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 Entered dateSiteRegionReactor typeEvent description
ENS 4017619 September 2003 04:16:00LimerickNRC Region 1GE-432 of 165 offsite sirens not functioning due to loss of power/equipment failure because of ongoing storm. The licensee will inform the affected counties/PEMA and the NRC Resident Inspector.
ENS 4032918 November 2003 10:47:00LimerickNRC Region 1GE-4On 11/18/03 at 0435 EST, it way discovered that the ENS phone system was inoperable when the NRC was unable to contact the Limerick Generating Station Control Room for a routine plant status update. The NRC was able to contact the Limerick Control Room via a normal station telephone. The cause of the communication loss was investigated and determined to be an ENS phone in TSC that was "off the hook". The TSC ENS phone had a headset connected that was inadvertently turned on and resulted in the busy signal when the NRC attempted to call. The TSC ENS phone headset was turned off restoring the communication line. Communications were verified with the NRC at 0459 via the ENS phone. This condition is being reported as an 8 hour notification per the requirements of 10 CFR 50.72(b)(3)(xiii) for loss of offsite communications capability. The licensee notified the NRC Resident Inspector.
ENS 4044413 January 2004 20:19:00LimerickNRC Region 1GE-4

Explosion occurred in a non-safety related transformer at 1908 EST 0n 01/13/04. The transformer became deenergized as a result of the explosion. Licensee declared an Unusual Event at 1921 EST on 01/13/04 due to an explosion resulting in visible damage to a non-safety related transformer in the Turbine Enclosure building. There was no fire or injured personnel, and the site did not require any off site assistance. The transformer explosion resulted in the loss of power to some 480 VAC non-safety related loads (most significant was a non-safeguard DC battery charger). The explosion has not severely impacted Unit 1 operations. The transformer has been inspected, and it appears that the explosion was internal to the transformer and due to an electrical malfunction. Security personnel conducted thorough walk downs of all areas and had no concerns. NRC Management determined that this event did not require entry into the Monitoring Phase of Normal Mode of Incident Response at 2040 on 01/13/04. The licensee notified the state and local emergency management agencies and notified the NRC Resident Inspector.

  • * * UPDATE FROM PETE ORPHANOS (VIA FACSIMILE) TO HOWIE CROUCH @ 0221 EST ON 1/14/04 * * *

Notification of reduction in classification status from Unusual Event. Failure of non-safeguards electrical supply determined to be due to cable fault. Plant remains stable at 100% power. No additional equipment damage identified. Blocking and repair planning in progress. The unusual event was terminated by the licensee at 2151 hrs. EST on 1/13/04. The licensee has notified the NRC Resident Inspector and State and County authorities. A media press release will be issued in the morning.

Notified DHS (Beal) and FEMA (Caldwell).
ENS 4060019 March 2004 21:00:00LimerickNRC Region 1GE-4

On 3/19/04 at 14:08 PM EST, the Unit-1. HPCI system was declared inoperable due to a hand-switch failure, which prevented main control room operation of the HV-055-1F0O1 HPCI steam admission valve. The system had just successfully completed its functional surveillance test and the switch broke resulting in the operators using an, alternate means to shutdown the HPCI system. The steam admission valve is not a PCIV. The valve was open all the time; the system was shutdown using an alternate procedure. The system is now blocked for hand-switch replacement. This report is being made pursuant to 10CFR50.72(b)(3)(v) for failure of a single train accident mitigation system. The NRC Resident inspector was notified. Operators entered the unit into a 14 day LCO for declaring HPCI system inoperable.

          • RETRACTED ON 4/14/04 AT 12:56 FROM GAMBLE TO LAURA*****

This is a retraction of the event notification made on 3/19/04 at 21:00 hours. This event (#40600) was initially reported as a safety system functional failure under the requirement of 10CFR50.72(b)(3)(v)(D). Unit 1 High Pressure Coolant Injection (HPCI) system was declared inoperable due to a handswitch failure that prevented operation of the HV-055-1F001 HPCI steam admission valve from the main control room. The handswitch failed while attempting to close the steam admission valve during system shutdown at the conclusion of surveillance testing. The operator then closed the outboard steam line isolation valve to complete the system shutdown. HPCI is automatically initiated by low reactor level or high drywell pressure signals. Manual HPCI initiation for inventory makeup is performed by depressing the initiation pushbutton. Both automatic initiation and manual initiation using the pushbutton open the steam admission valve. The failed handswitch did not adversely affect the initiation of the HPCI system in the inventory makeup mode. The manual startup of the system in the test mode of operation is unavailable when the handswitch is failed. The test mode can be used to remove decay heat following an isolation of the main steam lines but it is not a credited safety function. The steam admission valve handswitch would not be used to shutdown the system when an automatic initiation signal is present; the outboard steam line isolation valve would be closed to secure the system. This is the method that was used to secure the system during the surveillance test. The handswitch is mainly used to startup and secure the system during surveillance testing. The system was removed from service as part of a planned evolution to conduct surveillance testing in accordance with an approved procedure and the plant's Technical Specifications. The system was secured for the purpose of concluding the surveillance test and replacing the handswitch. The failed handswitch did not adversely affect the systems capability of performing its safety function. A condition did not exist at the time of discovery that could have prevented the fulfillment of the HPCI safety function. Notified R1DO (B. MCDERMOTT).

ENS 407883 June 2004 12:47:00LimerickNRC Region 1GE-4

Limerick has completed the 10CFR Part 21 evaluation of the failure of the spring charging function on an Asea Brown Boveri (ABB) Model HK circuit breaker. The investigation determined that the primary contributor to the failure was the replacement of ABB latch reset torsion spring number 195205A00 with a weaker spring that was supplied with the breaker overhaul kit number 716656T104. Secondary contributors to the failure were normal wear on additional parts in the operating mechanism. ABB supplied a six-turn latch reset torsion spring and a five-turn latch reset torsion spring under spring part number 195205A00 and overhaul kit number 716656T104. The spring of concern is a six-turn spring that does not provide as much force as the original six-turn or five-turn spring. When informally tested during the investigation the six-turn spring provided approximately 66 ounces of force and the five-turn spring provided approximately 102 ounces of force. The original six-turn spring provided a force of 88 ounces. Limerick's evaluation concluded that installation of the replacement six-turn latch reset torsion spring could create a substantial safety hazard depending on the breaker's application. Therefore, this notification is being submitted pursuant to the requirements of 10CFR21.21(d)(3)(i). The required 10CFR21.21(d)(3)(ii) 30-day written notification will provide more detail when submitted. ABB evaluation of this issue is still in progress. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 6/30/04 @ 1451 HRS. EDT FROM GAMBLE TO CROUCH * * *

This is a retraction of the Part 21 initial notification made per 10CFR21.21(d)(3)(i) on 6/3/04 at 12:47 EDT (EN# 40788). The issue involved an in-service malfunction of the closing spring charging function of an Asea Brown Boveri (ABB) Model HK circuit breaker following replacement of the latch reset torsion spring (ABB number 195205A00) during breaker maintenance. The spring was supplied with ABB overhaul kit number 716656T104. Upon further review of the Part 21 reporting requirements it has been determined that this issue does not require reporting. NUREG-1022 Rev.2 'Event Reporting Guidelines 10CFR50.72 and 50.73' provides guidance for Part 21 reporting in section 5.1.8. The NUREG section references a federal register notice (56 FR 36081, July 31, 1991) in footnote 18, which provided notification of an amendment to 10CFR Parts 21 and 50. The amendment was intended to reduce duplicate reporting of defects. The notice provides the following guidance for components that have been installed in operating plants: Operating license holders can reduce duplicate evaluation and reporting effort by evaluating deviations in basic components installed in operating plants which produce events which could meet the criteria of 50.72 and 50.73. If the evaluation of events using the criteria of 50.72 and 50.73 results in a finding that the event is reportable and the event is reported via these sections, then as indicated in 21.2(c), the evaluation, notification, recordkeeping, and reporting obligations of part 21 are met. If the event is determined not to be reportable under 50.72 or 50.73, then the obligations of part 21 are met by the evaluation. The evaluation using the criteria of 50.72 and 50.73 resulted in a finding that the event was not reportable. There was no reasonable expectation of preventing fulfillment of a safety function, no equipment was declared inoperable, and the principle safety barriers were not seriously degraded. Therefore, this event is not reportable using the criteria of 50.72 and 50.73 and the Part 21 evaluation obligation is met. The licensee has notified the NRC Resident Inspector of this retraction. The Headquarters Operations officer notified R1DO (Barkley), R2DO (Evans), R3DO (Gardner), R4DO (Whitten), and NRR (Dennig).

