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(                                         DUQUESNE LIGHT COMPANY 3eaver Valley Power Station NARRATIVE  
(
DUQUESNE LIGHT COMPANY 3eaver Valley Power Station NARRATIVE  


==SUMMARY==
==SUMMARY==
OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 January 1   Station in Operational Mode 4 at 950 PSIG and 337F. Heat-up of the reactor coolant system was in progress. Entered Operational Mode 3 at 0152 hours.
OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 January 1 Station in Operational Mode 4 at 950 PSIG and 337F. Heat-up of the reactor coolant system was in progress. Entered Operational Mode 3 at 0152 hours.
January 2   Station in Operational Mode 3 at 200 PSIG and 541F. Heat-up through of the reactor coolant system was in progress and the prerequisites January 5   for reactor criticality were being completed. At 2000 hours, a small packing leak developed on the 1B loop bypass flow isolation valve [1RC-45]. This leak could not be stopped. At 0303 hours on January 3, a station cooldown to Operational Mode 5 was begun.
January 2 Station in Operational Mode 3 at 200 PSIG and 541F. Heat-up through of the reactor coolant system was in progress and the prerequisites January 5 for reactor criticality were being completed. At 2000 hours, a small packing leak developed on the 1B loop bypass flow isolation valve [1RC-45]. This leak could not be stopped. At 0303 hours on January 3, a station cooldown to Operational Mode 5 was begun.
The Station entered Operational Mode 4 at 0940 hours and Operational Mode 5 at 1535 hours. Containment vacuum was broken at 1630 hours and RCS depressurization was begun at 2010 hours. The packing leak on [1RC-45] was repaired and the packing on other similar valves were checked and adjusted as necessary by 1220 hours on January 4. Filling the pressurizer was begun immediately and a steam bubble was established by 0300 hours on January 5. Drawing the containment vacuum was begun at 0550 hours.
The Station entered Operational Mode 4 at 0940 hours and Operational Mode 5 at 1535 hours. Containment vacuum was broken at 1630 hours and RCS depressurization was begun at 2010 hours.
Jaruary 6 Station in Operational Mode 5 at 317 PSIG and 153F. Heat-up of the reactor coolant system was in progress. At 0255 hours, with the RCS temperature at 180F, further heat-up was delayed to correct reactor coolant pump seal problems. Heat-up was l                   resumed at 0650 hours and the Station entered Operational Mode 4 at 1213 hours. At 1555 hours, the Company Engineering Department informed the Station of a pipe-whip-restraint deficiency at the main steam line non-return valves and an RCS cooldown to Operational Mode 5 was begun to repair the restraints.
The packing leak on [1RC-45] was repaired and the packing on other similar valves were checked and adjusted as necessary by 1220 hours on January 4.
January 7 Station in Operational Mode 4 at 390 PSIG and 300F. RCS pressure was being maintained at less than 400 PSIG.and RCS temperature was being maintained between 300F and 325F during main steam line restraint repairs. At 0745 hours, the Residual Heat Removal system was isolated and an increase of RCS pressure to 900 PSIG was commenced.
Filling the pressurizer was begun immediately and a steam bubble was established by 0300 hours on January 5.
January 8 Station in Operational Mode 4 at 870 PSIG and 323F. At 1040 hours the lA main feedwater stop-check isolation valve
Drawing the containment vacuum was begun at 0550 hours.
Jaruary 6 Station in Operational Mode 5 at 317 PSIG and 153F. Heat-up of the reactor coolant system was in progress. At 0255 hours, with the RCS temperature at 180F, further heat-up was delayed to correct reactor coolant pump seal problems. Heat-up was l
resumed at 0650 hours and the Station entered Operational Mode 4 at 1213 hours. At 1555 hours, the Company Engineering Department informed the Station of a pipe-whip-restraint deficiency at the main steam line non-return valves and an RCS cooldown to Operational Mode 5 was begun to repair the restraints.
January 7 Station in Operational Mode 4 at 390 PSIG and 300F. RCS pressure was being maintained at less than 400 PSIG.and RCS temperature was being maintained between 300F and 325F during main steam line restraint repairs. At 0745 hours, the Residual Heat Removal system was isolated and an increase of RCS pressure to 900 PSIG was commenced.
January 8 Station in Operational Mode 4 at 870 PSIG and 323F. At 1040 hours the lA main feedwater stop-check isolation valve
[MOV-FW-156A] was declared inoperable because the gear drive housing was discovered cracked. At'1850 hours, both Low Head Safety Injection (LHSI) Pumps were declared inoperable when they did not meet the Operational Surveillance Test (OST) acceptance criteria. The recirculation flow test line was discovered to have frozen.
