ENS 42950
ENS Event | |
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12:45 Oct 31, 2006 | |
Title | Reactor Trip From Turbine Trip On Low Auto Stop Oil Pressure |
Event Description | Reactor trip at 0445 following a turbine trip. Initial indication of cause is turbine trip due to low auto stop oil pressure. There were no complications in plant response. Plant is stabilized in mode three, heat removal is being maintained by turbine bypass valves.
All control rods fully inserted on the trip, no safety or relief valves lifted during the transient, reactor water level 3 isolations did isolate, and the minimum level attained during the transient was -6 inches. Vessel water level is being maintained with normal feedwater flow and the electrical lineup is the normal shut-down electrical lineup. The cause of the low auto stop oil pressure is under investigation. The licensee notified the NRC Resident Inspector.
In response to questions raised during this event notification, a verbal response was provided to the NRC that an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> notification in accordance with 50.72(b)(3)(iv)(A) [Specified System Actuation] was required. Upon further review it has been determined by Energy Northwest that this notification was not required because all required reporting was satisfied by 50.72(b)(2)(iv)(B). The licensee will notify the NRC Resident Inspector. Notified R4 DO (D. POWERS) |
Where | |
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Columbia Generating Station Washington (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
LER: | 05000397/LER-2006-001 |
Time - Person (Reporting Time:+-2.68 h-0.112 days <br />-0.016 weeks <br />-0.00367 months <br />) | |
Opened: | Don Gregoire 10:04 Oct 31, 2006 |
NRC Officer: | Mark Abramovitz |
Last Updated: | Oct 31, 2006 |
42950 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Shutdown (0 %) |
WEEKMONTHYEARENS 534102018-05-18T13:51:00018 May 2018 13:51:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Caused by Main Transformer Trip ENS 529182017-08-20T23:05:00020 August 2017 23:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to a Rise in Main Condenser Back Pressure ENS 524422016-12-18T19:24:00018 December 2016 19:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Scram Due to Load Reject from Substation ENS 518262016-03-28T20:22:00028 March 2016 20:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Scram Following Loss of Reactor Closed Cooling ENS 454842009-11-07T15:25:0007 November 2009 15:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to a Main Turbine Digital Electro-Hydraulic Control System Leak ENS 452452009-08-05T14:50:0005 August 2009 14:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Toxic Gas from a Switchgear Fire in the Turbine Building ENS 451692009-06-27T03:05:00027 June 2009 03:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Based on Fire Lasting Greater than 15 Minutes ENS 450512009-05-08T17:45:0008 May 2009 17:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram After Loss of Generator Seal Oil ENS 448392009-02-08T19:25:0008 February 2009 19:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Due to a Governor Valve Fast Closure Signal ENS 444322008-08-21T23:06:00021 August 2008 23:06:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Due to a Main Turbine Trip ENS 434572007-06-29T00:17:00029 June 2007 00:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Condensate Pump Trip ENS 429502006-10-31T12:45:00031 October 2006 12:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip from Turbine Trip on Low Auto Stop Oil Pressure ENS 417902005-06-23T20:46:00023 June 2005 20:46:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit Experienced an Automatic Reactor Scram Due to a Loss of Feedwater Flow ENS 417792005-06-15T21:00:00015 June 2005 21:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Turbine Throttle Valve Closure ENS 409642004-08-17T12:28:00017 August 2004 12:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Trip of Reactor Feedwater Pump "a" on Low Suction Pressure. ENS 409592004-08-15T20:03:00015 August 2004 20:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Reactor Feedwater Pump Trip ENS 409102004-07-30T17:00:00030 July 2004 17:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Alert Declared at Columbia Generating Station 2018-05-18T13:51:00 | |