ENS 4083222 June 2004 15:10:00LimerickNRC Region 1GE-4Unit 2 reactor scrammed at 13:13 (EDT) following an electrical yard manipulation. The reactor scram occurred as a result of an RPS (Reactor Protections System) actuation following an automatic trip of the main turbine from a generator lockout. All control rods inserted (fully). The plant is stable (in mode 3). No ECCS (Emergency Core Cooling System) or safety relief valve actuations have occurred. This report is being made pursuant to 50.72(b)(2)(iv)(b). At this time the plant is stable, as expected. An investigation is in progress to determine the reason for the electrical fault. All plant systems functioned as required and decay heat removal is being performed via bypass to the main condenser. The licensee notified local and State authorities and the NRC Resident Inspector.
ENS 4089523 July 2004 11:10:00LimerickNRC Region 1GE-4On May 26, 2004 at 16:22 hours and inadvertent primary containment isolation signal was initiated following restoration from a surveillance test on the 2A Reactor Enclosure ventilation exhaust duct radiation monitor. The isolation was due to a fuse failure that caused isolation signals on Group 6A, 6B, 6C, and 7A primary containment isolation valves (PCIVs). The Unit 2 reactor enclosure ventilation isolated. The 2A standby gas treatment system (SGTS) and 2A reactor enclosure recirculation system (RERS) trains initiated. The instrument gas compressor suction valve and the 2A instrument gas header supply valve closed. The containment nitrogen inerting valve and the 2A instrument gas header supply valve closed. The containment nitrogen inerting block valve closed. The containment atmospheric sample valves received an isolation signal but were in a closed position prior to the event. All system functioned as designed during the event. The laboratory analysis of the fuse determined that the most probable cause of the event was an age related degradation of the fuse that reduced its current carrying capacity. The fuse was operating under steady state conditions for approximately 30 seconds prior to the failure. A fuse replacement plan was in progress prior to the event due to prior age related failures of this type of fuse. The fuse replacement plan will be evaluated to ensure the current schedule is adequate. Component data: Type: Fuse Manufacturer: Bussmann Model number: MIN-5 The NRC Resident Inspector was notified of this event by the licensee.
ENS 4104316 September 2004 12:17:00LimerickNRC Region 1GE-4This 24 hour Notification to the NRC Operations Center is being made per Operating License No. NPF-39, Section 2.F to report a potential violation of the requirements contained in Section 2. C of Limerick Unit 1 license. On September 15, 2004 at 1600 Hrs. it was determined during an investigation of megawatt output differences between the two LGS Units, that LGS Unit 1 secondary plant parameters were identified as being outside of their expected range. This change occurred over several months at the rate of 0.1 %/month for a total potential error of 0.4%. This data indicates that LGS1 could possibly be above the operating license limit of 3458 MWth. Unit 1 power was reduced to 99% power to 3423 MWth as of 1618 to provide margin to licensed thermal power limit. A written report is required within 30 days in accordance with 10 CFR 50.73. The licensee has notified the NRC resident inspector.
ENS 4134619 January 2005 11:08:00LimerickNRC Region 1GE-4

The notification is being made pursuant to Unit 2 Operating License for potential non-compliance of the Fire Protection Program. At 12:55 on January 18, 2005 following the review of Operating Experience for Wolf Creek (ENS 41327), it was discovered that the pilot lines to the manual pneumatic actuator pilot lines on the Halon bottles for the Halon System for the Auxiliary Equipment Room were incorrectly piped. In accordance with TRM 3.7.6.4 a continuous fire watch was established in the area. This event resulted in a condition that could have rendered the Halon System for the Unit 2 Auxiliary Equipment Room inoperable during a fire. The Unit 1 Auxiliary Equipment Room Halon System was not affected and remained operable. At this time the cause of this condition is not currently known, and an investigation is ongoing. NRC Resident Inspector was notified of this event by the licensee. HOO NOTE: See Ens # 41326 and 41327 for similar reports.

  • * * UPDATE AT 1059 ON 02/16/05 FROM MARK CRIM TO W. GOTT * * *

The notification is being made to retract the ENS 41346 Rev 0 reported on 1/19/05 pursuant to Unit 2 Operating License for a potential noncompliance of the Fire Protection Program. At 12:55 on January 18, 2005 following the review of Operating Experience for Wolf Crook (ENS 41327), it was discovered that the pilot lines to the manual pneumatic actuator on the main and reserve Halon cylinders for the Unit 2 Auxiliary Equipment Room Under Floor Halon System were incorrectly piped. In accordance with TRM 3.7.6.4, a continuous fire watch was established in the area.. Immediately following the event, it was believed that the condition could have rendered the Unit 2 Auxiliary Equipment Room Under Floor Halon System inoperable during a fire. On January 19, 2005 Limerick corrected the piping to meet the vendor design for the manual-pneumatic actuators associated with the Unit 2 Auxiliary Equipment Room Under Floor Halon System. On January 26, 2005 Chemetron performed a functional test of the Halon System for Callaway with the incorrect pilot line piping and discovered that Halon injected properly with a 2 second delay (See IEN 2005-001). Callaway had a similar Halon system configuration as Limerick Unit 2 Auxiliary Equipment Room Under Floor Halon System (same make and model number manual-pneumatic actuators and cylinder heads). An evaluation of the test report concluded that the Limerick Unit 2 Auxiliary Equipment Room Under Floor Halon System would have actuated in the event of a fire. In conclusion, despite the pilot line piping error, the Unit 2 Auxiliary Equipment Room Under Floor Halon System would have remained operable and would have completed it's suppression function during a fire. Therefore, there was no violation of the Unit 2 Operating License Section 2.C.(3) for the Fire Protection. The licensee will notify the NRC Resident Inspector. Notified R1DO (E. Coby).