[MOV-FW-156A] was declared inoperable because the gear drive housing was discovered cracked. At'1850 hours, both Low Head Safety Injection (LHSI) Pumps were declared inoperable when they did not meet the Operational Surveillance Test (OST) acceptance criteria. The recirculation flow test line was discovered to have frozen.
81 02180W
81 02180W
Line 34: Line 39:
==SUMMARY==
==SUMMARY==
OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 (continued)
OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 (continued)
January 9     Station in Operational Mode 4 at 920 PSIG and 321F. RCS was through     being =aintained in the hot shutdown condition pending repairs January 10   to [MOV-FW-156A] and adding insulation to the LHSI Pump test line. At 1445 hours the LHSI pumps were declared operable after satisfactory completion of the surveillance tests, At 2100 hours, (MOV-FW-156A] was operable and RCS heat-up was commenced at 2127 hours. The Station entered Operational Mode 3 at 2320 hours with the RCS heat-up in progress.
January 9 Station in Operational Mode 4 at 920 PSIG and 321F. RCS was through being =aintained in the hot shutdown condition pending repairs January 10 to [MOV-FW-156A] and adding insulation to the LHSI Pump test line. At 1445 hours the LHSI pumps were declared operable after satisfactory completion of the surveillance tests, At 2100 hours, (MOV-FW-156A] was operable and RCS heat-up was commenced at 2127 hours. The Station entered Operational Mode 3 at 2320 hours with the RCS heat-up in progress.
January 11   Station in Operational Mode 3 at 2235 PSIG and 545F. The reactor through     start-up was com=enced at 1441 hours. The reactor was critical January 12   at 1535 hours and the main unit was synchronized at 0147 hcurs on January 12.
January 11 Station in Operational Mode 3 at 2235 PSIG and 545F.
January 13   Station in Operational Mode 1 at nominal 88% reactor power.
The reactor through start-up was com=enced at 1441 hours. The reactor was critical January 12 at 1535 hours and the main unit was synchronized at 0147 hcurs on January 12.
January 14   Station in Operational Mode 1 at nominal 99% reactor power.
January 13 Station in Operational Mode 1 at nominal 88% reactor power.
through January 20 January 21   Station in Operational Mode 1 at nominal 98" reactor power.
January 14 Station in Operational Mode 1 at nominal 99% reactor power.
through January 20 January 21 Station in Operational Mode 1 at nominal 98" reactor power.
Power level was reduced to 95% because of high backpressure in the main condenser. Electric power output varied slightly with main condenser performance.
Power level was reduced to 95% because of high backpressure in the main condenser. Electric power output varied slightly with main condenser performance.
January 22   Station in Operational Mode 1 at nominal 97% reactor power. An Emergency Preparedness Plan alert was declared at 0430 hours due to a high-high radiation alarm on the leak collection areas exhaust gas radiation monitor [RM-VS-105], which automatically diverts the discharge through the =ain filter banks. The maximum off-site gaseous releases did not exceed 3% MPC. The alert was terminated at 0848 hours. The apparent cause was gas-accumulation in the pipe trenches being released into the main building space when the trench cover blocks were removed January 23   Station in Operational Mode 1 at nominal 987. reactor power.
January 22 Station in Operational Mode 1 at nominal 97% reactor power. An Emergency Preparedness Plan alert was declared at 0430 hours due to a high-high radiation alarm on the leak collection areas exhaust gas radiation monitor [RM-VS-105], which automatically diverts the discharge through the =ain filter banks.
t    January 24   Station in Operational Mode 1 at nominal 99% reactor power. The through     power level was reduced to 64% at 2050 hours to remove the main i     January 26   condenser section A from service for a tube cleanliness inspection.
The maximum off-site gaseous releases did not exceed 3% MPC. The alert was terminated at 0848 hours. The apparent cause was gas-accumulation in the pipe trenches being released into the main building space when the trench cover blocks were removed January 23 Station in Operational Mode 1 at nominal 987. reactor power.
January 24 Station in Operational Mode 1 at nominal 99% reactor power. The t
through power level was reduced to 64% at 2050 hours to remove the main i
January 26 condenser section A from service for a tube cleanliness inspection.
Condenser section A was returned to service at 0830 hours on January 25 and section 3 was removed ~from service for inspection when the circulating water outlet isolation valve for section 3 could not be opened. The power level was further reduced to 46%
Condenser section A was returned to service at 0830 hours on January 25 and section 3 was removed ~from service for inspection when the circulating water outlet isolation valve for section 3 could not be opened. The power level was further reduced to 46%
l
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1     J NARRATIVE  
1 J
NARRATIVE  


