ML20098F073: Difference between revisions

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=Text=
=Text=
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Arizona Public Service Company Septenber 17, 1984 ANPP-30536-TDS/TRB U. S. Nuclear Regulatory Commission
Arizona Public Service Company Septenber 17, 1984 ANPP-30536-TDS/TRB U. S. Nuclear Regulatory Commission
              . Region V Creekside Oaks Office Park 1450 Maria Lane - Suite 210 Walnut Creek, CA 94596-5368 Attention: Mr. T. W. Bishop, Director Division of Resident Reactor Projects and Engineering Programs
. Region V Creekside Oaks Office Park 1450 Maria Lane - Suite 210 Walnut Creek, CA 94596-5368 Attention: Mr. T. W. Bishop, Director Division of Resident Reactor Projects and Engineering Programs


==Subject:==
==Subject:==
Line 26: Line 25:


==Dear Sir:==
==Dear Sir:==
The NRC was notified of a potentially reportable deficiency in the referenced telephone conversation. At that time, it was estimated that a determination of reportability would be made within thirty (30) days.
The NRC was notified of a potentially reportable deficiency in the referenced telephone conversation. At that time, it was estimated that a determination of reportability would be made within thirty (30) days.
Due to the extensive investigation and evaluation required, an Interim Report is attached. It is now expected that this information will be finalized by October 19, 1984, at which time a complete report will be submitted.
Due to the extensive investigation and evaluation required, an Interim Report is attached.
It is now expected that this information will be finalized by October 19, 1984, at which time a complete report will be submitted.
Very truly yours,
Very truly yours,
[C       D E. E. Van B runt, Jr.
[C D
APS Vice President Nuclear Production ANPP Project Director EEVB/TRB/nj Attachment cc: See Page Two         G W 02 d3S tasi fjj ? "
E. E. Van B runt, Jr.
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APS Vice President Nuclear Production ANPP Project Director EEVB/TRB/nj Attachment cc: See Page Two G W 02 d3S tasi fjj ? "
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Mr. T. W. ' Bishop
Mr. T. W. ' Bishop
                      .~ DER 84-5 5 Page Two cc:           Richard DeYoung, Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Washington, D. C.                 20555 T. G. Woods,-Jr.
.~ DER 84-5 5 Page Two cc:
Richard DeYoung, Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Washington, D. C.
20555 T. G. Woods,-Jr.
D. B. Karner W. E. Ide D. B. Fasnacht-
D. B. Karner W. E. Ide D. B. Fasnacht-
                                    . A. C. Rogers L.' A. Souza D..E. Fowler.-
. A. C. Rogers L.' A. Souza D..E. Fowler.-
T. ' D. Shriver C. N. Russo J. Vorees J. R. Bynum J. M. Allen J. A. Brand A;   C. Gehr W. J. Stubblefield W. G. Bingham R. L. Patterson R. W. Welcher H. D. Foster
T. ' D. Shriver C. N. Russo J. Vorees J. R. Bynum J. M. Allen J. A. Brand A; C. Gehr W. J. Stubblefield W. G. Bingham R. L. Patterson R. W. Welcher H. D. Foster
                                    .D. R. Hawkinson L. E. Vorderbrueggen R. P. Zimmerman S. R. Froet L. Clyde M. Woods T. J. Bloom Records Center Institute of Nuclear Power Operations 1100 Circle 75 Parkway, Suite 1500 Atlanta, GA 30339 1
.D. R. Hawkinson L. E. Vorderbrueggen R. P. Zimmerman S. R. Froet L. Clyde M. Woods T. J. Bloom Records Center Institute of Nuclear Power Operations 1100 Circle 75 Parkway, Suite 1500 Atlanta, GA 30339 1
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L INTERIM REPORT     DER'84                                 POTENTIAL REPORTABLE DEPICIENCY ARIZONA PUBLIC SERVICE COMPANY (APS)
INTERIM REPORT DER'84 POTENTIAL REPORTABLE DEPICIENCY ARIZONA PUBLIC SERVICE COMPANY (APS)
PVNGS UNIT 1 I.   . Potential Problem NCR SJ-4607 Unqualified Poxboro Modules have been installed in the following QlE instrumentation. cabinets: (R Class Material)
PVNGS UNIT 1 I.
Plant Tag No.                 Description               PO Spec.
. Potential Problem NCR SJ-4607 Unqualified Poxboro Modules have been installed in the following QlE instrumentation. cabinets: (R Class Material)
IJSBACO2A'         Process Protective Cabinet Al       NM-001 lJSBBC02A           Process Protective Cabinet B1       NM-001 lJSBBC02B           Process Protective Cabinet B2       NM-001 lJSBACO2B           Process Protective Cabinet A2       NM-001 lJSBDC02A           Process Protective Cabinet D       NM-001 NCR SM-4778
Plant Tag No.
Description PO Spec.
IJSBACO2A' Process Protective Cabinet Al NM-001 lJSBBC02A Process Protective Cabinet B1 NM-001 lJSBBC02B Process Protective Cabinet B2 NM-001 lJSBACO2B Process Protective Cabinet A2 NM-001 lJSBDC02A Process Protective Cabinet D NM-001 NCR SM-4778
: a. In accordance with Combustion Engi,eering (C-E) serial number list, IEC-84-675, there appears to be four Poxboro modules, serial numbers 3647589, 3647581, 4712336, and 4712337, installed in Unit -2 instead of Unit 1.
: a. In accordance with Combustion Engi,eering (C-E) serial number list, IEC-84-675, there appears to be four Poxboro modules, serial numbers 3647589, 3647581, 4712336, and 4712337, installed in Unit -2 instead of Unit 1.
: b. A total of six Foxboro modules are installed in Unit 2 which are not on the C-E serial number list.
: b. A total of six Foxboro modules are installed in Unit 2 which are not on the C-E serial number list.
Note: This condition is similar to that identified in DER 83-73.
Note: This condition is similar to that identified in DER 83-73.
II. Approach To and Status Of Proposed Rasolution Bechtel Engineering is currently studying this problem to
II.
                  . determine reportability and technical justification for corrective action.-
Approach To and Status Of Proposed Rasolution Bechtel Engineering is currently studying this problem to
III. Projected Completion of Corrective Action and Submittal of the Final Report The co'plete evaluation and final report are forecast to be -
. determine reportability and technical justification for corrective action.-
III.
Projected Completion of Corrective Action and Submittal of the Final Report The co'plete evaluation and final report are forecast to be -
completed by October 19, 1984 l
completed by October 19, 1984 l
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Latest revision as of 06:56, 13 December 2024