ENS 4141517 February 2005 10:28:00LimerickNRC Region 1GE-4On January 22, 2005 a radiation protection technician discovered that a radiation detector calibration source was missing from its locked storage cabinet. An investigation was initiated and efforts to locate the source continue but the source has not been located. The source is approximately 2 inches in diameter in the form of a metal disc containing 0.0154 micro-curies of Thorium-230 that is used to calibrate SAC-4 alpha counters. The source is labeled and poses no radiological hazard to individuals that could unknowingly be in close proximity to it. The source was last used to calibrate a SAC-4 alpha counter on 1/20/2005. 10CFR20.2201(a)(1)(ii) requires a telephone report to the Operations Center in accordance with 10CFR50.72 within 30 days of the loss of licensed material in a quantity greater than 10 times the quantity specified in Appendix C to Part 20. The quantity specified in Appendix C for Thorium-230 is 0.001 micro-curies; therefore, this report is required. The licensee notified the NRC Resident Inspector.
ENS 4154028 March 2005 23:56:00LimerickNRC Region 1GE-4The following information was obtained from the licensee via facsimile (licensee text in quotes): Unit 2 High Pressure Coolant Injection (HPCI) (was) declared inoperable due to a loose control power fuse clip associated with the HPCI Pump Suction from Suppression Pool Valve HV-055-212041. The loose clip resulted in loss of control power to this DC motor operated valve and therefore rendered the HPCI system inoperable. The fuse clip has been replaced and the HPCI system returned to an operable status. This report is being made pursuant to 10CFR 50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system that is needed to mitigate the consequences of an accident. The licensee will notify the NRC Resident Inspector.
ENS 415736 April 2005 22:56:00LimerickNRC Region 1GE-4At 1655 on April 6, 2005, a trip of the 4A/4B Transformer occurred at Limerick Generating Station in the 500 KV Substation. This de-energized one of the required off site sources and the associated 20 Start-up Bus and 201 Safeguard Bus, causing a valid actuation signal for the D12, D14, D21, and D23 Diesel Generators. All Diesels started and their associated 4 KV buses swapped to the 101 Safeguard Bus as required. Cause of the 4A/4B Transformer trip is under investigation. Power reduction on Unit 2 was performed in response to lowering Main Condenser vacuum during power supply transfers. Condition was stabilized and Unit 2 Reactor power restored to 100 %. The cause of the lowering main condenser vacuum was that when the bus transfer occurred, several air valves on Unit 2 cycled which caused the lowering vacuum. Once power transferred, Unit 2 stabilized and was restored to 100% power. Unit 1 main condenser vacuum was not affected since power was not transferred on Unit 1. Additionally, a Group 6A valve isolation signal was generated. This caused the purge valves to receive an isolation signal but the purge valves were not in operation nor were they required to be in operation at the time of the isolation signal. Both unit's Reactor Water Clean-up (RWCU) pumps tripped due to the isolation signal. At the time of this report, the isolation signal was reset, Unit 1 RWCU pump has been reset, and preparations are being made to restart Unit 2 RWCU pump. The only other anomaly is that Unit 2 D22 diesel is in a maintenance outage and is scheduled to be returned to service tomorrow. Currently, both units are in a 72-hour LCO action statement due to loss of one offsite power supply. The licensee will inform the NRC resident inspector.
ENS 416675 May 2005 15:44:00LimerickNRC Region 1GE-4This 60-day ENS report is being made per 10CFR 50.73(a)(2)(iv)(A) to report an invalid automatic actuation of systems listed in paragraph (a)(2)(iv)(B), namely ECCS, emergency diesel generator (EDG), and emergency service water (ESW). On March 6, 2005 at 15:07 hours a Unit 2 Division 3 LOCA signal was inadvertently initiated during replacement of a power supply on ECCS. Continuity on the 24 VDC power distribution signal common was lost while lifting leads on the power supply. One terminal on the power supply was part of a daisy chain circuit connection. This resulted in an unplanned actuation of the high drywell pressure relays. Two 24 VDC power supplies are connected in parallel to supply power to Division 3 ECCS trip units and relays. It was planned to replace one of these power supplies while the power distribution network remained energized by the redundant power supply. However, the continuity of the power distribution network relied on the connection of two leads on one terminal on the out-of-service power supply. When the two leads were separated several relays lost their normal connection to the signal common. Reverse currents caused the false actuation of the Division 3 high drywell pressure relays. D23 EDG automatically started and ran unloaded. The C ESW pump automatically started due to the EDG start. The 2A Core Spray (CS) loop received a partial actuation in that the Division 3 signal was initiated but the Division 1 signal was not initiated. 2C CS pump started as designed and 2A CS pump did not start which was expected. The 2A CS loop automatic valve alignment is initiated by the Division 1 signal; therefore, no automatic 2A CS loop valve alignment occurred. All systems functioned as designed during the event. The cause of the event was that the work package planner for the power supply replacement failed to recognize the impact on plant systems and as a result applied less than adequate technical rigor. The maintenance planning procedure will be revised to ensure the appropriate level of technical rigor is applied for work packages that lift or manipulate a signal common lead. This event Is reportable per 10CFR50.73(a)(2)(iv)(A) since 2C Core Spray pump, D23 EDG and C ESW pump automatically actuated on an invalid signal. The NRC Resident Inspector has been notified.
ENS 4172624 May 2005 15:33:00LimerickNRC Region 1GE-4A non-licensed employee supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been terminated. Contact the Headquarters Operations Officer for additional details. The licensee notified the NRC Resident Inspector.
ENS 4173631 May 2005 17:22:00LimerickNRC Region 1GE-4On Tuesday May 31, 2005, Limerick Unit 2 was operating at 100% power at 10:31 hours when the 2A Reactor Recirculation Motor-Generator speed increased to the high-speed stop. Reactor power increased to approximately 106% and three main steam bypass valves opened as designed to control pressure. Operators reduced power to 98% as directed by emergency operating procedures using the 2B Reactor Recirculation Pump. This event caused thermal power to exceed the 100% rated maximum power level of 3458 megawatts thermal specified in section 2.C.(1.) of the Limerick Unit 2 operating license. Therefore, this event is being reported via ENS within 24 hours with a written followup within 30 days as required by section 2.E of the Limerick Unit 2 operating license. The licensee stated that power level exceeded 100% for approximately 1 minute during the event transient. Both the mechanical and electrical overspeed stops on the MG set were actuated. The licensee reviewed the transient and it does not appear that any other thermal limits were exceeded and there is no indication of any affect on the core or the fuel. Although trouble-shooting of the problem is still in progress, the licensee currently believes that the event was caused by the MG set controller. The licensee plans to remain at approximately 97% power until the problem is resolved. The licensee notified the NRC Resident Inspector.
ENS 4184818 July 2005 11:15:00LimerickNRC Region 1GE-4Unit 1 reactor automatically scrammed at 09:52 as a result of an RPS Actuation following a main turbine trip caused by unit protection relaying. All control rods inserted. The plant is stable. No ECCS or SRV actuations occurred. This report is made pursuant to 50.72(b)(2)(iv)(B). An investigation into the cause is currently in progress. The plant is currently stable in mode 3. No safety relief valves actuated. The current decay heat removal path is normal feedwater to the reactor steaming through the turbine bypass valves to the condenser. No other safety systems actuated. Electric power to the safety busses was supplied via normal offsite power. No bad weather conditions are present. Current reactor pressure is 900 psi with temperature at about 540 degrees. Currently troubleshooting is ongoing to investigate the cause of the trip. The licensee currently plans to stay in mode 3 until the investigation is complete. No safety related systems are currently out of service. There was no estimated restart date. The licensee notified the NRC Resident Inspector.
ENS 4205412 October 2005 23:55:00LimerickNRC Region 1GE-4Unit 2 Reactor automatically scrammed at 2224 (EDT) as a result of an RPS actuation due to Reactor High Pressure. All control rods inserted. The plant is stable. No ECCS or SRV actuation occurred. This report is made pursuant to 50.72(B)(2)(iv)(B). An investigation into the cause is currently in progress. Electric plant lineup is in a normal stable lineup. Reactor water level is being maintained via main feedwater system and removing decay heat via the steam bypass valves to the main condenser. This event had no effect on Unit 1. The licensee notified the NRC Resident Inspector, Pennsylvania Emergency Management Agency (PEMA), and the Berks, Chester, and Montgomery County emergency agencies.
ENS 421939 December 2005 13:15:00LimerickNRC Region 1GE-4At 0901 on December 9, 2005, a trip of the 10 Startup Bus Breaker occurred at Limerick Generating Station in the 220 KV substation. This de-energized one of the required offsite sources and the associated 10 Startup Bus and 101 Safeguard Bus, causing a valid actuation signal for the D11, D13, D22 and D24 Diesel Generators. All diesels started and their associated 4 KV buses swapped to the 201 Safeguard Bus as required. The cause of the 10 Startup Bus Breaker trip is under investigation. Units 1 and 2 remain at 100% power. No safety related loads were lost. The diesel generators were still running at the time of the call but, the licensee was shutting down the diesels per procedure. The licensee notified the NRC Resident Inspector.
ENS 4257212 May 2006 10:35:00LimerickNRC Region 1GE-4The notification is being made pursuant to 10CFR50.73(a)(2) (iv) (A) and is reported per 10CFR50.73(a)(1) An invalid actuation of the 1 C Core Spray Pump start during D13 LOCA/LOOP Testing. a) The specific train(s) and system(s) that were actuated. The 1C Core Spray Pump actuated automatically on an inadvertent Division 3 LOCA signal during LOCA/LOOP testing. No other ECCS train/system actuated. b) Whether each train actuation was complete or partial. The 1C Core Spray Pump actuated in the minimum flow protection mode. c) Whether or not the system started and functioned successfully. The 1 C Core Spray System started and functioned successfully but did not inject into the vessel. On March 14, 2006 at 5:40 PM during performance of the D13 LOCA/LOOP Test, ST-6-092-117-1, the 1 C Core Spray pump was inadvertently started. The pump started (but did not inject) when an I&C Technician attempted to demonstrate operation of the test switch. He inadvertently picked up the energized test switch which was next to 2 spare test switches and manipulated it which resulted in a Division 3 LOCA signal to the 1C Core Spray Pump. The 1C Core Spray Pump never injected and was running with min-flow protection and functioned as expected. The cause of the event was lack of attention to detail and self check. The licensee notified the NRC Resident Inspector.
ENS 4271519 July 2006 01:07:00LimerickNRC Region 1GE-4