==SUMMARY==
==SUMMARY==
OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 (continued) at 1615 hours on January 26 in order to shut down the 1C Cooling Tower Pu=p to reduce the pressure on the valve. Power level was increased to 74% at 1840 hours with two (1A and 1D) cooling tower pumps in service. The 1C Cooling Tower Pump was placed into service at 2023 hours and the power level was increased to 93% by 2220 hours. Power level was reduced to 90% at 2232 hours due to high condensate temperatures.
OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 (continued) at 1615 hours on January 26 in order to shut down the 1C Cooling Tower Pu=p to reduce the pressure on the valve. Power level was increased to 74% at 1840 hours with two (1A and 1D) cooling tower pumps in service. The 1C Cooling Tower Pump was placed into service at 2023 hours and the power level was increased to 93% by 2220 hours. Power level was reduced to 90% at 2232 hours due to high condensate temperatures.
January 27     Station in Operational Mode 1 at nominal 90% reactor power.
January 27 Station in Operational Mode 1 at nominal 90% reactor power.
through       Maintaining the condenser vacuum / turbine backpressure was the January 29     major operational difficulty and some adjustment of power level was required to retain proper station operating conditions.
through Maintaining the condenser vacuum / turbine backpressure was the January 29 major operational difficulty and some adjustment of power level was required to retain proper station operating conditions.
January 30     Station in Operational Mode 1 at nominal 94% reactor power. At through       2043 hours, commenced reducing power level to 59% to perform January 31     main condenser inspection and maintenance.
January 30 Station in Operational Mode 1 at nominal 94% reactor power. At through 2043 hours, commenced reducing power level to 59% to perform January 31 main condenser inspection and maintenance.
MAJOR SAFETY-RELATED MAINTENANCE - JANUARY 1981
MAJOR SAFETY-RELATED MAINTENANCE - JANUARY 1981 1.
: 1. The gear housing for the motor-operated 1A main feedwater isolation valve [MOV-F'4-156A] was replaced after the housing was found to be cracked.                                          .
The gear housing for the motor-operated 1A main feedwater isolation valve [MOV-F'4-156A] was replaced after the housing was found to be cracked.
1
1 y
                      *  -  -                y              t
t


