ENS 40858: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by Mark Hawes)
 
(Created page by program invented by StriderTol)
 
Line 16: Line 16:
| event date = 07/08/2004 22:32 CDT
| event date = 07/08/2004 22:32 CDT
| last update date = 07/09/2004
| last update date = 07/09/2004
| title = Reactor Scram Due To A Turbine Generator Load Rejection Signal
| title = Reactor Scram Due to a Turbine Generator Load Rejection Signal
| event text = The following information was received from the licensee via facsimile:
| event text = The following information was received from the licensee via facsimile:
On 7/08/2004 at approximately 2232 hours CDT, Browns Ferry Unit 2 scrammed due to a Turbine Generator Load Reject Signal.  All systems responded as required to the scram signal.  No ECCS initiations occurred as a result of this event.  Reactor Water Level lowered to the Low Level setpoint which generated a redundant SCRAM signal and initiated the Primary Containment Isolation System (PCIS) function for PCIS groups 2 (Primary Containment), 3 (RWCU) [Reactor Water Clean Up], 6 (Secondary Containment), and 8 (TIP system) [Transverse Incore Probe].  As expected, Main Steam Relief Valves (MSRVs) opened due to the high reactor pressure (maximum value observed was 1137 psig) as a result of the Main Turbine / Generator Trip.  Reactor Water level was restored to normal via the Reactor Feedwater system and all PCIS isolations have been reset.  The cause of the Load Reject Signal is still under investigation at this time.
On 7/08/2004 at approximately 2232 hours CDT, Browns Ferry Unit 2 scrammed due to a Turbine Generator Load Reject Signal.  All systems responded as required to the scram signal.  No ECCS initiations occurred as a result of this event.  Reactor Water Level lowered to the Low Level setpoint which generated a redundant SCRAM signal and initiated the Primary Containment Isolation System (PCIS) function for PCIS groups 2 (Primary Containment), 3 (RWCU) [Reactor Water Clean Up], 6 (Secondary Containment), and 8 (TIP system) [Transverse Incore Probe].  As expected, Main Steam Relief Valves (MSRVs) opened due to the high reactor pressure (maximum value observed was 1137 psig) as a result of the Main Turbine / Generator Trip.  Reactor Water level was restored to normal via the Reactor Feedwater system and all PCIS isolations have been reset.  The cause of the Load Reject Signal is still under investigation at this time.

Latest revision as of 21:23, 1 March 2018

ENS 40858 +/-
Where
Browns Ferry Tennessee Valley Authority icon.png
Alabama (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.18 h-0.0492 days <br />-0.00702 weeks <br />-0.00162 months <br />)
Opened: Chris Vaughn
02:21 Jul 9, 2004
NRC Officer: Howie Crouch
Last Updated: Jul 9, 2004
40858 - NRC Website
Loading map...