48 of 165 offsite sirens are not functioning due to loss of power/equipment problems because of recent storm. Efforts are in progress to restore power to the affected sirens. The affected sirens are located in Chester County. Compensatory measures are in effect to alert the public should the need arise. The licensee informed the NRC Resident Inspector.

      • UPDATE FROM C. PEAKS TO J. KNOKE AT 08:40 EDT ON 07/21/06 ***

The licensee reported that only 22 of 165 sirens are now inoperable. This is less than the reportable (25%) amount of 41 sirens.

The licensee notified the NRC Resident Inspector.  Notified R1DO (Kinneman).
ENS 428306 September 2006 16:23:00LimerickNRC Region 1GE-4This 60-day ENS report is being made per 10CFR 50.73(a)(2)(iv)(A) and 10CFR50.73(a)(1) to report an invalid automatic actuation of systems listed in paragraph (a)(2)(iv)(B), namely emergency service water (ESW). On Sunday July 9, 2006, at 18:49 hours, an invalid actuation of the B ESW pump occurred. The B ESW loop start was a partial actuation and the loop functioned successfully following the invalid actuation. The A ESW loop was not affected. An investigation identified that corrosion on the D12 emergency diesel generator (EDG) jacket water pump discharge pressure switch caused the invalid partial actuation. The cause of the pressure switch failure was due to a cracked supply tube, which allowed moisture to enter the cabinet causing the corrosion. EDG jacket water pump discharge pressure is utilized to initiate logic that starts the ESW pump when the EDG is running. ESW is the cooling medium for the EDG. The switch failure also caused inoperability of D12 EDG since it defeated the capability for the EDG to start. The failed pressure switch and associated tubing were replaced and successfully tested. D12 EDG was declared operable on Monday July 10, 2006 at 12:46 hours. An inspection of the other seven EDGs identified that the D11 EDG pressure switch was also corroded. The D11 EDG pressure switch was replaced. The inspection determined that the jacket water pressure switches on the other six EDGs were not degraded. This event is reportable per 10CFR50.73(a)(2)(iv)(A) since B ESW pump automatically actuated on an invalid signal. Component data: Equipment number: PSH-GA-110B Manufacturer: A160 Allen-Bradley Co. Model number: 636-C3 The licensee notified the NRC Resident Inspector.
ENS 428837 October 2006 11:05:00LimerickNRC Region 1GE-4

A division 2 Primary Containment Isolation Instrument System component inoperable required the manual isolation of High Pressure Coolant Injection (HPCI) outboard Primary Containment Isolation valves (PCIV). This isolation was required by T/S action 3.3.2.b.1. This report made pursuant to 10CFR 50,72 (b)(3)(v)(D) for the inability of single train system to mitigate the consequences of an accident. At approximately midnight on 10/7/06, Control Room Operators received a Div 2 Steam Leak Detection Trouble Alarm. Troubleshooting identified the failure as associated with the GE NUMAC drawer where temperature inputs are processed. The applicable 14-day T/S LCO Action Statement requires completion of repairs within 6 hours or isolation of HPCI 1 hour later. HPCI was isolated at 0657 EDT. There was no I&C work in progress at the time of the failure. Repair parts are available and onsite. The licensee informed the NRC Resident Inspector.

  • * * RETRACTION RECEIVED FROM EDWARD DENNIN TO JOE O'HARA AT 1500 ON 12/04/06 * * *

This is a retraction of the event notification made on 10/07/06 at 11:05 hours. This event (#42883) was initially reported as a safety system functional failure under the requirement of 10CFR50.72(b)(3)(v)(D). Unit 2 High Pressure Coolant Injection (HPCI) system was declared inoperable due to a manual closure of the HPCI steam line outboard primary containment isolation valve (PCIV). The PCIV was closed to support the maintenance on an inoperable steam leak detection (SLD) channel and to satisfy the Technical Specification (TS) 3.3.2 Isolation Actuation Instrumentation action statement. The event was initiated at 00:06 hours by a trouble alarm due to a 'self test fault' condition on the Division 2 SLD instrument channel. Troubleshooting determined that the instrument channel was inoperable. TS 3.3.2 Action 'b.1' requires the channel to be restored to operable status within 6 hours. Since this action could not be completed Table 3.3.2-1 Action 23 was applicable. Action 23 required the affected system isolation valves to be closed within one hour and the system (HPCI) to be declared inoperable. This action was completed at 06:57 hours. Two modules were replaced in the SLD instrument chassis. The instrument channel was tested satisfactorily and returned to service, Unit 2 HPCI was restored to operable status at 23:48 hours. The system was removed from service as part of a planned evolution to conduct maintenance in accordance with an approved procedure and the plant's Technical Specifications. The system was secured for the purpose of conducting maintenance on an inoperable SLD instrument channel and completing the TS action. The failed instrument did not adversely affect the HPCI system's capability of performing its safety function. HPCI remained capable of automatic initiation until the PCIV was manually closed to support maintenance by completing the TS actions. A condition did not exist at the time of discovery that could have prevented the fulfillment of the HPCI safety function. The licensee notified the NRC Resident Inspector. Notified R1DO(Sykes).

