ML19309G036: Difference between revisions

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0425004003
0425004003
              .e y 7                                                               8006020250       $
.e y 7 8006020250
          % 77                                                                                         l' LJZJ                                                                                       i
% 77 LJZJ i
;          PUBLIC SERVICE                                                     April 25, 1980 INDIANA                                                                                 j S. W. Shields                                                                           ;
PUBLIC SERVICE April 25, 1980 INDIANA j
Vice President - Electric System 1
S. W. Shields Vice President - Electric System 1
Mr. James G. Keppler Director                               Docket Nos.: STN - 546 U. S. Nuclear Eagulatory Co:ccission                                     STN - 547 Region III Construction Permit Nos.:
Mr. James G. Keppler Director Docket Nos.: STN - 546 U. S. Nuclear Eagulatory Co:ccission STN - 547 Region III Construction Permit Nos.:
1           799 Roosew it Road                                                     CPPR - 170 Glen Ellyn, Illinois 601r                                               CPPR - 171 I                                     Marble Hill Nuclear Gencating Station q
1 799 Roosew it Road CPPR - 170 Glen Ellyn, Illinois 601r CPPR - 171 I
Units 1 and 2
Marble Hill Nuclear Gencating Station Units 1 and 2 q


==Dear Mr. Keppler:==
==Dear Mr. Keppler:==
 
On December 28, 1979, Messrs. R. E. Turner and T. D. Geib of Public l
On December 28, 1979, Messrs. R. E. Turner and T. D. Geib of Public l           Service Company of Indiana, Inc. (PSI) telephoned your office to notify you of a potentially reportable incident as required by 10CFR 50.55(e).
Service Company of Indiana, Inc. (PSI) telephoned your office to notify you of a potentially reportable incident as required by 10CFR 50.55(e).
i          The following report resolves that item and constitutes a final report under the Regulation.             In late December 1979, PSI Quality Assurance personnel discovered several joints in safety related structural steel located in the Auxiliary Building which had not been bolted properly.
The following report resolves that item and constitutes a final report i
under the Regulation.
In late December 1979, PSI Quality Assurance personnel discovered several joints in safety related structural steel located in the Auxiliary Building which had not been bolted properly.
Standards governing structural steel erection require plate washers to be used when bolting joints with long slotted connection holes.
Standards governing structural steel erection require plate washers to be used when bolting joints with long slotted connection holes.
These washers must be large enough to cover the entire slotted hole.
These washers must be large enough to cover the entire slotted hole.
The structural steel joints in question either had washers which were not large enough to cover the entire slotted hole or did nM have any washer over the slotted hole at all. Some of these structural steel joints had also been inspected and approved by contractor quality assurance personnel.
The structural steel joints in question either had washers which were not large enough to cover the entire slotted hole or did nM have any washer over the slotted hole at all. Some of these structural steel joints had also been inspected and approved by contractor quality assurance personnel.
i Absence of plate washers on long slotted connection holes can modify the way a joint reacts to structural loading. While the struc6 tre is l           conservatively designed, failure of the joint may result if it is subjected to the extreme loadings which may occur during certain design basis events.
i Absence of plate washers on long slotted connection holes can modify the way a joint reacts to structural loading. While the struc6 tre is l
As discussed in the interim report of January 24, 1980 PSI has l           developed and is presently implementing a procedure under the Construction Verification program to verify the proper installation of washers in all sr.fety related structural steel joints. This procedure, Special Process Procedure 3 (SPP-3), will serve to identify those 56
conservatively designed, failure of the joint may result if it is subjected to the extreme loadings which may occur during certain design basis events.
                                                                                                  /b 1000 East Main Street. Plainfield, Indiana 46168       .                317 . 839 .9611
As discussed in the interim report of January 24, 1980 PSI has l
developed and is presently implementing a procedure under the Construction Verification program to verify the proper installation of washers in all sr.fety related structural steel joints. This procedure, Special Process Procedure 3 (SPP-3), will serve to identify those 56
/b 1000 East Main Street. Plainfield, Indiana 46168 317. 839.9611


