05000267/LER-1979-055-03, /03X-1: on 791026,during Scheduled Surveillance Testing,Check Valve V-22370 Was Found to Be Stuck Open. Cause Not Identified.Valve Was Opened & Inspected,Then Cleaned & Lubricated

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/03X-1: on 791026,during Scheduled Surveillance Testing,Check Valve V-22370 Was Found to Be Stuck Open. Cause Not Identified.Valve Was Opened & Inspected,Then Cleaned & Lubricated
ML19323D016
Person / Time
Site: Fort Saint Vrain 
Issue date: 05/09/1980
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19323D010 List:
References
LER-79-055-03X-01, LER-79-55-3X-1, NUDOCS 8005190537
Download: ML19323D016 (1)


LER-1979-055, /03X-1: on 791026,during Scheduled Surveillance Testing,Check Valve V-22370 Was Found to Be Stuck Open. Cause Not Identified.Valve Was Opened & Inspected,Then Cleaned & Lubricated
Event date:
Report date:
2671979055R03 - NRC Website

text

NT.C FORM 366 U.S. NUCLEAR REGULATbRY COMMISSION 87 77)

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LICENSEE EVENT REPORT CONTROL BLOCK: l l

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PRCBABLE CONSEQUENCES h lol2l l During scheduled surveillance testing, a check valve (V-22370) was found to be stuck

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l o 13 l lopen. This event degraded the firewater booster pumos for helium circulator drive.

I I o I.: I l The reactor had been operated at power since the last demonstrated operability of the l l

Io!sl l booster pumps. LCO 4.2.19 recuires that one booster pump be ooerable when the reactor l 1

I o 16 I l is at power.

It must be assumed that the reactor was coerated at oower with degraded I 10171 l boos te r pucos.

There was no ef fect uoon the health or safety of the public.

Re-l l o i a I l dundant systems were available.

Reportable per Technical Soecification AC 7.5.2(b)2. I 7

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CODE SUSC E COMPONENT CODE SUSC DE SU E

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h I i I a l l The cause of the valve malfunction was not identified.

At the time of the event, the l l

m Ivalve was rapped sharoly which freed it for operation.

The valve was ocened and in-I 1il2l lspected, but no specific cause for sticking was found. The valve and shaf t were l

l l1l l cleaned and lubricated. The valve is a Walworth 4 inch check valve, body Model WO8 l

1iI4 i Iwith a R13 disc.

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%PCWER CTHER STATUS 315 O RY DISCOVERY CESCRIPTICN l1 l 5 l l G l@ l0 l 0 l0 l@lN/A l

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ACTIVITY CO TENT

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^P RELEASE AMCUNT OF ACTIVITY LOCATION CP RELEASE li l6 l l Z j h lZ lgl N/A l

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7 3 9 to 11 44 45 80 PERSCNNEL EXPCSURES NUMBER TYPE D ESCRIPTION l i l 71 10101 O l@l Z l@l N/A l

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NUVeER CESCRIPTICN lt la l l 0 l 0 l 0 l@l N/A l

7 8 9 11 12 80 LOSS OF CR DAMAGE TO FACILITY TY8E OESCRIPTION li 191 l Z l@l N/A l

7 d 9 10 80 NRC USE CNLY ISSUE DE CRIPTION 1:101 l N @l N/A I

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