OPERATING DATA REPORT                                                                                                   ,
OPERATING DATA REPORT 1
1
DOCKET NO. 50-334 DATE 2-4-81 COMP!.ETED BY D.
_                                              DOCKET NO. 50-334 DATE 2-4-81 COMP!.ETED BY                 D.     ?. TSko TELEPHONE. '' '-4'-9308                           i OPERATLNG STATUS                                                                                                                                                                                 ;
?. TSko TELEPHONE. '' '-4'-9308 i
i
OPERATLNG STATUS i
: 1. Unit Name:. 3eaver M ay ?cuer Scacien Uni:"11                                                                                       h                                                             !
: 1. Unit Name:. 3eaver M ay ?cuer Scacien Uni:"11 h
Januar7, 1981
Januar7, 1981
: 2. Reporting Period:                                                                                                                                                                                   ;
: 2. Reporting Period:
: 3. Licensed Thermal Power (MWt):                                                               7 ' ' ''
: 3. Licensed Thermal Power (MWt):
: 4. Nameplate Rating (Gross MWe):                                                                   923
7 ' ' ''
923
: 4. Nameplate Rating (Gross MWe):
352
: 5. Design Electrical Ranng (Net MWe):
: 5. Design Electrical Ranng (Net MWe):
352 d'3
d'3
: 6. Maximum Dependable Capacity (Gross MWe):
: 6. Maximum Dependable Capacity (Gross MWe):
: 7. Maximum Dependable Capacity (Net MWe):                                                           810                                                                                               l
: 7. Maximum Dependable Capacity (Net MWe):
: 8. If Chantes Occur in Capacity Ratings (Items Number 3 Througn 7) Since Last Report. Give Ressons:                                                                                                   l l
l 810
: 8. If Chantes Occur in Capacity Ratings (Items Number 3 Througn 7) Since Last Report. Give Ressons:
l l
t
t
: 9. Power Level To Which Restricted.If Any(Net MWe):                                                                         None
: 9. Power Level To Which Restricted.If Any(Net MWe):
: 10. Reasons For Rasmcrions,If Any;                                                                                           N/A                                                                      i 1
None N/A i
This Month                         Yr.-to. Oste                   Cumulative
: 10. Reasons For Rasmcrions,If Any; 1
                              !!. Hours In Reporting Period                                                                           744                                  744                    &T d49                            t I
This Month Yr.-to. Oste Cumulative 744 744
: 12. Number of Hours Resetor Was Critical                                                                 488.42                               488.42                 14.08c.co
&T d49
: 13. Reactor Reserve Shutdown Hours 0                              0                        4.482.8                      ;
!!. Hours In Reporting Period t
: 14. Hour:Generatoron.Line                                                                               478.22                               478.22             E 84.47                                 ;
I
: 15. Unit Reserve Shutdown Hours                                                                                 0                               0                                 0                   ,
: 12. Number of Hours Resetor Was Critical 488.42 488.42 14.08c.co 0
: 16. Gross Thermal Energy Generated (MWH)                                                       1,118,511.5                                 1.118,511.5               29.226.404.65                     !
0 4.482.8
353,500                             353,500                     8,980,840 l
: 13. Reactor Reserve Shutdown Hours
: 17. Gross Electrical Energy Genersted (MWH)                                                                                         _ _ ,                                                              [
: 14. Hour:Generatoron.Line 478.22 478.22 E 84.47
: 18. Net Electrics! Energy Generated (MWH)                                                               324.787                             324.787                     8.1Ar, 201 .
: 15. Unit Reserve Shutdown Hours 0
!.                            19. Unit Service Factor                                                                                     64.3                             64.3                               34.9 l
0 0
: 20. Unit Availability Factor                                                                                64.3                             64.3                               34.9                 l
: 16. Gross Thermal Energy Generated (MWH) 1,118,511.5 1.118,511.5 29.226.404.65 353,500 353,500 8,980,840
: 21. Unit Capacity Factor (Using MDC Net)                                                                    53.9                             53.9                               27.0                 !
[
: 22. Unit Capacity Factor (Using DER Net)                                                                     51.2                             51.2                               25.7                 ,
l
i                              23. Unit Forced Outsge Rate                                                                                  35.7                             35.7                               45.7                 L l
: 17. Gross Electrical Energy Genersted (MWH)
: 24. Shutdowns Scheduled Over Next 6 Months (Type. Date. and Duration of Each t-Major =cdification outage /May 15, 1981/7 weelus                                                                                                                     i
: 18. Net Electrics! Energy Generated (MWH) 324.787 324.787 8.1Ar, 201
: 25. If Shut Down At End Of Report Period. Estimated Date of Startup:                                                                                                                                   ,.
: 19. Unit Service Factor 64.3 64.3 34.9 64.3 64.3 34.9 l
: 26. Units In Test Status Prior to Commereist Operation):                                                                                     Forecast                       Achieved l
l
f                                                                                 INITIAL CRITICALITY                                                                         Y/A                             N/A                   !
: 20. Unit Availability Factor 53.9 53.9 27.0
INITIAL ELECTRICITY                                                                         N/A                             N/A                   E COMMERCIAL OPER ATION                                                                       N/A                             N/A i
: 21. Unit Capacity Factor (Using MDC Net) 51.2 51.2 25.7
* T l
: 22. Unit Capacity Factor (Using DER Net) 35.7 35.7 45.7 L
D**                      &,                              (9/77)       i ww         o                               n
: 23. Unit Forced Outsge Rate i
  . . _ _ . _ _ , . . _    .      ._    . . ~ . . _ , _ _ _ . _ _ . _ _ _ _ _ .                   ._ . . . _ . _ _ _ _ . . . . , . . . _ . . _ . . - . , . . .                          . , _ . . . . - ,          _
l
: 24. Shutdowns Scheduled Over Next 6 Months (Type. Date. and Duration of Each t-Major =cdification outage /May 15, 1981/7 weelus i
: 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
: 26. Units In Test Status Prior to Commereist Operation):
Forecast Achieved l
f INITIAL CRITICALITY Y/A N/A INITIAL ELECTRICITY N/A N/A E
COMMERCIAL OPER ATION N/A N/A i
D**
T l
(9/77) i ww o
n
.. ~.. _, _ _ _. _ _. _ _ _ _ _.