ENS 4290715 October 2006 15:44:00LimerickNRC Region 1GE-4During routine testing of the Unit 2 High Pressure Coolant Injection (HPCI) Turbine Hydraulic Control System, the HPCI Turbine Control Valve failed to Open as expected. The Unit 2 HPC1 system was declared Inoperable per T/S 3.5.1 (14 day LCO). This report made pursuant to 10CFR 50.72 (b)(3)(v)(D) for the inability of single train system to mitigate the consequences of an accident. All other ECCS systems are operable. The licensee notified the NRC Resident Inspector.
ENS 4323113 March 2007 15:14:00LimerickNRC Region 1GE-4It was discovered that a valid Low Main Condenser Vacuum group 1A Nuclear Steam Supply Shutoff System (NS4) isolation for the Main Steam Isolation Valves (MSIV's) had been received while breaking main condenser vacuum while in Mode 4 for planned refueling outage 2R09. The isolation actuation was received as main condenser vacuum lowered below the isolation setpoint during the planned evolution of breaking of main condenser (vacuum). All valves for this isolation signal had previously been closed by approved plant procedures while in Mode 3. The valid isolation signal was caused by not having the isolation signal bypassed as allowed by approved plant procedures. The licensee will notify the NRC Resident Inspector.
ENS 4331524 April 2007 04:04:00LimerickNRC Region 1GE-4Limerick Unit 2 automatically shutdown on low reactor water level (+12.5 inches) at 0210 on 4/24/07. The cause is under investigation at this time. All control rods inserted as required. HPCI and RCIC initiated, injected and restored reactor water level. Lowest reactor water level noted was -73 inches. Primary containment isolation signals on +12.5 inches and -38 inches occurred. All isolations completed as required. The plant is currently in hot shutdown maintaining normal reactor level with feedwater in service. Approximately 16000 gallons was injected in 4 minutes. There was no indication of RCS leakage. The licensee is investigating whether a feedwater runback had occurred. No SRVs lifted with the highest pressure observed at 1050 psi. The main condenser remains in service for decay heat removal. All EDGs are available, if needed. The licensee informed the NRC Resident Inspector and will inform both the State and Local authorities.
ENS 4336616 May 2007 14:30:00LimerickNRC Region 1GE-4This 60-day ENS report is being made per 10CFR 50.73(a)(2)(iv)(A) and 10CFR 50.73(a)(1) to report invalid automatic actuations of systems listed in paragraph (a)(2)(iv)(B), namely core spray (CS) and residual heat removal (RHR). Unit 2 commenced refueling outage activities on Saturday March 10, 2007. Relay replacements for the 4 kv safeguard bus LOCA auxiliary control time delay relays were planned for all four buses due to a relay failure on Unit 1 that was identified during the prior refueling outage testing. On Monday March 19, 2007, at 02:20 hours, during emergency diesel generator (EDG) surveillance testing a Unit 2 Division 3 LOCA signal was inadvertently initiated during the planned replacement of the D23 bus LOCA auxiliary control relay (162-117). The relay was being replaced at a pre-determined step in the test. The relay was in an energized state when removed. When the new relay was installed an unplanned actuation of LOCA load shedding and sequential loading occurred. The relay was subsequently replaced and tested successfully. D23 EDG had been secured just prior to the event. The following loads were tripped and automatically restored: 2C CS pump and D234 load center breaker. The C emergency service water (ESW) pump tripped and did not restart since the EDG was not running. The 2C RHR pump continued to run. The 2A CS loop received a partial actuation in that the Division 3 signal was initiated but the Division 1 signal was not initiated. The 2C CS pump was operating in full flow test mode; therefore, it tripped and re-started as designed and 2A CS pump did not start which was expected. The 2A CS loop automatic valve alignment is initiated by the Division 1 signal; therefore, no automatic 2A CS loop valve alignment occurred. On Wednesday March 21, 2007 at 14:08 hours during EDG surveillance testing a Unit 2 Division 2 LOCA signal was initiated during the test which started the D22 EDG and tripped the D224 load center breaker as expected. However, the load center breaker did not re-close which was not expected and other expected actions did not occur. At 14:41 hours, 33 minutes later, the remaining LOCA actions occurred when 2B RHR pump, 2B CS pump, and 2B reactor enclosure recirculation system (RERS) fan automatically started, and D224 load center breaker automatically closed due to a late actuation of the D22 bus LOCA auxiliary control relay (162-116). At 15:48 an additional unexpected relay actuation caused the 2B CS pump and D224 load center breaker to trip. The relay had been replaced earlier in the day and the ongoing testing was intended to satisfy the post maintenance test (PMT). However, the relay did not actuate at the point in the test designated as the PMT; the relay actuated unexpectedly 33 minutes later. The cause of the first event was a less than adequate technical review of a test revision that added a step to replace the bus LOCA auxiliary control relay. The affected tests have been revised to replace the relay at a point in the test when it is de-energized. The cause of the second event was an equipment failure due to an intermittent connection between the relay pin connector and the relay base. The affected relay and base have been replaced and tested successfully. All of the systems that received start signals functioned successfully. The only equipment malfunction was associated with the degraded relay. The RHR and CS starts were partial actuations. The D22 EDG train start was an expected actuation. The C ESW train was tripped but was not automatically started. This event is reportable per 10CFR50.73(a)(2)(iv)(A) since 2B RHR pump, 2B CS pump, and 2C CS pump automatically actuated on an invalid signal. Component data: Equipment name: D22 Bus LOCA Aux Control Time Delay Relay Equipment number: 162-116 Manufacturer: A348 Amerace Corp Model number: ETR14D3A002 Serial number: 83330224 The licensee notified the NRC Resident Inspector.
ENS 4343621 June 2007 04:05:00LimerickNRC Region 1GE-4

During performance of the quarterly HPCI valve stroke test the HV-55-2F006, HPCI pump discharge isolation valve to Core Spray failed to open within the maximum allowed time. The HV-55-2F006 valve is a motor operated valve and the maximum allowed opening time is 17.25 seconds. The valve was given an open signal via the hand switch as required by the test but did not initially respond. Several minutes later the valve went full open. HPCI was declared inoperable at 0315 on 6/21/2007. Cause for valve stroke time failure is not known at this time. As a result, the licensee is in a 14 day shutdown LCO. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM ARNOSKY TO HUFFMAN AT 0807 EDT ON 8/01/07 * * *

This is a retraction of the event notification made on 6/21/07 at 04:05 hours EDT. This event (#43436) was initially reported as a condition that at the time of discovery could have prevented the fulfillment of the High Pressure Coolant Injection (HPCI) system safety function under the requirement of 10CFR50.72(b)(3)(v)(D). The Unit 2 HPCI system was declared inoperable due to failure of the HPCI pump discharge isolation valve to Core Spray to open within the maximum allowed time during surveillance testing. The valve was required to open within 17.25 seconds but opened several minutes after the open signal was initiated. The open contactor was replaced and the valve was successfully tested. The affected valve was declared operable on 6/22/07 at 04:07 hours. The HPCI system was restored to operable on 6/23/07 at 04:07 hours following completion of maintenance and testing activities. An evaluation determined that HPCI was capable of injecting sufficient flow to complete its safety function through the unaffected operable injection flow path to the feedwater header. The achievable flow rate would have exceeded the leakage from a one-inch liquid line break. Also, HPCI operation remained capable of being terminated by operator action during an ATWS event. Therefore, HPCI remained capable of fulfilling its safety function while the injection flow path to Core Spray was unavailable. A condition did not exist at the time of discovery that could have prevented the fulfillment of the HPCI safety function. The licensee notified the NRC Resident Inspector. R1DO (White) notified.

