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Category:NRC Preliminary Notification of Event/Occurrence
MONTHYEARPNO-III-23-002B, Prairie Island Update to PNO-III-23-002 Declaration of an Unusual Event Following a Turbine Generator and Reactor Trip Due to Fault on Unit 2 Generator Main Transformer2023-06-0808 June 2023 PNO-III-23-002B Prairie Island Update to PNO-III-23-002 Declaration of an Unusual Event Following a Turbine Generator and Reactor Trip Due to Fault on Unit 2 Generator Main Transformer PNO-III-23-002, Prairie Island Nuclear Power Station Declaration of an Unusual Event Following a Turbine Generator and Reactor Trip Due to Fault on Unit 2 Generator Main Transformer2023-06-0101 June 2023 PNO-III-23-002 - Prairie Island Nuclear Power Station Declaration of an Unusual Event Following a Turbine Generator and Reactor Trip Due to Fault on Unit 2 Generator Main Transformer PNO-III-15-011, Prairie Island Nuclear Plant: Shutdown of Unit 2 and Notice of Unusual Event2015-12-18018 December 2015 PNO-III-15-011 - Prairie Island Nuclear Plant: Shutdown of Unit 2 and Notice of Unusual Event PNO-III-15-008, Prairie Island Unit 2 Shutdown Due to Trip of Main Power Turbine2015-06-0909 June 2015 PNO-III-15-008: Prairie Island Unit 2 Shutdown Due to Trip of Main Power Turbine PNO-III-15-003, A: Update: Shutdown of Prairie Island Unit 2 Due to Loss of Instrument Air to Containment Building2015-03-26026 March 2015 PNO-III-15-003A: Update: Shutdown of Prairie Island Unit 2 Due to Loss of Instrument Air to Containment Building ML15069A1852015-03-10010 March 2015 PNO-III-15-003 Prairie Island Nuclear Plant: Shutdown of Prairie Island Unit 2 Due to Loss of Instrument Air to Containment Building and Notification of Unusual Event PNO-III-15-001, A: Update: Shutdown of Prairie Island Unit 1 Due to Increasing Trend in Reactor Coolant System Leakage2015-02-17017 February 2015 PNO-III-15-001A: Update: Shutdown of Prairie Island Unit 1 Due to Increasing Trend in Reactor Coolant System Leakage ML15028A0232015-01-27027 January 2015 PNO-III-15-001 - Shutdown of Prairie Island Unit 1 Due to Increasing Trend in Reactor Coolant System Leakage PNO-III-14-012, A Update: Shutdown of Prairie Island Unit 1 Due to Increasing Trend in Reactor Coolant System Leakage2014-12-29029 December 2014 PNO-III-14-012A Update: Shutdown of Prairie Island Unit 1 Due to Increasing Trend in Reactor Coolant System Leakage ML14346A4682014-12-12012 December 2014 PNO-III-14-012 Shutdown of Prairie Island Unit 1 Due to Increasing Trend in Reactor Coolant System Leakage PNO-III-12-014, Notification of Unusual Event at Prairie Island Nuclear Generating Plant2012-11-0101 November 2012 PNO-III-12-014, Notification of Unusual Event at Prairie Island Nuclear Generating Plant ML12234A6382012-08-20020 August 2012 Update to Prairie Island Unit 1 Unplanned Shutdown Due to Both Emergency Diesel Generators Being Declared Inoperable ML12229A3572012-08-16016 August 2012 PNO-lll-12-008 - Prairie Island, Unit 1 Unplanned Shutdown Due to Both Emergency Diesel Generators Being Declared Inoperable PNO-III-11-013, A, Prairie Island Unit 2 Unplanned Shutdown for Greater than 72 Hours (Update)2011-10-20020 October 2011 PNO-III-11-013A, Prairie Island Unit 2 Unplanned Shutdown for Greater than 72 Hours (Update) ML1127804832011-10-0505 October 2011 PNO-III-11-013 - Prairie Island Unit 2 Unplanned Shutdown for Greater than 72 Hours PNO-III-10-002, Prairie Island Units 1 and 2, Fire in a Nonsafety-Related Diesel Generator2010-01-21021 January 2010 PNO-III-10-002, Prairie Island Units 1 and 2, Fire in a Nonsafety-Related Diesel Generator PNO-III-09-003, Prairie Island - Unplanned Unit 1 Shutdown Greater than 72 Hours2009-05-20020 May 2009 PNO-III-09-003: Prairie Island - Unplanned Unit 1 Shutdown Greater than 72 Hours PNO-III-08-007, A - Prairie Island, Unplanned Unit 1 Shutdown Greater than 72 Hours (Update)/ Notification of Unusual Event Due to a Release of a Toxic Gas Deemed Detrimental to Normal Operation of the Plant2008-08-0404 August 2008 PNO-III-08-007A - Prairie Island, Unplanned Unit 1 Shutdown Greater than 72 Hours (Update)/ Notification of Unusual Event Due to a Release of a Toxic Gas Deemed Detrimental to Normal Operation of the Plant ML0821408742008-08-0101 August 2008 PNO-III-08-007, Prairie Island Unit 1, Unplanned Unit 1 Shutdown Greater than 72 Hours/Special Inspection PNO-III-07-016, Prairie Island, Unplanned Unit 1 Shutdown Greater than 72 Hours2007-12-26026 December 2007 PNO-III-07-016: Prairie Island, Unplanned Unit 1 Shutdown Greater than 72 Hours PNO-III-07-005, Prairie Island Non-Credible Bomb Threat2007-03-20020 March 2007 PNO-III-07-005 - Prairie Island Non-Credible Bomb Threat PNO-III-06-003, Prairie Island Technical Specification Required Shutdown of Unit 2 for Greater than 72 Hours2006-02-0606 February 2006 PNO-III-06-003, Prairie Island Technical Specification Required Shutdown of Unit 2 for Greater than 72 Hours PNO-III-05-009, Technical Specification Required Shutdown of Prairie Island Unit 2 for Greater than 72 Hours2005-04-20020 April 2005 PNO-III-05-009, Technical Specification Required Shutdown of Prairie Island Unit 2 for Greater than 72 Hours 2023-06-08
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PRELIMINARY NOTIFICATION- REGION III May 20, 2009
PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-09-003
This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date.
Facility Prairie Island Unit 1 Northern States Power-Minnesota Welch, Minnesota Docket: 50-282 License: DPR-42 Licensee Emergency Classification Notification of Unusual Event Alert Site Area Emergency General Emergency X Not Applicable
SUBJECT:
UNPLANNED UNIT 1 SHUTDOWN
DESCRIPTION:
On May 18, 2009 at 1:05 p.m. (CDT), the Unit 1 reactor tripped after a trip of the 12 circulating water pump. The trip of the circulating water pump resulted in a condenser A/B differential pressure trip of the main turbine which in turn caused an automatic reactor trip. Auxiliary Feedwater Pumps automatically started on low steam generator level. All control rods fully inserted and the other plant equipment responded as expected. The 12 circulating water pump is one of two pumps needed to operate at full power.
The licensee is investigating the cause of the pump trip and considering options for testing the pump and plant restart.
The NRC resident inspectors are evaluating the licensee's progress.
State and local officials have been informed about the situation.
The information in this preliminary notification has been reviewed with licensee management.
This information is current as of 10:00 a.m.
on May 20, 2009.
CONTACTS: Jack Giessner Karla Stoedter 630-829-9619 651-388-8209