Interim Deficiency Rept DER 84-55 Re Unqualified Foxboro Modules.Initially Reported on 840817.Due to Extensive Investigation & Evaluation Required,Final Rept Delayed Until 841019
ML20098F073
Person / Time
Site: Palo Verde 
Issue date: 09/17/1984
From: Van Brunt E
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To: Bishop T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
ANPP-30536-TDS, DER-84-55, NUDOCS 8410020288
Download: ML20098F073 (3)


Text

s.

Arizona Public Service Company Septenber 17, 1984 ANPP-30536-TDS/TRB U. S. Nuclear Regulatory Commission

. Region V Creekside Oaks Office Park 1450 Maria Lane - Suite 210 Walnut Creek, CA 94596-5368 Attention: Mr. T. W. Bishop, Director Division of Resident Reactor Projects and Engineering Programs

Subject:

Interim Report - DER 84-55 A 50.55(e) Potentially Reportable Deficiency Relating To Unqualified Foxboro Modules.

File: 84-019-026; D 4.33.2 Ref erence: Telephone Conversation between P. Narbut and T. Bradish on August 17, 1984

Dear Sir:

The NRC was notified of a potentially reportable deficiency in the referenced telephone conversation. At that time, it was estimated that a determination of reportability would be made within thirty (30) days.

Due to the extensive investigation and evaluation required, an Interim Report is attached.

It is now expected that this information will be finalized by October 19, 1984, at which time a complete report will be submitted.

Very truly yours,

[C D

E. E. Van B runt, Jr.

APS Vice President Nuclear Production ANPP Project Director EEVB/TRB/nj Attachment cc: See Page Two G W 02 d3S tasi fjj ? "

011 turf 8410020288 840917 PDR ADOCK 05000528

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Mr. T. W. ' Bishop

.~ DER 84-5 5 Page Two cc:

Richard DeYoung, Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Washington, D. C.

20555 T. G. Woods,-Jr.

D. B. Karner W. E. Ide D. B. Fasnacht-

. A. C. Rogers L.' A. Souza D..E. Fowler.-

T. ' D. Shriver C. N. Russo J. Vorees J. R. Bynum J. M. Allen J. A. Brand A; C. Gehr W. J. Stubblefield W. G. Bingham R. L. Patterson R. W. Welcher H. D. Foster

.D. R. Hawkinson L. E. Vorderbrueggen R. P. Zimmerman S. R. Froet L. Clyde M. Woods T. J. Bloom Records Center Institute of Nuclear Power Operations 1100 Circle 75 Parkway, Suite 1500 Atlanta, GA 30339 1

l'

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INTERIM REPORT DER'84 POTENTIAL REPORTABLE DEPICIENCY ARIZONA PUBLIC SERVICE COMPANY (APS)

PVNGS UNIT 1 I.

. Potential Problem NCR SJ-4607 Unqualified Poxboro Modules have been installed in the following QlE instrumentation. cabinets: (R Class Material)

Plant Tag No.

Description PO Spec.

IJSBACO2A' Process Protective Cabinet Al NM-001 lJSBBC02A Process Protective Cabinet B1 NM-001 lJSBBC02B Process Protective Cabinet B2 NM-001 lJSBACO2B Process Protective Cabinet A2 NM-001 lJSBDC02A Process Protective Cabinet D NM-001 NCR SM-4778

a. In accordance with Combustion Engi,eering (C-E) serial number list, IEC-84-675, there appears to be four Poxboro modules, serial numbers 3647589, 3647581, 4712336, and 4712337, installed in Unit -2 instead of Unit 1.
b. A total of six Foxboro modules are installed in Unit 2 which are not on the C-E serial number list.

Note: This condition is similar to that identified in DER 83-73.

II.

Approach To and Status Of Proposed Rasolution Bechtel Engineering is currently studying this problem to

. determine reportability and technical justification for corrective action.-

III.

Projected Completion of Corrective Action and Submittal of the Final Report The co'plete evaluation and final report are forecast to be -

completed by October 19, 1984 l

t f

(-

C

-