LER-1979-024, Forwards LER 79-024/03L-0 |
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FT public service company o f c cil e n d e
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P. O. Box 361, Platteville, Colorado 80651 i
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August 31, 1979 Fort S t. Vrain Unit No. 1 P-79195 Mr. Karl V. S eyf rit, Director Nuclear Regulatory Cocmission Region IV Office of Inspection and Enforcement 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76012 REF: Facility Operacing License No. DPR-34 Docket No. 50-267
Dear Mr. Seyfrit:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/79-24/03-L-0, Final, submitted per the requirem.nts o f Technical Specification AC 7.5.2(b)2.
Also, please find enclosed one copy or the Licensee Event Report for Reportable Occurrence Report No. 50-267/79-24/03-L-0.
Very truly yours, Wwu Don Warembou&
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Manager, Nuclear Production DW/alk cc:
Director, MIPC Y
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REPORT DATE:
August 31, 1979 REPORTABLE OCCURRENCE 79-24 ISSUE O OCCURRENCE DATE:
Augus t 4, 19 79 Page 1 of 6 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO P. O. BOX 361 PLAITEVILLE, COLORADO 80651 REPORT NO. 50-267/ 79-24 /03-L-0 Final Ic2NTIFICATION OF OCCURRENCE :
On three occasions during the period from August 4,1979, through Augus t 16, 1979, total primary coolant oxidants (the sum of water, carbon monoxide, and carbon dioxide) exceeded 10 parts per million with core average outlet tem-perature greater than 1,200*F.
This constitutes operation in a degraded mode permitted by LCO 4.2.10 and is reportable per Technical Specification ~ AC 7.5.2(b)2.
EVENT DESCRIPTION
At about 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br /> on August 4,1979, with the reactor operating at approxi-mately 452' power and total pri=ary coolant oxidants at approxicately 11.8 ppm, core average outlet temperature exceeded 1,200*
for the first time since the refueling shutdown (referenc Figure 1, point 1 ).
Following an initial increase, (Figure 1, point 2 ) oxidant levels appeared to be following a decreasing trend antil approximately 1745 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.639725e-4 months <br /> on August 6,1979. Since as
=uch moisture as possible had been removed at existing plant conditions, reac-tor power was increased to approximately 60% to f acilitate additional " drying out" operations. At that time, it was observed that carbon monoxide indica-tions were on the increase.
At 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br /> on August 7,1979, it was observed that primary coolant carbon dioxide levels were also increasing. At this point, it was determined that 4
the "A" helium purification dryer had apparently broken through. Maximum oxi-dant concentration of 51.5 ppm was reached at approximately 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> ich average core outlet temperature of 1,300*F (reference Figure 1, point
).
Operation continued at approximately 65 power and 1,340*F core outlet tem-perature, and primary coolant oxidant levels followed a generally decreasing trend as the increased temperatures allowed the moisture to outgas f rom the graphite in the core.
REPORTABLE OCCURRENCE 79-24 ISSUF 0 Page 2 of 6 EVENT DESCRIPTION (continued) :
Due to a circulator trip on August 11, 1979, t =peratures were decreased to less than 1,200*F (reference Figure 1, point 4 ).
With the subsequent rise in power later that same day, temperatures were again increased to greater than 1,200*F, while oxidant levels continued their decreasing trend. At 1937 hours0.0224 days <br />0.538 hours <br />0.0032 weeks <br />7.370285e-4 months <br /> on August 11, 1979, the reactor scrammed, a d temperatues again decreased to less than 1,200*F (reference Figure 1, Point 5
).
Oxidant levels con-tinued to decrease until a subsequent increase in temperature on August 13, 1979, resulted in LCO 4.2.10 limits again being exceeded at approxi=ately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on August 13,1979 (reference Figure 1, point (f) ).
At 0040 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> on August 16, 1979, a circulator trip occurred.
Reactor power and temperature w re decreased to allow recovery of the circulator (reference Figure 1, point 7
).
Following this occurrence, no further degraded mode operation of LCO 4.2.10 occurred.
CAUSE
DESCRIPTION :
It is assumed that the continued level of oxidants in the primary coolant follcwing regeneration of the purification train was a result of off-gassing due to a previous buf fer helium dryer bypass which resulted in water ingress to the cote.
