ML19351E894

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Monthly Operating Rept for Nov 1980
ML19351E894
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/03/1980
From: Gillett W
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML19351E889 List:
References
NUDOCS 8012190505
Download: ML19351E894 (6)


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50-316 DATI 12-3 A0 COMPL.. ; y, f W.T. G111ett 616-465-5901 7" ".*fCNI CP!aAT"NG 5"ATCS Donald C. Cook 2

No:=

g Novem0er 1980

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3391

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3. L.sansedThs==al?swer(MWt):

1133

4. Namesiase As:i=g (Csess 50Ve):

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1100

5. Design "*W R::ing(Mes SDVe):

1110

6. hum Dependshte Capaci:y (Cross 11Weg 1082

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7. '.fazunan D-~~'* <*---~y (Nec Mwe):
5. If Champs ce=stin Capaci:7 Razf=gs (Itar=: Nu=ser 3 Th:ougi: 7) Sisca L::: Reper:. C;ve Ruscas:

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9. ?mver Level To Mi=h 2ar=- R If Any (Not 3Cve):
10. Ransons For ?"-d-IfAsy:

l This51oash Y to.Cata Cu:=n!= rave j

720 8,040 25,560 k

11. ha.-s Is Rapor:iss Ped 0

6,160.4-17,240.3 w:C" r

12. Nwasar Cf Esa:s Ranc:or s

0 0

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13. Ra=c:ar Rasarve Shu= iowa Est=s 0

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Eoans C-m Ca.L*ns 0

0 0

15. U=ic Raserve Shardown Eat =s 0

19.906.4 %

52.130.876

16. Censs Thennal!===3y c-d OtwH)
17. Cros EInc=fc=1Isargy C-~d G.twH) 0 __,,

6.457,370 16.611.780 0

6.228,971 15,996,383 ts. Nec :t i Isargy c

-,' g.:wE) 0 75.5-71.9 0

75.5 71.9 8

19. Unit Service se:or
23. Unic Ar ilmoi!Ly 7:c:or 0

71.6 66.7

. Unit Capaczy 7:snar(Using >lDC.Wr) 0 70.4 66.0
. Unis Caa city F:c:or(Using CER Nect 100 15.6 14.6
23. Unic Forend Cu=ge Rac,
24. Shutdowns M '"tu CverNex: 6 Ston:hs(Type. Oste.:sd Cic=: ion of E:ci:::
25. If Sh:: Cown At End Cr Repore ?sriod. I::ussed Oste of $cs.-==:

Foreast Achieved

. 25. Caits is Tes: Sc: s IP:ior to C =arci:1 Ops;:: font:

INITIA L C?.!TICALITY INiTZAL I*a..a. 07:"f CO.*:*.:ZZC A :. C.*ER.GCN

($8(~71 8012T9000$

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-316 UNIT 2

DATE 12-3-80 COMPLETED BY W.T. Gillett TELEPHONE 616-465-5901 MONTH November 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net)

(MWe-Net) 1 0

17 0

2 0

18 0

3 0

19 0

4 0

20 0

5 0

21 0

l 6

0 22 0

l 7

0 23 0

8 0

24 0

9 0

25 0

10 0

26 0

11 0

27 0

12 0

28 0

13 0

29 0

14 0

30 0

15 0

31 0

16 0

1 i

INSTRUCTIONS On this famat list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whola megawatt.

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l 50 - 316 DOCKETNO.

UNIT SilU1 DOWNS AND POWE:H REI)UCTIONS D.C. Cook - Unit 2 UNil' N AhlE I

DATE 12-11-80 l

i i HEPORT &'lONill November, 1980 CohlPLiclED uy 8. A. Svensson lEl.LPilONE (616) 465-5901 j

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Cause & Cossc(sive 3

Attiam to No.

Date 9;

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89 Cont'd.

801018 F

720 A

3 N.A.

IIA GENERA Electrical generator repair outage continued from previous month. The unit remained out of service at the end of the month.

Return to service i

is scheduled for the week of December 8, 1980.

CcE2)

GEED W e) 1 2

3 4

1;: Fenced Heason:

hictinal:

lixhibit G. Instantitons S: Stliedulcil A-l'ilnipmens Failmo(1.nplain) l-blannal for Psepasation of Data Il blalutenance oi Test 2 Manual Sciam, lintiy Slicens fm 1.icensee g

C Hefueling 3 Automatic Sciam.

Event l<cpust (I IIH) I'de INIIRIE D Hegulaimy itestsiclion 4-Oilies (E xpl.iin) 0161) pg I!-Opesato l'eahdng& License lixaminallon F Administrative 5

M G Opesasional llenos (lixplain)

'lisinbis 1 - S.sme Soma y

l'l/17) ll Othes (Emplain)

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Docket No.: 50-316 Unit Nama:

D. C. Cook Unit #2 Completed By:

R. S. Keith Telephone:

(616) 465-5901 Date: December 12, 1980 Page:

1 of 1 MONTHLY OPERATING ACTIVITIES - NOVEMBER, 1980 Highlights:

The unplanned outage that started October 18, 1980 with a Generator trip from 1007. power continued the entire month.

The Unit was in Mode 5 the entire month with the Reactor Coolant System at-the loop level for modification to the Peactor Coolant Pump Motor Oil System.

Summary:

Major repair work performed during this report period included:

a) Replace 4 bars in main generator stator, b) Modification to main turbine bearing #2 housing.

c)

Inspection of Main Transformer instrumentation.

d)

Ice Condenser Ice Basket Weighing.

e) Repairs to "A" Low Pressure Turbine Stop and Intercept Valves.

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f)

Inspection of Moisture Separator.

g)

Installed new fasteners in Reactor Coolant Pump fire protection casings.

h) Numerous repairs to correct packing gland and body l

to bonnet leaks on steam system valves.

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Installed additional grating in all low pressure turbine condensers.

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DOCKET NO.

50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 12-11-80 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 1 MAJOR SAFETY-RELATED MAINTENANCE NOVEMBER, 1980 M-1 The steam inlet flange to the auxiliary feedpump turbine was leaking.

Replaced the flexitallic gasket.

Studs were checked for cracks by ncndestructive examination.

M-2 No. 4 steam generator power operated relief valve, MRV-243 was leaking by.

Replaced the cage and disc and machined,the pilot disc.

Proper valve operation was verified.

M-3 East containment spray heat exchanger inlet isolation valve, CTS-121E was leaking by.

Machined valve seats and reassembled with new gaskets.

M-4 Containment spray header drain isolation valve, 2-CTS-123E was leaking by. A new valve was installed. Necessary NDE was per-formed.

C&I-l MRV-223, steam generator No. 2 power operated relief valve could only be opened 50% when controlled by the hand / auto station in the control room. The valve's positioner was repaired and the calibration was performed.

C&I-2 The low alarm for the AB diesel generator intake air filter was periodically received. The transmation thermostat control for the heater had failed. A failed capacitor was replaced. The thermostat and alarm unit were calibrated and returned _to ser vice.

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