ENS 41997: Difference between revisions

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| event date = 09/17/2005 11:29 CDT
| event date = 09/17/2005 11:29 CDT
| last update date = 09/17/2005
| last update date = 09/17/2005
| title = Reactor Scram Due To Maintenance
| title = Reactor Scram Due to Maintenance
| event text = On 09/17/2005 at 1129 CDT, Browns Ferry Unit 3 reactor automatically scrammed due to the trip of the main generator turbine on low main condenser vacuum.  Prior to the trip, the unit was operating at reduced power (74 percent) and maintenance was in progress to repair in place a secondary plant moisture separator level control valve. This maintenance activity resulted in the low condenser vacuum condition.
| event text = On 09/17/2005 at 1129 CDT, Browns Ferry Unit 3 reactor automatically scrammed due to the trip of the main generator turbine on low main condenser vacuum.  Prior to the trip, the unit was operating at reduced power (74 percent) and maintenance was in progress to repair in place a secondary plant moisture separator level control valve. This maintenance activity resulted in the low condenser vacuum condition.
Plant response to the scram was as expected.  Post-scram transient RPV low water level caused a valid automatic initiation of primary containment isolation (PCIS) valves group 2 (containment sumps and shutdown cooling valves), group 3 (reactor water cleanup system), group 6 (ventilation systems, including initiation of standby gas treatment and control room emergency ventilation systems), and group 8 (traversing in-core probe system).
Plant response to the scram was as expected.  Post-scram transient RPV low water level caused a valid automatic initiation of primary containment isolation (PCIS) valves group 2 (containment sumps and shutdown cooling valves), group 3 (reactor water cleanup system), group 6 (ventilation systems, including initiation of standby gas treatment and control room emergency ventilation systems), and group 8 (traversing in-core probe system).

Latest revision as of 21:20, 1 March 2018

ENS 41997 +/-
Where
Browns Ferry Tennessee Valley Authority icon.png
Alabama (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-0.37 h-0.0154 days <br />-0.0022 weeks <br />-5.06826e-4 months <br />)
Opened: Mike Morrow
16:07 Sep 17, 2005
NRC Officer: Bill Gott
Last Updated: Sep 17, 2005
41997 - NRC Website
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