As temperatures increase, the water reacts with the graphite in the core to form carbon monoxide and carbon dioxide. During the period covered by this report there were no significant changes in the moisture concentrations ob-served in the primary coolant, so the increased oxidant levels are attributed to the reaction b-. ween the water and graphite as a result of efforts to dry out the core following an extended refueling shutdown and the previously men-tioned dryer bypass.
CO RRECTIVE ACTION:
4 "B" purification train was placed in service in an attempt to keep the total primary coolant oxidant levels from increasing, and the "A" purification train which had broken through was regenerated.
Dr"ing out operations were continued with consideration to the limits allowed per LCO 4.2.10.
Decreases in te=perature due to periodic circulator trips and reactor scrams precluded any necessity for planned temperature decreases.
REPORTABLE OCCURRENCE 79-24 ISSUE O Page 3 of 6 CORRECTIVE ACTION (continued) :
Following the return to a core average outlet te=perature greater than 1,200*F on Augus t 16, 1979, no further degraded mode operation per LCO 4.2.10 was ob-served.
No further corrective action is anticipated or required.
L-
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ISSUE 0 Page 4 of 6 E
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FIGURE 1 4-; '
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REPORTABLE OCCURRENCE 79-24 ISSUE 0 Page 6 of 6 Prepared by:
M, n d
Cathy y Collard Technical Services Technician Reviewed by:
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'J. W. Gahm Technical Services Supervisor Reviewed by:
Frank M. Mathie Operations Manager Approved by:
775u,_ Ls_
Don Ware = bourg g
Manager, Nuclear Production 4
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| 05000267/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000267/LER-1979-001-03, /03L-0 on 790102:total Primary Coolant Oxidant Concentration Exceeded 10 Vol Ppm While Core Average Outlet Temp Was Greater than 1200 F.Caused by Low Temp Absorber Heatup,Releasing Oxidant to Primary Coolant | /03L-0 on 790102:total Primary Coolant Oxidant Concentration Exceeded 10 Vol Ppm While Core Average Outlet Temp Was Greater than 1200 F.Caused by Low Temp Absorber Heatup,Releasing Oxidant to Primary Coolant | | | 05000267/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000267/LER-1979-002-03, /03L-0 on 790127:operation in Degraded Mode Resulted from Repairs to Seat of Buffer Helium Purge Valve. Bypass of Buffer Helium Dryer Caused by Leakage Past Valve Seat Insert of Velan Model P-33876-N/78R Valve | /03L-0 on 790127:operation in Degraded Mode Resulted from Repairs to Seat of Buffer Helium Purge Valve. Bypass of Buffer Helium Dryer Caused by Leakage Past Valve Seat Insert of Velan Model P-33876-N/78R Valve | | | 05000267/LER-1979-004-03, /03L-0 on 790203:during Normal Operation,Cooling Tower Blowdown Exceeded Limit But Was Not Reported.Caused by Incorrect Completion of Surveillance Forms.Forms Changed & Personnel Instructed | /03L-0 on 790203:during Normal Operation,Cooling Tower Blowdown Exceeded Limit But Was Not Reported.Caused by Incorrect Completion of Surveillance Forms.Forms Changed & Personnel Instructed | | | 05000267/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000267/LER-1979-005-03, /03L-0 on 790209:during Semiannual Loss of Outside Electrical Power Test,Output Circuit Breaker Did Not Close.Cause Unknown.Breaker Replaced W/Equivalent Spare | /03L-0 on 790209:during Semiannual Loss of Outside Electrical Power Test,Output Circuit Breaker Did Not Close.Cause Unknown.Breaker Replaced W/Equivalent Spare | | | 05000267/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000267/LER-1979-013, Forwards RO 50-267/79-13/03-L-O & LER 79-013/03L-0 | Forwards RO 50-267/79-13/03-L-O & LER 79-013/03L-0 | | | 05000267/LER-1979-013-03, /03L-0 on 790412:during Test of Snubbers Many Found Inoperable Due to Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Snubbers