ENS 42887: Difference between revisions
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StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
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| event date = 10/07/2006 18:02 EDT | | event date = 10/07/2006 18:02 EDT | ||
| last update date = 10/08/2006 | | last update date = 10/08/2006 | ||
| title = Unusual Event - Loss | | title = Unusual Event - Loss of Containment Integrity | ||
| event text = During testing, a small crack (3"- 4" axial crack) was identified on a return line to the torus for both HPCI and RCIC (steam driven ECCS systems). The valve upstream of the leak has been closed, however, the leak is still unisolable between that valve and the torus. This plant condition does not threaten public safety. | | event text = During testing, a small crack (3"- 4" axial crack) was identified on a return line to the torus for both HPCI and RCIC (steam driven ECCS systems). The valve upstream of the leak has been closed, however, the leak is still unisolable between that valve and the torus. This plant condition does not threaten public safety. | ||
The licensee notified the NRC Resident Inspector, as well as State and local agencies. | The licensee notified the NRC Resident Inspector, as well as State and local agencies. |
Latest revision as of 22:17, 1 March 2018
Where | |
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Peach Bottom Pennsylvania (NRC Region 1) | |
Reporting | |
Emergency class: | Unusual Event |
10 CFR 50.72(a) (1) (i), Emergency Class Declaration | |
Time - Person (Reporting Time:+-3.8 h-0.158 days <br />-0.0226 weeks <br />-0.00521 months <br />) | |
Opened: | Mike Berg 18:14 Oct 7, 2006 |
NRC Officer: | John Knoke |
Last Updated: | Oct 8, 2006 |
42887 - NRC Website
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