ENS 4345528 June 2007 10:56:00LimerickNRC Region 1GE-4This eight hour notification is being made per 10 CFR 50.72(b)(3)(xiii) to report a loss of >25% of the EPZ sirens for greater than one hour. 44 of 165 offsite sirens are not functioning due to loss of power/equipment problems because of a recent storm. Efforts are in progress to restore the affected sirens. At 1000 6/28/07 less than 25% of sirens are unavailable. The licensee notified the NRC Resident Inspector, the State of Pennsylvania, and local governments.
ENS 4364517 September 2007 03:16:00LimerickNRC Region 1GE-4During performance of the quarterly HPCI valve stroke test the HV-055-2F093, HPCI Vacuum Breaker Outboard PCIV, failed to close. The PCIV was declared inoperable. The valve was subsequently closed and de-energized to meet Technical Specification requirements. The valve did close from the handswitch on the subsequent attempt, investigation into the cause is in progress. The closure of this valve at 0149 on 9/17/07 prevents Unit 2 HPCI from performing it's safety related function. Unit 2 RCIC and all other Unit 2 ECCS systems remain operable. The licensee notified the NRC Resident Inspector.
ENS 4389812 January 2008 19:09:00LimerickNRC Region 1GE-4An overvoltage condition occurred on the D23 Safeguards 4kv bus during planned system outage window EDG governor testing. The EDG output breaker was immediately opened and the engine secured per test direction. Due to the output breaker being opened, the D23 bus then experienced an undervoltage condition. Bus voltage monitoring instrumentation automatically initiated automatic closure of the 201-D23 Bus Offsite Supply Feed Breaker after a 1 second time delay and re-energized the D23 Safeguards Bus per design. The remaining three 4kv buses and Emergency Diesel Generators were unaffected and remain operable. The voltage regulation circuit is being investigated at this time to assist in determining the cause of the overvoltage condition. The EDG was out of service and inoperable during the testing. The EDG governor was replaced during the outage window and was being fine tuned when the event occurred. The licensee is currently in day 6 of a 30 day LCO (3.8.1.1). The licensee notified the NRC Resident Inspector.
ENS 4394229 January 2008 21:50:00LimerickNRC Region 1GE-4

The D/C power supply for the Unit 1 High Pressure Coolant Injection (HPCI) system instrumentation has failed resulting in the inability of HPCI to meet its requirement to support safely shutting down the reactor during a Station Blackout (Complete Loss of A/C Power) situation. The Emergency Core Cooling System (ECCS) function of HPCI is still available with the alternate A/C power supply. The licensee is actively troubleshooting the power supply. The HPCI unavailability places the licensee in a 14-day Limiting Condition for Operation action statement. The licensee has notified the NRC Resident Inspector.

* * * RETRACTION FROM D. SEMETER TO P. SNYDER ON 3/27/08 AT 1300 * * * 

This is a retraction of the event notification made on 1/29/08 at 21:50 EST hours. This event (#43942) was initially reported as a safety system functional failure under the requirement of 10 CFR 50.72(b)(3)(v)(A). The notification stated that the D.C. power supply for the Unit 1 High Pressure Coolant Injection (HPCI) system instrumentation failed resulting in the inability of HPCI to meet its requirement to support safely shutting down the reactor during a Station Blackout (SBO) (Complete Loss of A/C Power) situation. The Emergency Core Cooling System (ECCS) function of HPCI is still available with the alternate A/C power supply. A review of the station's current licensing basis determined that HPCI is not credited with a safety function during a Station Blackout (SBO) event. Operating procedures direct securing HPCI early in an SBO event to minimize the discharge rate on the Class 1E batteries. The Reactor Core Isolation Cooling (RCIC) system is credited with maintaining reactor inventory during a SBO event. HPCI remained capable of completing its safety function to inject coolant into the reactor pressure vessel during a loss of coolant accident (LOCA) concurrent with loss of offsite power (LOOP) event. The Division 2 automatic initiation logic was inoperable but the Division 4 automatic initiation logic was unaffected by the Division 2 instrument power supply failure. Division 2 instrument power is required for HPCI automatic flow control and would not have been initially available during a LOOP event. However, the Division 2 instrument power would have been restored when the 480 VAC load center is re-energized approximately 13 seconds into the event. The 13 second delay in HPCl injection is offset by existing margin in HPCI's capability to meet the Technical Specification response time of 60 seconds. Therefore, a condition did not exist at the time of discovery that could have prevented the fulfillment of the HPCI safety function. The licensee notified the NRC Resident Inspector. Notified R1DO (Bellamy).

ENS 439491 February 2008 05:45:00LimerickNRC Region 1GE-4Unit 2 automatically scrammed (at) 0445 as a result of an RPS actuation due to a turbine trip. All rods inserted. The plant is stable. No ECCS or SRV actuation occurred. This report is made pursuant to 50.72(B)(iv)(B). An investigation into the cause is currently in progress. Primary plant pressure is 900 psig. with the decay heat path to the condenser via turbine bypass valves. All safety related systems are operable, and the licensee is investigating a potential issue with the EHC system. The NRC Resident Inspector has been informed. The Commonwealth of Pennsylvania and local government agency will be informed. The licensee will issue a press release.
ENS 4399117 February 2008 08:31:00LimerickNRC Region 1GE-4

The Emergency Notification System (ENS), Health Physics Network (HPN), site commercial telephone lines and Emergency Response Data System (ERDS) have been taken out of service for a planned maintenance outage. The outage is scheduled for a duration of six hours. The plant radio system, plant page system, and Prelude phone system are unaffected by the maintenance. The licensee notified the NRC Resident Inspector.

* * * UPDATE AT 1534 ON 2/17/08 FROM NED DENNIN TO JEFF ROTTON * * * 

All phones are back in service and operable. The licensee will notify the NRC Resident Inspector. Notified R1DO (Dentel).

ENS 4408822 March 2008 20:50:00LimerickNRC Region 1GE-4Limerick Unit 1 automatically shutdown from a turbine trip at 1939 hrs on 03/22/08. The cause of the turbine trip is under investigation at this time. All control rods inserted as required. No ECCS (Emergency Core Cooling System) and no RCIC (Reactor Core Isolation Cooling) initiation occurred. No primary or secondary containment isolations were received. The plant is currently in Hot Shutdown maintaining normal reactor level with feedwater in service. Minimum water level after the scram was 5 inches. Level 3 had been reached however all level 3 isolation valves were already shut. No SRVs lifted after the scram. Decay heat is being removed by steam loads with the turbine bypass valves available if needed. The plant is in its normal shutdown electrical lineup. The licensee will issue a press release and has informed the NRC Resident Inspector.
ENS 4416925 April 2008 22:55:00LimerickNRC Region 1GE-4Limerick Generating Station experienced a loss of the Emergency Response Data System (ERDS), which provides real time plant data to the NRC Operations Center, from approximately 17:30 until 21:30 on 4/25/08. The plant monitoring system (PMS) and Safety Parameter Display System (SPDS) in the main control room were functional for the duration that ERDS was out of service, providing the Limerick Operators with all required data for monitoring the plant had an actual event occurred. In addition, all external phone lines were functioning to allow contact with the NRC Operations Center had an actual event occurred. The licensee notified the NRC Resident Inspector.
ENS 442603 June 2008 12:50:00LimerickNRC Region 1GE-4On Wednesday April 9, 2008 at 0416 hours, an invalid actuation of the 1B Refueling Floor Ventilation Exhaust Radiation Monitor occurred. The actuation caused a Division 2 Group 6C isolation signal, which caused primary containment isolation valves (PCIVs) to automatically close on the Containment Leak Detector Radiation Monitor (10-S182) and the Drywell Hydrogen/Oxygen Analyzer (10-S205). The 1A, 1C, and 1D channels were unaffected and indicated normal ventilation exhaust radiation levels during the event. The cause of the event was a failure of the K2 relay in the 1B Refueling Floor Ventilation Exhaust Radiation Monitor. The failed relay has been replaced and the radiation monitor was declared operable on Wednesday April 9, 2008 at 2024 hours. The portion of the primary containment isolation system that received an actuation signal functioned successfully. All of the affected open isolation valves automatically closed. The only equipment malfunction during the event was the failed K2 relay. The Division 2 Group 6C isolation was a partial actuation. This event is reportable per 10CFR50.73(a)(2)(iv)(A) since isolation valves for the Containment Leak Detector Radiation Monitor and Drywell Hydrogen/Oxygen Analyzer automatically closed due to an invalid signal. The licensee has notified the NRC Resident Inspector.
ENS 4428311 June 2008 00:59:00LimerickNRC Region 1GE-4

On June 10, 2008, at 2255 hours it was determined that 54 of the 165 Limerick Generating Station's Emergency Offsite Sirens were inoperable due to a loss of power. The loss was a result of heavy storms which passed through the area resulting in power outages throughout the region. Efforts are underway to restore power to the affected sirens. The licensee notified the NRC Resident Inspector

  • * * UPDATE FROM BRANDON SHULTZ TO HOWIE CROUCH AT 1709 EDT ON 6/11/08 * * *

On June 11, 2008 at 1645 restoration efforts have recovered 44 of the 54 sirens rendered inoperable by the storm. The remaining 10 inoperable sirens no longer represents a major loss of emergency preparedness capabilities. Restoration of power to the remaining inoperable sirens continues under normal prioritization and using routine siren operating and maintenance procedures. No completion time was provided concerning repair of the remaining sirens. The licensee will be notifying the NRC Resident Inspector. Notified R1DO (Summers).