Repaired & Adjusted | /03L-0 on 790412:during Test of Snubbers Many Found Inoperable Due to Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Snubbers Repaired & Adjusted | | | 05000267/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000267/LER-1979-015-03, /03L-0 on 790507:during Routine Surveillance Testing,Setpoint of Pcrv Rupture Disc M-11702 Found to Be 826 Psig.Caused by Calibr Drift.Disc Recalbr | /03L-0 on 790507:during Routine Surveillance Testing,Setpoint of Pcrv Rupture Disc M-11702 Found to Be 826 Psig.Caused by Calibr Drift.Disc Recalbr | | | 05000267/LER-1979-016, Forwards LER 79-016/01T-0 | Forwards LER 79-016/01T-0 | | | 05000267/LER-1979-016-01, /01T-0 on 790521:punch Gap of Pcrv Rupture Disc M-11702 Found Out of Tolerance W/Vendor Specs.Caused by Undocumented Change of Punch Gap Specs.Tolerances Returned to Original Specs | /01T-0 on 790521:punch Gap of Pcrv Rupture Disc M-11702 Found Out of Tolerance W/Vendor Specs.Caused by Undocumented Change of Punch Gap Specs.Tolerances Returned to Original Specs | | | 05000267/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000267/LER-1979-017-01, /01T-0 on 790626:fault Current Trip Occurred, Causing Reactor Scram & Interrupted Reactor Cooling.Caused by Water Spray in Switchgear,Resulting in Short Circuit Due to Voltage Perturbation | /01T-0 on 790626:fault Current Trip Occurred, Causing Reactor Scram & Interrupted Reactor Cooling.Caused by Water Spray in Switchgear,Resulting in Short Circuit Due to Voltage Perturbation | | | 05000267/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000267/LER-1979-018-03, /03L-0 on 790630:one motor-operated Butterfly Valve Found Inoperable by Remote Manual Control.Cause Is Unknown.Cause & Corrective Action to Be Reported in Future Suppl | /03L-0 on 790630:one motor-operated Butterfly Valve Found Inoperable by Remote Manual Control.Cause Is Unknown.Cause & Corrective Action to Be Reported in Future Suppl | | | 05000267/LER-1979-019-03, /03L-0 on 790711:during Normal Operation,Weekly Functional Test of Area Radiation Monitors Not Performed for 1 Wk.Caused by Misfiling of Card for Surveillance Test. Computer Readout Will Be Used as Cross Check on Card Sys | /03L-0 on 790711:during Normal Operation,Weekly Functional Test of Area Radiation Monitors Not Performed for 1 Wk.Caused by Misfiling of Card for Surveillance Test. Computer Readout Will Be Used as Cross Check on Card Sys | | | 05000267/LER-1979-020-03, /03L-0 on 790717:during Normal Plant Operation, Engine Failed to Start.Caused by Failure of Emergency Diesel Temp Switch C.Switch Replaced | /03L-0 on 790717:during Normal Plant Operation, Engine Failed to Start.Caused by Failure of Emergency Diesel Temp Switch C.Switch Replaced | | | 05000267/LER-1979-021-03, /03L-1 on 790720:during Review of Surveillance Tests,Discovered That Halon Fire Suppression Sys Surveillance Test for Second Quarter Not Performed.Caused by Inadequate Control & Direction Re Refueling Work Load | /03L-1 on 790720:during Review of Surveillance Tests,Discovered That Halon Fire Suppression Sys Surveillance Test for Second Quarter Not Performed.Caused by Inadequate Control & Direction Re Refueling Work Load | | | 05000267/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000267/LER-1979-022-03, /03L-0 on 790720:lack of Aquatic Macroinvertebrate Sample Collection.Caused by Oversight of Field Sampling Personnel Employed by Contract Agent.Agent Indicated Program Was Resumed & Will Continue Biweekly | /03L-0 on 790720:lack of Aquatic Macroinvertebrate Sample Collection.Caused by Oversight of Field Sampling Personnel Employed by Contract Agent.Agent Indicated Program Was Resumed & Will Continue Biweekly | | | 05000267/LER-1979-023-03, /03L-0 on 790727:while Performing Normal Surveillance,Fixed Feedwater Low Flow Switch Found Inoperable. Caused by Component Failure from Normal Wear. Module Was Repaired,Reinstalled & Retested Satisfactorily | /03L-0 on 790727:while Performing Normal Surveillance,Fixed Feedwater Low Flow Switch