l I
l l
l AVERAGE DA!Li UNIT POWER LEVEL                                                           i DOCKET NO.
AVERAGE DA!Li UNIT POWER LEVEL i
50-334 UNIT 372S Uni" Y1 DATE   2-4-81 COMPLETED BY D. R. %
50-334 DOCKET NO.
17.LEPHONE           412-443-530S MONTH             Januari, 1981 DAY           AVERAGE DAILY POWER LEVEL                               DAY       AVERAGE DAILY POWER LEVEL (MWe.Netj                                                     (Mwe Nec3 1
UNIT 372S Uni" Y1 DATE 2-4-81 D. R. %
0                                  37              781-1                                 0                                   gg               785 3                                 0                                   19               791 4                                 0                                   20               776 5                                  0                                   23               735 6                                 0                                  22               756 7                                 0                                   23      _
COMPLETED BY 17.LEPHONE 412-443-530S MONTH Januari, 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe.Netj (Mwe Nec3 0
752 3                                 0                                   24              707 9
781-1 37 1
0                                  ,3               474 10                                 0                                   26              470 11 0                                  27 690 g2                                425                                                   707 23 803                                   ,9               731                  -
0 gg 785 3
13 803                                                   665 34                                                                     30 13 799                                  33 336 16                               791 INSTRUCTIONS On this for:::st.!ist the average d:aly unit power !celin MWe. Net for each day in the repurring month. Compute to the r.esrest whvie megswatt.
0 19 791 4
0 20 776 0
23 735 5
0 756 6
22 7
23 752 0
707 0
24 3
0 474 9
,3 0
470 10 26 0
690 11 27 425 707 g2 23 803 731 13
,9 803 665 34 30 799 336 13 33 791 16 INSTRUCTIONS On this for:::st.!ist the average d:aly unit power !celin MWe. Net for each day in the repurring month. Compute to the r.esrest whvie megswatt.
(4/77)
(4/77)


I      KE          50-334                   '
50-334 I
UNIT SillllDOWNS AND POWER REllOCIlONS                                           BVPS linit #1 NAhE DATE     2-4-81
KE UNIT SillllDOWNS AND POWER REllOCIlONS BVPS linit #1 NAhE DATE 2-4-81 COMPl.E I ED ilY _lla L Tilak" REPOR T MONill
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Latest revision as of 12:23, 24 December 2024

Monthly Operating Rept for Jan 1981
ML19343B972
Person / Time
Site: Beaver Valley
Issue date: 02/04/1981
From: Timko D
DUQUESNE LIGHT CO.
To:
Shared Package
ML19343B969 List:
References
NUDOCS 8102180406
Download: ML19343B972 (6)


Text

.