ENS 446232 November 2008 20:33:00LimerickNRC Region 1GE-4The Unit 1 MCR (Main Control Room) HPCI (High Pressure Coolant Injection) flow indicator was observed oscillating just above zero gpm with periodic spikes to approximately 50% of scale (3000 gpm) with a concurrent drop in flow controller output signal while in standby. There were no activities in progress on or near the HPCI system when the oscillation and instrument spikes occurred. Walkdown of the instrument rack and HPCI room equipment found no abnormalities. The HPCI system was declared inoperable at 1550 hours 11/2/2008 (14 day Shutdown LCO). Troubleshooting is in progress to determine the cause of the flow oscillations. The HPCI system is considered available as there are no indications of controller failure that would impact operation in manual flow control mode. Unit 1 RCIC, and all other ECCS systems remain OPERABLE. The licensee will inform the NRC Resident Inspector.
ENS 4494329 March 2009 20:18:00LimerickNRC Region 1GE-4A worker performing U2 outage activities was exhibiting signs of heat stress and dizziness when exiting the U2 drywell access control point. Offsite medical assistance was requested and the worker was transported to the Pottstown Memorial Medical Facility as a potentially contaminated person. The ambulance left the site at 1825 hours 3-29-09. At 1845 hours while at the Pottstown Memorial Medical Facility it was determined that the worker was NOT contaminated. This report being submitted via the requirements of 10CFR50.72 (b)(3)(xii). The individual was performing routine valve operations and was a plant employee. The licensee notified the NRC Resident Inspector.
ENS 449481 April 2009 00:10:00LimerickNRC Region 1GE-4A valid actuation of the D23 Emergency Diesel Generator bus undervoltage minimum actuation logic occurred following manual operator action to mitigate a bus overvoltage condition during emergency diesel generator post maintenance testing . Due to the output breaker being opened, the D23 EDG experienced a undervoltage start signal. EDG undervoltage actuation instrumentation actuated, however, the EDG was in PTL (Pull-to-Lock) EDG shutdown. The event was caused by a failure of the emergency diesel generator voltage regulator most likely due to an intermittent failure of the #1 rectifier bank. The licensee stated that the D23 EDG was powering an isolated safety related bus for a post-maintenance test when the overvoltage condition occurred. The operator opened the EDG output breaker and placed the EDG in PTL. With the bus de-energized, a valid start signal was sent to EDG D23. However, EDG D23 did not actually start because it was in PTL. No safety related equipment was lost when the bus was de-energized because the bus had been unloaded prior to the test. The licensee has notified the NRC Resident Inspector.
ENS 4513316 June 2009 05:51:00LimerickNRC Region 1GE-4

(The licensee experienced) a loss of the ability to send ERDS data to the NRC for greater than 60 minutes due to a computer problem. The HPN and ENS communications systems were not affected and remained available through a commercial communication line. SPDS also remained in service and remained available during this period. The ERDS system was restored to service after 109 minutes. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 1240 EDT ON 06/22/09 FROM MARK ARNOSKY TO VINCE KLCO * * *

06-22-2009 Update to clarify the above statement: The HPN and ENS communications systems were affected by the computer problem, however, they remained available for use through an alternate and unaffected commercial communication line. Notified R1DO (Burritt).

ENS 4515323 June 2009 22:40:00LimerickNRC Region 1GE-4

A partial loss of the ability to send ERDS data to the NRC for greater than 60 minutes occurred. The loss affects transmission of Standby Liquid Control Tank levels, Main Condenser Vacuum levels, and data for North and South Ventilation Stacks and Drywall Post LOCA radiation monitors. The (Safety Parameter Display System) SPDS, (Health Physics Network) HPN and (Emergency Notification System) ENS systems are not affected. Troubleshooting to identify and correct the data loss to ERDS is in progress. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 0029 EDT ON 6/24/09 FROM SHULTZ TO HUFFMAN * * *

Data for North and South Ventilation Stacks and Drywell Post LOCA radiation monitors was restored to ERDS at 2345 hours on 6/23/09" The licensee will notify the NRC Resident Inspector.

  • * * UPDATE AT 1310 EDT ON 06/24/09 FROM MARK CHRISTOPHER TO S. SANDIN * * *

Data gathered from Standby Liquid Control and Main Condenser Vacuum is not plant data that is transmitted to ERDS. ERDS was fully restored with the required input data at 2345 hours on 6/23/2009. The licensee informed the NRC Resident Inspector. Notified R1DO (Henderson).

ENS 4530728 August 2009 01:13:00LimerickNRC Region 1GE-4

Non-conservative Tech Spec setpoints were discovered that affected Steam Leak Detection for Unit 1 and Unit 2 (High Pressure Coolant Injection) HPCI room high differential temperatures. During a steam leak detection system design basis leak, the present temperature setpoint would not isolate the HPCI steam supply piping. A calculation has been performed by engineering which demonstrates that, with both room coolers secured, a design basis steam leak will result in the room ventilation differential temperature exceeding the present Tech Spec setpoints. At this time, the room unit coolers have been secured and HPCI and the associated steam leak detection system remain operable. Calculations are in-progress by engineering for changes to the high differential temperature steam leak detection setpoint. The licensee notified the NRC Resident Inspector.

* * * RETRACTION FROM J. BROILET TO P. SNYDER ON 10/20/09 AT 1154 EDT * * * 

This is a retraction of the event notification made on 8/28/09 at 0113 EDT. This event (#45307) was initially reported as a condition that could have prevented fulfillment of a safety function under the requirement of 10 CFR 50.72 (b)(3)(v)(c). A follow-up review of the HPCI equipment room steam leak detection system calculations determined that other HPCI equipment room ambient high temperature instruments would have automatically actuated a HPCI steam line isolation during a 25 gpm design basis HPCI steam line leak event. Therefore, a condition did not exist at the time of discovery that could have prevented the fulfillment of the HPCI steam line isolation safety function. The licensee notified the NRC Resident Inspector. Notified R1DO (Doerflein).