Found Inoperable. Caused by Component Failure from Normal Wear. Module Was Repaired,Reinstalled & Retested Satisfactorily | | | 05000267/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000267/LER-1979-024-03, /03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core | /03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core | | | 05000267/LER-1979-025-03, /03X-0:on 790806,during Steady State Operation at 45% Thermal Power,Emergency Diesel Generator a Found in Degraded Mode, & B Engine Also Declutched.Caused by Relay Failure Due to Normal End of Life.Relay Replaced | /03X-0:on 790806,during Steady State Operation at 45% Thermal Power,Emergency Diesel Generator a Found in Degraded Mode, & B Engine Also Declutched.Caused by Relay Failure Due to Normal End of Life.Relay Replaced | | | 05000267/LER-1979-026-03, /03L-0:on 790807,bearing Water Makeup Pump P-2105 Removed from Svc to Perform Line Repair W/Reactor at 65% Power.Caused by Hole in Recirculation Line of Pump,Requiring Removal from Svc.Line Repaired.Pump Returned to Svc | /03L-0:on 790807,bearing Water Makeup Pump P-2105 Removed from Svc to Perform Line Repair W/Reactor at 65% Power.Caused by Hole in Recirculation Line of Pump,Requiring Removal from Svc.Line Repaired.Pump Returned to Svc | | | 05000267/LER-1979-027-01, /01T-0:on 790817,noted That Recent Pipe Hanger Installation Power Operated Relief Valve Cooling Water Lines Would Have Prevented Proper Installation of Pipe Spools. Caused by Pipe Ends Changing Alignment | /01T-0:on 790817,noted That Recent Pipe Hanger Installation Power Operated Relief Valve Cooling Water Lines Would Have Prevented Proper Installation of Pipe Spools. Caused by Pipe Ends Changing Alignment | | | 05000267/LER-1979-028-01, Plant Personnel Inadvertently Grounded Instrument Panel I-36,blowing Panel Fuses & Causing Voltage Perturbation on Bus 2.Caused by Personnel Error.Ground Corrected | Plant Personnel Inadvertently Grounded Instrument Panel I-36,blowing Panel Fuses & Causing Voltage Perturbation on Bus 2.Caused by Personnel Error.Ground Corrected | | | 05000267/LER-1979-029-03, /03L-0:on 790819,during Plant Startup,B Instrument Air Compressor Became Inoperable.Caused by Failure of Discharge Feather Valve.All Discharge Valves on Compressor Replaced & C Air Compressor Returned to Svc | /03L-0:on 790819,during Plant Startup,B Instrument Air Compressor Became Inoperable.Caused by Failure of Discharge Feather Valve.All Discharge Valves on Compressor Replaced & C Air Compressor Returned to Svc | | | 05000267/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000267/LER-1979-030, Forwards LER 79-030/03L-0 | Forwards LER 79-030/03L-0 | | | 05000267/LER-1979-030-03, /03L-0:on 790821,primary Coolant Oxidants Exceeded Limiting Condition for Operation.Caused by Offline Helium Dryer Drying Out Operations & Extended Regeneration Period. Core Outlet Temps Reduced Whenever Oxidant Limits Excee | /03L-0:on 790821,primary Coolant Oxidants Exceeded Limiting Condition for Operation.Caused by Offline Helium Dryer Drying Out Operations & Extended Regeneration Period. Core Outlet Temps Reduced Whenever Oxidant Limits Exceeded | | | 05000267/LER-1979-031-03, /03L-0:on 790821 & 0830,plant Operated W/Reactor Dewpoint Outside Tech Spec Limits.Caused by Helium Dryer Bypass,Due to Faulty Time Delay Relay.No Cause for 790821 Event.Relay Replaced & Tested | /03L-0:on 790821 & 0830,plant Operated W/Reactor Dewpoint Outside Tech Spec Limits.Caused by Helium Dryer Bypass,Due to Faulty Time Delay Relay.No Cause for 790821 Event.Relay Replaced & Tested | | | 05000267/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000267/LER-1979-032, Forwards LER 79-032/03X-1 | Forwards LER 79-032/03X-1 | | | 05000267/LER-1979-032-03, During Testing,Four of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Would Not Trip.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Testing,Four of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Would Not Trip.