3 startup transformer to become inoperable. The licensee performed repair activities on the degraded power cables to remove areas where strands of the power cables were severed and re-established proper connections. Also, the licensee created work orders in their work management process to replace the drop down lines on the Unit 1 and Unit 3 startup transformers. The licensee entered this issue into their corrective program as NCR 01733811. The licensees failure to establish an adequate procedure to detect degradation of startup transformer power cables during periodic maintenance was a performance deficiency. The performance deficiency was determined to be more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, the power cable failure caused inoperability of the Unit 3 startup transformer. The finding was screened in accordance with IMC 0609, Significance Determination Process, Attachment 4 and Appendix A and determined to require a detailed risk evaluation. A senior reactor analyst performed a detailed risk evaluation of this condition and determined delta CDF was 3E-7 (Green). The finding was determined to have a cross-cutting aspect of evaluation in the problem identification and resolution cross-cutting area because the licensees corrective actions resulting from a degraded power cable in 2002 failed to incorporate sufficient detail into their procedures necessary to detect frayed cables.
05000287/FIN-2016002-042016Q2OconeeFailure to Make a Non-Emergency Eight Hour Notification of a Loss of Safety FunctionAn NRC-identified Severity Level IV NCV of 10 CFR 50.72(b)(3)(v) was identified for the licensees failure to make a required non-emergency eight hour notification for a loss of the emergency AC power path function. On December 7, 2015 Oconee Nuclear Station Unit 3 experienced a loss of the emergency AC power path function for approximately 21 minutes. The licensee entered this issue into their corrective action program as NCR 01981762 and will evaluate their internal reportability procedures regarding the time of discovery. The failure to make an eight hour non-emergency report for a loss of the emergency AC power path function per 10 CFR 50.72(b)(3)(v) was a performance deficiency. This performance deficiency impacted the ability of the NRC to perform its regulatory oversight function and was dispositioned using traditional enforcement. This violation was assessed using Section 2.2.4 of the NRCs Enforcement Policy, revised February 4, 2015. Using the example listed in Section 6.9.d.9, A licensee fails to make a report required by 10 CFR 50.72, the issue was determined to be a Severity Level IV violation. In accordance with IMC 0612, because this violation involved traditional enforcement and does not have an underlying technical violation that would be considered more than minor, a cross-cutting aspect was not assigned to this violation.
05000287/FIN-2016003-022016Q3OconeeLicensee-Identified ViolationTechnical Specification (TS) 5.4.1., Procedures, states, in part, written procedures shall be established, implemented, and maintained covering activities described in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Procedure MP/0/A/3009/017, Visual PM Inspection and Electrical Motor Tests is used by the licensee during maintenance of electric motors. Contrary to the above, on April 25, 2016, the licensee did not adequately implement maintenance procedure MP/0/A/3009/017. Specifically, the licensee incorrectly wired the 3C RBCU motor control center contactor leads during maintenance causing 3C RBCU fan to operate in the reverse direction. On June 16, 2016, during an engineer walkdown, the engineer noted anomalies in the RBCU inlet temperature readings. On June 28, 2016, while investigating the temperature readings the licensee discovered that the 3C RBCU fan was operating in the reverse direction and declared the 3C RBCU inoperable. The 3C RBCU was inoperable when the plant entered Mode 4 on May 14, 2016 until June 28, 2016 when the 3C RBCU was repaired (approximately 45 days). Technical Specification 3.6.5, Reactor Building Spray and Cooling Systems, requires all three trains of RBCU operable while in Modes 1, 2, 3, and 4. On May 14, 2016, Unit 3 was starting-up from the refueling outage and entered Modes 4 through 1 with one train of RBCU inoperable. This action of changing modes with the 3C RBCU inoperable is prohibited by TS 3.0.4. The licensee entered this condition into their corrective action program as NCR 02041501. The licensee also restored 3C RBCU operability, trained/counseled technicians, and incorporated a procedure change which will enhance configuration control for the lifted leads aspect in the maintenance procedure for this activity. This finding was assessed using IMC 0609, Phase 1 screening worksheet of Attachment 4, Appendix A, and Appendix H, and was determined to be of very low safety significance (Green).