(

DUQUESNE LIGHT COMPANY 3eaver Valley Power Station NARRATIVE

SUMMARY

OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 January 1 Station in Operational Mode 4 at 950 PSIG and 337F. Heat-up of the reactor coolant system was in progress. Entered Operational Mode 3 at 0152 hours0.00176 days <br />0.0422 hours <br />2.513228e-4 weeks <br />5.7836e-5 months <br />.

January 2 Station in Operational Mode 3 at 200 PSIG and 541F. Heat-up through of the reactor coolant system was in progress and the prerequisites January 5 for reactor criticality were being completed. At 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />, a small packing leak developed on the 1B loop bypass flow isolation valve [1RC-45]. This leak could not be stopped. At 0303 hours0.00351 days <br />0.0842 hours <br />5.009921e-4 weeks <br />1.152915e-4 months <br /> on January 3, a station cooldown to Operational Mode 5 was begun.

The Station entered Operational Mode 4 at 0940 hours0.0109 days <br />0.261 hours <br />0.00155 weeks <br />3.5767e-4 months <br /> and Operational Mode 5 at 1535 hours0.0178 days <br />0.426 hours <br />0.00254 weeks <br />5.840675e-4 months <br />. Containment vacuum was broken at 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br /> and RCS depressurization was begun at 2010 hours0.0233 days <br />0.558 hours <br />0.00332 weeks <br />7.64805e-4 months <br />.

The packing leak on [1RC-45] was repaired and the packing on other similar valves were checked and adjusted as necessary by 1220 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.6421e-4 months <br /> on January 4.

Filling the pressurizer was begun immediately and a steam bubble was established by 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br /> on January 5.

Drawing the containment vacuum was begun at 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />.

Jaruary 6 Station in Operational Mode 5 at 317 PSIG and 153F. Heat-up of the reactor coolant system was in progress. At 0255 hours0.00295 days <br />0.0708 hours <br />4.21627e-4 weeks <br />9.70275e-5 months <br />, with the RCS temperature at 180F, further heat-up was delayed to correct reactor coolant pump seal problems. Heat-up was l

resumed at 0650 hours0.00752 days <br />0.181 hours <br />0.00107 weeks <br />2.47325e-4 months <br /> and the Station entered Operational Mode 4 at 1213 hours0.014 days <br />0.337 hours <br />0.00201 weeks <br />4.615465e-4 months <br />. At 1555 hours0.018 days <br />0.432 hours <br />0.00257 weeks <br />5.916775e-4 months <br />, the Company Engineering Department informed the Station of a pipe-whip-restraint deficiency at the main steam line non-return valves and an RCS cooldown to Operational Mode 5 was begun to repair the restraints.

January 7 Station in Operational Mode 4 at 390 PSIG and 300F. RCS pressure was being maintained at less than 400 PSIG.and RCS temperature was being maintained between 300F and 325F during main steam line restraint repairs. At 0745 hours0.00862 days <br />0.207 hours <br />0.00123 weeks <br />2.834725e-4 months <br />, the Residual Heat Removal system was isolated and an increase of RCS pressure to 900 PSIG was commenced.

January 8 Station in Operational Mode 4 at 870 PSIG and 323F. At 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br /> the lA main feedwater stop-check isolation valve

[MOV-FW-156A] was declared inoperable because the gear drive housing was discovered cracked. At'1850 hours0.0214 days <br />0.514 hours <br />0.00306 weeks <br />7.03925e-4 months <br />, both Low Head Safety Injection (LHSI) Pumps were declared inoperable when they did not meet the Operational Surveillance Test (OST) acceptance criteria. The recirculation flow test line was discovered to have frozen.