ENS 4551824 November 2009 14:19:00LimerickNRC Region 1GE-4On Monday, October 19, 2009, Limerick Unit 1 was operating at 100% power. At 1105 hours, an invalid actuation of the 1B Reactor Enclosure Ventilation Exhaust Radiation Monitor occurred. The actuation caused a Division 2 Group 6C isolation signal, which caused primary containment isolation valves (PCIVs) to automatically close on the Containment Leak Detector Radiation Monitor (10-S182) and the Drywell Hydrogen/Oxygen Analyzer (10-S205). The 1A, 1C, and 1D channels were unaffected and indicated normal ventilation exhaust radiation levels during the event. The cause of the event was a failure of a fuse holder in the 1B Reactor Enclosure Ventilation Exhaust Radiation Monitor. The radiation monitor is designed to fail-safe on a loss of power. The automatic closure of the PCIVs placed them in their fail-safe position. The failed fuse holder has been replaced and the radiation monitor was declared operable on Tuesday, October 20, 2009 at 1348 hours. The portion of the primary containment isolation system that received an actuation signal functioned successfully. All of the affected open isolation valves automatically closed. The only equipment malfunction during the event was the failed fuse holder. The Division 2 Group 6C isolation was a partial actuation. This event is reportable per 10CFR50.73(a)(2)(iv)(A) since isolation valves for the Containment Leak Detector Radiation Monitor and Drywell Hydrogen/Oxygen Analyzer automatically closed due to an invalid signal. The licensee notified the NRC Resident Inspector.
ENS 4569311 February 2010 08:00:00LimerickNRC Region 1GE-4

On Thursday, February 11, 2010, the Limerick Technical Support Center (TSC) emergency ventilation system will be removed from service for planned preventative maintenance activities on the damper flow controller and air filtration charcoal system. During the maintenance, the non-emergency ventilation system will be functional. The TSC air filtration fan and dampers will be non-functional, rendering the TSC HVAC accident mode non-functional. This maintenance is scheduled to minimize out of service time. The planned TSC ventilation outage is scheduled to be completed within 12 hours. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing EP (Emergency Planning) procedures and checklists. If radiological conditions require TSC facility evacuation during ventilation system restoration, the Station Emergency Director will evacuate and relocate the TSC staff in accordance with applicable site procedures. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM BRANDON SHULTZ TO DONG PARK ON 2/11/10 AT 1721 EST * * *

The maintenance on the Limerick Technical Support Center (TSC) emergency ventilation system has been completed and the TSC is available. The licensee has notified the NRC Resident Inspector. Notified R1DO (Powell)

ENS 4596228 May 2010 14:53:00LimerickNRC Region 1GE-4On Friday April 2, 2010, Unit 1 refueling outage activities were in progress and the 1A RPS/UPS Static Inverter was being removed from service. At 2156 hours, the inverter static transfer switch was placed in 'Bypass' which transferred the load from the inverter to the secondary alternate source. The manual bypass switch was then placed in 'Bypass' which was followed by the RPS/UPS series breakers tripping on an overvoltage condition. The actuation caused a loss of power to the IA RPS/UPS power distribution panel loads which provides power to the Division 1A and IIA RPS relays and Division IA and IIA NS4 relays. This caused primary containment isolation valves (PCIVs) to automatically close on more than one system. The IB and IIB channels were unaffected. Troubleshooting determined that the secondary, alternate source voltage was 132 VAC which exceeded the overvoltage setpoint of 126 VAC. During outages, the 13kV bus voltages are higher than on-line voltages due to low operating equipment loading on the buses. The secondary alternate source to the inverter is not regulated which can result in greater than normal voltage to the RPS/UPS loads. The portion of the primary containment isolation system that received an actuation signal functioned successfully. All of the affected open isolation valves automatically closed. The isolation was a partial actuation. This 60-day ENS report is being made per 10CFR 50.73(a)(2)(iv)(A) and 10CFR 50.73(a)(1) to report invalid automatic actuation of systems listed in paragraph (a)(2)(iv)(B). The listed system that actuated was general containment isolation signals affecting containment isolation valves in more than one system. Primary containment isolation valves (PCIVs) closed on drywell chilled water (DWCW), reactor enclosure cooling water (RECW), primary containment instrument gas (PCIG), and suppression pool cleanup. The licensee notified the NRC Resident Inspector.
ENS 4600513 June 2010 15:00:00LimerickNRC Region 1GE-4

On June 14, 2010 at 0300 hours, Limerick Generating Station will apply a clearance to inspect and repair Fire Suppression Equipment associated with the Onsite Technical Support Center (TSC) Emergency Ventilation System and perform corrective maintenance associated with MD-1 (Outside Air Damper). During the time that the clearance is applied, the TSC Ventilation System will not be available to be restored in a time period required to staff and activate the TSC Emergency Response Organization. This work is expected to be completed on June 16, 2010. If an emergency is declared requiring TSC activation, the TSC will be staffed and activated using emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature. Radiological or other conditions. If relocation becomes necessary, the Station Emergency Director will relocate the TSC staff to an alternate TSC location in accordance with applicable Site procedures. This notification is being made in accordance with 10CFR50.72(b)(3)(xiii) due to the Loss of an Emergency Response Facility (ERF) because of the Unavailability of the Emergency Ventilation System. The NRC Resident Inspector has been informed.

  • * * UPDATE FROM BROILLET TO HUFFMAN AT 2206 EDT ON 6/14/10 * * *

The TSC Emergency Ventilation System was returned to service at 2150 EDT on 6/14/10. The licensee has informed the NRC Resident Inspector. R1DO (Holody) notified.

ENS 4604223 June 2010 23:57:00LimerickNRC Region 1GE-4Limerick Unit 1 was manually scrammed from 100% power on 6/23/10 at 2051 hours in accordance with plant procedure OT-112 'Recirculation Pump Trip' when both 1A and 1B recirc pump MG set drive motor breakers were observed to have tripped, resulting in a loss of both reactor recirculation pumps. Preliminary indication is a loss of power to 114A Load Center, caused by 'A' phase overcurrent trip of 13.2 KV feeder breaker (11-BUS-07) to the 114A Transformer and Load Center. The cause of the MG set drive motor breaker trips is under investigation at this time. All Control Rods inserted as required. No ECCS or RCIC initiations occurred. No Primary or Secondary Containment Isolations were received. The plant is currently in Hot Shutdown maintaining normal reactor level with feedwater in service. All systems functioned as required during the transient. The manual scram was characterized as uncomplicated. No PORVs or Safety Relief valves lifted during the transient. Decay heat is being discharged to the condenser via turbine bypass valves. The unit is in a normal shutdown electrical lineup and there was no impact on Unit 2. The electrical supplies for the recirc pump MG sets has been walked down by the licensee and no indication of any damage or electrical faults has been found at this time. The NRC Resident Inspector has been notified and the licensee indicated a media or press release will be made.
ENS 4629029 September 2010 20:04:00LimerickNRC Region 1GE-4During quarterly testing of the Technical Support Center (TSC) HVAC System, Emergency Damper MD-1 failed to fully close when the system was placed into the Emergency mode of operation. This damper being not fully closed allows outside air to bypass the filter train and renders the Emergency mode of operation unavailable. At 1725 the Emergency Damper MD-1 was failed to the closed position which makes the Emergency mode of the TSC HVAC system available. Troubleshooting and restoration of Emergency Damper MD-1 will continue on dayshift 9/30/2010. The licensee has notified the NRC Resident Inspector.
ENS 4633013 October 2010 09:50:00LimerickNRC Region 1GE-4

This ENS is being issued in advance of a planned activity. On 10/14/10 at 0100 hours Limerick Generating Station will apply a clearance to inspect and repair fire suppression equipment associated with the onsite Technical Support Center (TSC) Emergency Ventilation System and perform corrective maintenance associated with the MD-1 (outside air) damper. While the clearance is applied, the TSC Emergency Ventilation system will not be available to be restored within the time period required to staff and activate the TSC Emergency Response Organization (ERO). This work is expected to be completed 10/14/10. If an emergency is declared requiring TSC ERO activation, the TSC will be staffed and activated using emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature, radiological, or other conditions. If relocation of TSC staff becomes necessary, the Station Emergency Director will relocate the staff to an alternate TSC location in accordance with applicable procedures. This notification is being made in accordance with 10CFR50.72(b)(3)(xiii) due to the loss of an Emergency Response Facility because of the planned unavailability of the TSC Emergency Ventilation system. The NRC Resident Inspector has been informed.

  • * * UPDATE FROM JOHN WEISSINGER TO HOWIE CROUCH AT 1833 EDT ON 10/14/10 * * *

The Technical Support Center Emergency Ventilation System maintenance is complete and the system has been returned to service. The licensee has notified the NRC Resident Inspector. Notified R1DO (Jackson).