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1979-033, Forwards LER 79-033/03L-0 | Forwards LER 79-033/03L-0 | | | 05000267/LER-1979-033-03, /03L-0:on 790828,unauthorized Release Made from 1A Gas Waste Surge Tank.Caused by Wrong Valve Lineup.Valve Checkoff Sheets Revised to Require Operator Initials for Each Valve.Personnel Admonished | /03L-0:on 790828,unauthorized Release Made from 1A Gas Waste Surge Tank.Caused by Wrong Valve Lineup.Valve Checkoff Sheets Revised to Require Operator Initials for Each Valve.Personnel Admonished | | | 05000267/LER-1979-034-03, /03L-0:on 790830,while Operating at 36% Thermal Power,Emergency Diesel Generator Day Tanks Did Not Have 500 Gallons of Fuel Oil as Required Per Tech Specs.Caused by Inoperable High Level Switch Which Controls Pump Operations | /03L-0:on 790830,while Operating at 36% Thermal Power,Emergency Diesel Generator Day Tanks Did Not Have 500 Gallons of Fuel Oil as Required Per Tech Specs.Caused by Inoperable High Level Switch Which Controls Pump Operations | | | 05000267/LER-1979-034, Forwards LER 79-034/03L-0 | Forwards LER 79-034/03L-0 | | | 05000267/LER-1979-035-01, /01X-1:on 790831,field Audit & Preliminary Engineering Analysis of Random Sample of as-built safety-related Piping Drawings Showed Several Hangers W/Inconsistencies.Caused by Design Inconsistencies | /01X-1:on 790831,field Audit & Preliminary Engineering Analysis of Random Sample of as-built safety-related Piping Drawings Showed Several Hangers W/Inconsistencies.Caused by Design Inconsistencies | | | 05000267/LER-1979-036-03, /03L-0:on 790910,cold Reheat Snubber CRS-262 Inoperable W/Reactor in Shutdown Condition.Caused by Missing Pin That Kept Snubber from Being Properly Attached to Pipe. New Pin Fabricated & Installed.Snubber Returned to Svc | /03L-0:on 790910,cold Reheat Snubber CRS-262 Inoperable W/Reactor in Shutdown Condition.Caused by Missing Pin That Kept Snubber from Being Properly Attached to Pipe. New Pin Fabricated & Installed.Snubber Returned to Svc | | | 05000267/LER-1979-037, Forwards LER 79-037/03L-0 | Forwards LER 79-037/03L-0 | | | 05000267/LER-1979-037-03, /03L-0:on 790919,during Normal Operation,Liquid Radwaste Release Was Made in Noncompliance W/Limiting Conditions for Operation.Caused by Operator Failure to Reset Flow Switch to New Required Flow Rate.Operators Admonished | /03L-0:on 790919,during Normal Operation,Liquid Radwaste Release Was Made in Noncompliance W/Limiting Conditions for Operation.Caused by Operator Failure to Reset Flow Switch to New Required Flow Rate.Operators Admonished | | | 05000267/LER-1979-038-03, /03L-0:on 790921,analytical Sys Primary Coolant Moisture Monitor ME-9307 Became Inoperable W/Reactor at Less than 2% Power.Caused by Burned Out Thermal Electric Heater/Cooler & Two Faulty Relays.Head & Relays Replaced | /03L-0:on 790921,analytical Sys Primary Coolant Moisture Monitor ME-9307 Became Inoperable W/Reactor at Less than 2% Power.Caused by Burned Out Thermal Electric Heater/Cooler & Two Faulty Relays.Head & Relays Replaced | | | 05000267/LER-1979-038, Forwards LER 79-038/03L-0 | Forwards LER 79-038/03L-0 | | | 05000267/LER-1979-039-03, /03L-0:on 790924,authorized Liquid Waste Release Was Made,Requiring Raising Setpoints on Liquid Waste Activity Monitors Above Normal.Caused by Failure to Return Monitors to Normal Setpoints Prior to Starting Release | /03L-0:on 790924,authorized Liquid Waste Release Was Made,Requiring Raising Setpoints on Liquid Waste Activity Monitors Above Normal.Caused by Failure to Return Monitors to Normal Setpoints Prior to Starting Release | | | 05000267/LER-1979-040-03, Ler 79-040/03L-0:on 791001,two Snubbers Required During Power Operation Found Inoperable.Caused by Oil Reservoir Leak in HRS-194 & Loose Lock Nut on HOS-29.Reservoir Refilled & Lock Nut Tightened | Ler 79-040/03L-0:on 791001,two Snubbers Required During Power Operation Found Inoperable.Caused by Oil Reservoir Leak in HRS-194 & Loose Lock Nut on HOS-29.Reservoir Refilled & Lock Nut Tightened | |
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