81 02180W

NARRATIVE

SUMMARY

OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 (continued)

January 9 Station in Operational Mode 4 at 920 PSIG and 321F. RCS was through being =aintained in the hot shutdown condition pending repairs January 10 to [MOV-FW-156A] and adding insulation to the LHSI Pump test line. At 1445 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.498225e-4 months <br /> the LHSI pumps were declared operable after satisfactory completion of the surveillance tests, At 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, (MOV-FW-156A] was operable and RCS heat-up was commenced at 2127 hours0.0246 days <br />0.591 hours <br />0.00352 weeks <br />8.093235e-4 months <br />. The Station entered Operational Mode 3 at 2320 hours0.0269 days <br />0.644 hours <br />0.00384 weeks <br />8.8276e-4 months <br /> with the RCS heat-up in progress.

January 11 Station in Operational Mode 3 at 2235 PSIG and 545F.

The reactor through start-up was com=enced at 1441 hours0.0167 days <br />0.4 hours <br />0.00238 weeks <br />5.483005e-4 months <br />. The reactor was critical January 12 at 1535 hours0.0178 days <br />0.426 hours <br />0.00254 weeks <br />5.840675e-4 months <br /> and the main unit was synchronized at 0147 hcurs on January 12.

January 13 Station in Operational Mode 1 at nominal 88% reactor power.

January 14 Station in Operational Mode 1 at nominal 99% reactor power.

through January 20 January 21 Station in Operational Mode 1 at nominal 98" reactor power.

Power level was reduced to 95% because of high backpressure in the main condenser. Electric power output varied slightly with main condenser performance.

January 22 Station in Operational Mode 1 at nominal 97% reactor power. An Emergency Preparedness Plan alert was declared at 0430 hours0.00498 days <br />0.119 hours <br />7.109788e-4 weeks <br />1.63615e-4 months <br /> due to a high-high radiation alarm on the leak collection areas exhaust gas radiation monitor [RM-VS-105], which automatically diverts the discharge through the =ain filter banks.

The maximum off-site gaseous releases did not exceed 3% MPC. The alert was terminated at 0848 hours0.00981 days <br />0.236 hours <br />0.0014 weeks <br />3.22664e-4 months <br />. The apparent cause was gas-accumulation in the pipe trenches being released into the main building space when the trench cover blocks were removed January 23 Station in Operational Mode 1 at nominal 987. reactor power.

January 24 Station in Operational Mode 1 at nominal 99% reactor power. The t

through power level was reduced to 64% at 2050 hours0.0237 days <br />0.569 hours <br />0.00339 weeks <br />7.80025e-4 months <br /> to remove the main i

January 26 condenser section A from service for a tube cleanliness inspection.

Condenser section A was returned to service at 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br /> on January 25 and section 3 was removed ~from service for inspection when the circulating water outlet isolation valve for section 3 could not be opened. The power level was further reduced to 46%

l

1 J

NARRATIVE

SUMMARY

OF MONTHLY OPERATING EXPERIENCE - JANUARY 1981 (continued) at 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br /> on January 26 in order to shut down the 1C Cooling Tower Pu=p to reduce the pressure on the valve. Power level was increased to 74% at 1840 hours0.0213 days <br />0.511 hours <br />0.00304 weeks <br />7.0012e-4 months <br /> with two (1A and 1D) cooling tower pumps in service. The 1C Cooling Tower Pump was placed into service at 2023 hours0.0234 days <br />0.562 hours <br />0.00334 weeks <br />7.697515e-4 months <br /> and the power level was increased to 93% by 2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br />. Power level was reduced to 90% at 2232 hours0.0258 days <br />0.62 hours <br />0.00369 weeks <br />8.49276e-4 months <br /> due to high condensate temperatures.