  .        o d
o daf PUBLIC SERVICE Letter:
af PUBLIC SERVICE Letter:         Mr. James G. Keppler                           April 25, 1980 INDIANA joints which do not have washers properly installed and is enclosed with this letter. All structural steel joints which do not have the proper washers will be reinstalled with the correct washer configuration.
Mr. James G. Keppler April 25, 1980 INDIANA joints which do not have washers properly installed and is enclosed with this letter. All structural steel joints which do not have the proper washers will be reinstalled with the correct washer configuration.
This reinstallation will be done in accordance with approved ccntractor installation procedures.
This reinstallation will be done in accordance with approved ccntractor installation procedures.
To prevent the reoccurance of this situation, contractor inspection procedures will be revised to incorporate the characteristics of verification procedure, SPP-3 by July 1,1980.
To prevent the reoccurance of this situation, contractor inspection procedures will be revised to incorporate the characteristics of verification procedure, SPP-3 by July 1,1980.
If you have any questions on this item, please feel free to contact me.
If you have any questions on this item, please feel free to contact me.
Sincerely, t Y' S. W. Shields TDG:jkw cc: Director of Inspection & Enforcement U. S. Nuclear Regulatory Cocsission Washington, D. C. 20555 E. R. Schweibinz, P. E.
Sincerely, Y'
t S. W. Shields TDG:jkw cc: Director of Inspection & Enforcement U. S. Nuclear Regulatory Cocsission Washington, D. C.
20555 E. R. Schweibinz, P. E.
J. J. Harrison 9
J. J. Harrison 9
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Latest revision as of 02:38, 2 January 2025

Final Deficiency Rept Re Improperly Bolted Joints in Auxiliary Bldg safety-related Structural Steel.Encl Special Process Procedure SPP-3,Revision 3, Category I Structural Steel, Resolves Problem
ML19309G036
Person / Time
Site: Marble Hill
Issue date: 04/25/1980
From: Shields S
PSI ENERGY, INC. A/K/A PUBLIC SERVICE CO. OF INDIANA
To:
Shared Package
ML19309G037 List:
References
NUDOCS 8005020250
Download: ML19309G036 (2)


Text

_

0425004003

.e y 7 8006020250

% 77 LJZJ i

PUBLIC SERVICE April 25, 1980 INDIANA j

S. W. Shields Vice President - Electric System 1

Mr. James G. Keppler Director Docket Nos.: STN - 546 U. S. Nuclear Eagulatory Co:ccission STN - 547 Region III Construction Permit Nos.:

1 799 Roosew it Road CPPR - 170 Glen Ellyn, Illinois 601r CPPR - 171 I

Marble Hill Nuclear Gencating Station Units 1 and 2 q

Dear Mr. Keppler:

On December 28, 1979, Messrs. R. E. Turner and T. D. Geib of Public l

Service Company of Indiana, Inc. (PSI) telephoned your office to notify you of a potentially reportable incident as required by 10CFR 50.55(e).

The following report resolves that item and constitutes a final report i

under the Regulation.

In late December 1979, PSI Quality Assurance personnel discovered several joints in safety related structural steel located in the Auxiliary Building which had not been bolted properly.

Standards governing structural steel erection require plate washers to be used when bolting joints with long slotted connection holes.

These washers must be large enough to cover the entire slotted hole.

The structural steel joints in question either had washers which were not large enough to cover the entire slotted hole or did nM have any washer over the slotted hole at all. Some of these structural steel joints had also been inspected and approved by contractor quality assurance personnel.

i Absence of plate washers on long slotted connection holes can modify the way a joint reacts to structural loading. While the struc6 tre is l

conservatively designed, failure of the joint may result if it is subjected to the extreme loadings which may occur during certain design basis events.

As discussed in the interim report of January 24, 1980 PSI has l

developed and is presently implementing a procedure under the Construction Verification program to verify the proper installation of washers in all sr.fety related structural steel joints. This procedure, Special Process Procedure 3 (SPP-3), will serve to identify those 56

/b 1000 East Main Street. Plainfield, Indiana 46168 317. 839.9611

o daf PUBLIC SERVICE Letter:

Mr. James G. Keppler April 25, 1980 INDIANA joints which do not have washers properly installed and is enclosed with this letter. All structural steel joints which do not have the proper washers will be reinstalled with the correct washer configuration.

This reinstallation will be done in accordance with approved ccntractor installation procedures.

To prevent the reoccurance of this situation, contractor inspection procedures will be revised to incorporate the characteristics of verification procedure, SPP-3 by July 1,1980.

If you have any questions on this item, please feel free to contact me.

Sincerely, Y'

t S. W. Shields TDG:jkw cc: Director of Inspection & Enforcement U. S. Nuclear Regulatory Cocsission Washington, D. C.

20555 E. R. Schweibinz, P. E.

J. J. Harrison 9

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