05000287/FIN-2017004-022017Q4OconeeFailure to Properly Risk Screen Work Within Two Feet of a Single Point Vulnerability ComponentA self-revealing Green NCV of Oconee Nuclear Station TS, Section 5.4, Procedures, was identified for the licensees failure to identify and properly risk screen work within 2 feet of a single point vulnerability (SPV) component in accordance with procedure AD-OP-ALL-0201, Protected Equipment. Specifically, the transmission and Oconee organizations failed to recognize that planned maintenance on a breaker in the 525 kilovolt (kV) switchyard was within 2 feet of an SPV component and, as a result, appropriate planning and oversight were not in place to prevent a plant trip during maintenance activities. The licensee entered this issue into their CAP as NCR 02138958. Corrective actions included revisions to station and transmission procedures to ensure inclusion of appropriate SPV program information, addition of the SY special emphasis code to all switchyard type work which require coordination of transmission resources, and the addition of the T1 trip/transient risk special emphasis code to all breaker failure relays in the 230 kV and 525 kV switchyard cabinets containing SPV components.The licensees failure to identify and properly risk screen the planned maintenance on PCB-57 as work within 2 feet of an SPV component in accordance with AD-OP-ALL-0201 was a performance deficiency. The performance deficiency was determined to be more than minor because it was associated with the human performance attribute of the initiating events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, human errors led to a Unit 3 main generator lockout, which resulted in a reactor trip. The finding was assessed using IMC 0609, Attachment 4 and IMC 0609, Appendix A. The inspectors determined the finding was of very low safety significance (Green) because the finding did not represent a transient initiator that caused both a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition (i.e. loss of condenser, loss of feedwater). The inspectors utilized IMC 0310, Aspects Within the Cross-Cutting Areas, dated December 4, 2014, and determined the finding had a cross-cutting aspect of work management in the human performance area, because the organization failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process failed to include the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. (H.5)
05000287/FIN-2018002-012018Q2OconeeFailure to Perform ISI General Visual Examinations of Containment Moisture Barrier Associated with Containment Liner Leak Chase Test Connection PipingThe inspectors identified a Green NCV of 10 CFR Part 50.55a, Codes and Standards, involving the licensees failure to properly apply Subsection IWE, of ASME Section XI, for conducting general visual examinations of the leak chase test connection piping at the concrete floor interface which provides a moisture barrier to the containment liner seam welds.
05000302/FIN-2011002-012011Q1Crystal RiverOperating Crew Failures on the 2011 Annual Requalification Operating TestA self-revealing Green finding, associated with operating crew performance on the simulator during facility-administered requalification examination was identified. Two of the eight crews evaluated failed to pass their simulator examinations. As immediate corrective action, the failed operating crews were remediated (i.e., the operating crews were re-trained and successfully retested) prior to returning to shift. The licensee has entered this issue into the corrective action program as Nuclear Condition Report (NRC) 450196. The inspectors determined that the crew failures constituted a performance deficiency based on the fact that licensed operators are expected to operate the plant with acceptable standards of knowledge and abilities demonstrated through periodic testing as required by 10 CFR 55.59(a)(2). Two out of eight crews of licensed operators failed to demonstrate a satisfactory understanding of the required actions and mitigating strategies required to safely operate the facility under normal, abnormal, and emergency conditions. The finding is greater than minor because the performance deficiency potentially affects the Human Performance attribute of the Mitigating Systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the finding reflected the crews potential inability to take timely actions in response to actual abnormal and emergency conditions. The cause of this finding was directly related to the cross-cutting aspect of personnel training and qualifications in the Resources component of the Human Performance area, in that the licensee failed to ensure the adequacy of the training provided to operators to assure nuclear safety.
05000302/FIN-2011002-022011Q1Crystal RiverLicensee-Identified ViolationImproved Technical Specification (ITS) 3.4.9 states that two pressurizer code safety valves (PCSVs) shall be operable in Modes 1, 2 and 3. To be operable, the lift setpoints must be within +/- 2 percent of 2500 psig. Contrary to the above, on September 1, 2010 and on October 5, 2010, Progress Energy was notified that the as-found lift setpoints of PCSVs RCV-9 and RCV-8 were outside ITS setpoint limits, respectively. The as-found lift setpoint of RCV-9 was 5.32 percent above the lift setpoint and RCV-8 was 2.08 percent above the lift setpoint. The licensee identified a selected cause associated with the licensees failure to manage vendor quality. The performance deficiency, failure to provide proper relief valve specifications to the vendor, was determined to be greater than minor because if left uncorrected, the performance deficiency would have the potential to lead to a more significant safety concern regarding the integrity of the reactor coolant system (RCS) barrier during plant transients. Corrective actions planned or completed include: changing the as-left setpoint to +0/-1 percent of the nominal setpoint; installing PCSVs with +0/-1 percent of nominal setpoint prior to unit startup; creation of a test procedure for steam testing the PCSV to meet the licensees standards; and revision of specifications associated with PCSV repairs. As documented in Section 4OA3, the finding was determined to be of very low safety significance (Green) because there was no loss of safety function due to the lift setpoints being outside of the ITS limit. This issue was documented in the licensees corrective action program as NCR 426852.