January 27 Station in Operational Mode 1 at nominal 90% reactor power.

through Maintaining the condenser vacuum / turbine backpressure was the January 29 major operational difficulty and some adjustment of power level was required to retain proper station operating conditions.

January 30 Station in Operational Mode 1 at nominal 94% reactor power. At through 2043 hours0.0236 days <br />0.568 hours <br />0.00338 weeks <br />7.773615e-4 months <br />, commenced reducing power level to 59% to perform January 31 main condenser inspection and maintenance.

MAJOR SAFETY-RELATED MAINTENANCE - JANUARY 1981 1.

The gear housing for the motor-operated 1A main feedwater isolation valve [MOV-F'4-156A] was replaced after the housing was found to be cracked.

1 y

t

OPERATING DATA REPORT 1

DOCKET NO. 50-334 DATE 2-4-81 COMP!.ETED BY D.

?. TSko TELEPHONE. '-4'-9308 i

OPERATLNG STATUS i

1. Unit Name:. 3eaver M ay ?cuer Scacien Uni:"11 h

Januar7, 1981

2. Reporting Period:
3. Licensed Thermal Power (MWt):

7 ' '

923

4. Nameplate Rating (Gross MWe):

352

5. Design Electrical Ranng (Net MWe):

d'3

6. Maximum Dependable Capacity (Gross MWe):
7. Maximum Dependable Capacity (Net MWe):

l 810

8. If Chantes Occur in Capacity Ratings (Items Number 3 Througn 7) Since Last Report. Give Ressons:

l l

t

9. Power Level To Which Restricted.If Any(Net MWe):

None N/A i

10. Reasons For Rasmcrions,If Any; 1

This Month Yr.-to. Oste Cumulative 744 744

&T d49

!!. Hours In Reporting Period t

I

12. Number of Hours Resetor Was Critical 488.42 488.42 14.08c.co 0

0 4.482.8

13. Reactor Reserve Shutdown Hours
14. Hour:Generatoron.Line 478.22 478.22 E 84.47
15. Unit Reserve Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWH) 1,118,511.5 1.118,511.5 29.226.404.65 353,500 353,500 8,980,840

[

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17. Gross Electrical Energy Genersted (MWH)
18. Net Electrics! Energy Generated (MWH) 324.787 324.787 8.1Ar, 201
19. Unit Service Factor 64.3 64.3 34.9 64.3 64.3 34.9 l

l

20. Unit Availability Factor 53.9 53.9 27.0
21. Unit Capacity Factor (Using MDC Net) 51.2 51.2 25.7
22. Unit Capacity Factor (Using DER Net) 35.7 35.7 45.7 L
23. Unit Forced Outsge Rate i

l

24. Shutdowns Scheduled Over Next 6 Months (Type. Date. and Duration of Each t-Major =cdification outage /May 15, 1981/7 weelus i
25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status Prior to Commereist Operation):

Forecast Achieved l

f INITIAL CRITICALITY Y/A N/A INITIAL ELECTRICITY N/A N/A E

COMMERCIAL OPER ATION N/A N/A i

D**

T l

(9/77) i ww o

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.. ~.. _, _ _ _. _ _. _ _ _ _ _.

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AVERAGE DA!Li UNIT POWER LEVEL i

50-334 DOCKET NO.

UNIT 372S Uni" Y1 DATE 2-4-81 D. R. %

COMPLETED BY 17.LEPHONE 412-443-530S MONTH Januari, 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe.Netj (Mwe Nec3 0

781-1 37 1

0 gg 785 3

0 19 791 4

0 20 776 0

23 735 5

0 756 6

22 7

23 752 0

707 0

24 3

0 474 9

,3 0

470 10 26 0

690 11 27 425 707 g2 23 803 731 13

,9 803 665 34 30 799 336 13 33 791 16 INSTRUCTIONS On this for:::st.!ist the average d:aly unit power !celin MWe. Net for each day in the repurring month. Compute to the r.esrest whvie megswatt.

(4/77)

50-334 I

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