ENS 40858: Difference between revisions
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StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
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| event date = 07/08/2004 22:32 CDT | | event date = 07/08/2004 22:32 CDT | ||
| last update date = 07/09/2004 | | last update date = 07/09/2004 | ||
| title = Reactor Scram Due | | title = Reactor Scram Due to a Turbine Generator Load Rejection Signal | ||
| event text = The following information was received from the licensee via facsimile: | | event text = The following information was received from the licensee via facsimile: | ||
On 7/08/2004 at approximately 2232 hours CDT, Browns Ferry Unit 2 scrammed due to a Turbine Generator Load Reject Signal. All systems responded as required to the scram signal. No ECCS initiations occurred as a result of this event. Reactor Water Level lowered to the Low Level setpoint which generated a redundant SCRAM signal and initiated the Primary Containment Isolation System (PCIS) function for PCIS groups 2 (Primary Containment), 3 (RWCU) [Reactor Water Clean Up], 6 (Secondary Containment), and 8 (TIP system) [Transverse Incore Probe]. As expected, Main Steam Relief Valves (MSRVs) opened due to the high reactor pressure (maximum value observed was 1137 psig) as a result of the Main Turbine / Generator Trip. Reactor Water level was restored to normal via the Reactor Feedwater system and all PCIS isolations have been reset. The cause of the Load Reject Signal is still under investigation at this time. | On 7/08/2004 at approximately 2232 hours CDT, Browns Ferry Unit 2 scrammed due to a Turbine Generator Load Reject Signal. All systems responded as required to the scram signal. No ECCS initiations occurred as a result of this event. Reactor Water Level lowered to the Low Level setpoint which generated a redundant SCRAM signal and initiated the Primary Containment Isolation System (PCIS) function for PCIS groups 2 (Primary Containment), 3 (RWCU) [Reactor Water Clean Up], 6 (Secondary Containment), and 8 (TIP system) [Transverse Incore Probe]. As expected, Main Steam Relief Valves (MSRVs) opened due to the high reactor pressure (maximum value observed was 1137 psig) as a result of the Main Turbine / Generator Trip. Reactor Water level was restored to normal via the Reactor Feedwater system and all PCIS isolations have been reset. The cause of the Load Reject Signal is still under investigation at this time. |
Latest revision as of 21:23, 1 March 2018
Where | |
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Browns Ferry Alabama (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.18 h-0.0492 days <br />-0.00702 weeks <br />-0.00162 months <br />) | |
Opened: | Chris Vaughn 02:21 Jul 9, 2004 |
NRC Officer: | Howie Crouch |
Last Updated: | Jul 9, 2004 |
40858 - NRC Website
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