05000302/FIN-2011003-012011Q2Crystal RiverLicensee-Identified Violation10 CFR 50 Appendix B, Criterion III, Design Control, requires, in part, that measures shall be established to assure that applicable regulatory requirements and design basis for those structures, systems, and components are correctly translated into specifications, drawings, procedures and instructions. Licensee corporate engineering procedures EGR-NGGC-0005, Engineering Change; and Administrative Corporate procedure ADM-NGGC-0116, Nuclear Planning, implement those requirements. Contrary to the above, the licensee failed to translate the design basis requirements of modifications MAR 86-09-15, Raw Water Joint Encapsulation Sleeve, and MAR 90-08-16, Circulating Water Joint Encapsulation Sleeve, into work orders or procedures to ensure continued maintenance of design basis requirements. As a result, the raw water and circulating water encapsulation sleeves were found to have a larger gap than allowed by design, and consequently would have caused a greater internal flood rate into the auxiliary building had the expansion joints failed. The performance deficiency of failing to maintain the gaps within the required tolerances on the raw water and circulating water encapsulation sleeves is more than minor because, if left uncorrected, would have the potential to lead to a more significant safety concern during a rupture of a raw water or circulating water expansion joint. The licensees corrective actions include revising maintenance procedures to add acceptance criteria for the encapsulation sleeve gaps. The finding was determined to be of very low safety significance (Green) because after performing additional engineering evaluations and calculations, it was concluded that the auxiliary building internal design basis flood requirements were not exceeded. This issue was documented in the licensees corrective action program as NCRs 456729, 457510, and 457181.
05000302/FIN-2011005-012011Q4Crystal RiverLicensee-Identified ViolationThe following violation of very low safety significance (Green) was identified by the licensee and was a violation of NRC requirements which met the criteria of the NRC Enforcement Policy for being dispositioned as a Non-Cited Violation: &#149; Improved Technical Specification 5.6.1.1a requires that written procedures recommended in Regulatory Guide (RG) 1.33, Revision 2, Appendix A, be established, implemented, and maintained. RG 1.33, Appendix A, includes general operating procedures for Refueling & Core Alterations in the list of recommended procedures. Plant Operating Manual FP-601A, Operation of the Main Fuel Handling Bridge FHCR-1, Section 3.2.22, requires, in part, that a refueling SRO be stationed during a core alteration. Contrary to this requirement, the licensee secured the refueling SRO during activities determined to be a core alteration for approximately seven-hours on May 24, 2011. The licensee entered this issue into their CAP as CR 467392. The significance of the finding was determined using Manual Chapter 0609, Significance Determination Process, Appendix G, Checklist 4 (PWR Refueling Operation, RCS level > 23 ft) and determined to be of very low safety significance (Green), because it did not cause the loss of mitigating capability of core heat removal, inventory control, power availability, containment control, or reactivity control. Additional information regarding this NCV is discussed in Section 4OA2 of this inspection report.
05000302/FIN-2012005-012012Q4Crystal RiverLicensee-Identified ViolationThe inspectors reviewed the reportability evaluations associated with the unsatisfactory penetrations. The inspectors questioned the adequacy of these evaluations in that they estimated that a significant level of water (approximately three to four feet) would accumulate in the turbine building during PMH conditions, but concluded that none of this flood water would pass through the set of fire doors from the turbine building to the auxiliary building. The subject fire doors are rated for 2 feet of water pressure. The reportability evaluations heavily relied upon actions taken in the licensees adverse weather procedure EM-220, Violent Weather, to sandbag the fire doors prior to hurricane conditions. The inspectors did not have confidence in the adequacy of sandbagging instructions in EM-220 or that the door could withstand three to four feet of turbine building flooding to preclude flooding in auxiliary building. As a result of the inspectors concerns, the licensee initiated CR 563931 to re-evaluate the expected flood levels in the turbine building during PMH conditions. The inspectors reviewed the completed evaluation and noted that more reasonable external flooding conditions were used and the evaluation took credit for other actions in the adverse weather procedure such as use of dewatering pumps. The inspectors also noted that the evaluation included the estimated flooding contribution from two additional unsatisfactory penetrations which were identified in August 2012 during the licensees Fukushima flooding walkdowns and documented in CRs 556385 and 557156. The inspectors concluded that, due to the location and condition of the two penetrations, their overall flooding contribution was negligible when compared to the overall flood level due to the 29 penetrations previously identified by the licensee. The new evaluation concluded that the resulting flood level through the 29 penetrations during PMH conditions would be 1.27 feet of water in the turbine building, which is within the rating of the fire doors. The inspectors concurred with the licensees conclusion that this flood level would not adversely impact the allowable flood limit in the auxiliary building. The inspectors verified that the licensee had performed an adequate extent of condition review to identify the unsatisfactory below grade penetrations and that appropriate actions were being taken to correct the issue. The inspectors verified that, as of the end of this inspection period, 19 of the 28 unsatisfactory penetrations had been repaired. The remaining were scheduled for repair.