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APPENDIX B
                                                            APPENDIX B
U.S. NUCLEAR REGULATORY COMMISSION
                                              U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
                                                                REGION IV
inspection Report:
              inspection Report:           50-458/92-34
50-458/92-34
              Operating License: HPF-47
Operating License: HPF-47
              Licensee:   Gulf States Utilities
Licensee:
                          P.O. Box 220                                                         4
Gulf States Utilities
                                                                                                I
P.O. Box 220
                          St. Francisville, Louisiana 70775-0220
4
              Facility Name:           River Bend Station                 -
St. Francisville, Louisiana 70775-0220
                                                                                                1
Facility Name:
              Inspection At:           St. Francisville, Louisiana                             l
River Bend Station
              Inspection Conducted:             November 8 through December 19, 1992
-
              Inspectors:     W. F. Smith, Senior Resident inspector
1
                              D. P. Loveless, Resident inspector
Inspection At:
                              R. H. Bernhard, Senior Resident inspector,
St. Francisville, Louisiana
                                      Grand Gulf Nuclear Station, Region 11
l
                              J. M. Keeton, Examiner, Operational Programs Section,
Inspection Conducted:
                                J Di ision of Reactor Safety
November 8 through December 19, 1992
                                                                                I   >
Inspectors:
              Approved:       '
W. F. Smith, Senior Resident inspector
                                      .  gliardo, Chlef, Project Section C     Ifa
D. P. Loveless, Resident inspector
              inspection Summary
R. H. Bernhard, Senior Resident inspector,
              Areas inspected:           Routine, unannounced inspection of onsite response to
Grand Gulf Nuclear Station, Region 11
              events, operational safety verification,- maintenance and surveillance-
J. M. Keeton, Examiner, Operational Programs Section,
              observations, open item followup, and onsite review of a licensee event
J Di ision of Reactor Safety
              report.
I
              Results:
>
              e      Overall, the licensee's responses to operational events during the
Approved:
                      report period were very good (paragraph 2.3).
gliardo, Chlef, Project Section C
              e      The operators' response to the motor trip on Chiller B was noteworthy.
Ifa
                      They entered the shutdown evolution in an expeditious manner and used
'
                      good judgement in utilizing the available equipment to maintain the
.
                      control room atmosphere (paragraph 2.1).
inspection Summary
              e       The licensee's response to the November 24 reactor scram was very good,
Areas inspected:
                      including the posttrip review and the facility review committee response
Routine, unannounced inspection of onsite response to
                      (paragraph 2.2).
events, operational safety verification,- maintenance and surveillance-
                                                                                              ,
observations, open item followup, and onsite review of a licensee event
                -9301150056 9301og
report.
                gDR- ADOCK 05000450
Results:
                                            PDR
Overall, the licensee's responses to operational events during the
..   _
e
      . .-           .       - . .       _-             - .
report period were very good (paragraph 2.3).
                                                                      .- -   - -
The operators' response to the motor trip on Chiller B was noteworthy.
e
They entered the shutdown evolution in an expeditious manner and used
good judgement in utilizing the available equipment to maintain the
control room atmosphere (paragraph 2.1).
e
The licensee's response to the November 24 reactor scram was very good,
including the posttrip review and the facility review committee response
(paragraph 2.2).
,
-9301150056 9301og
gDR- ADOCK 05000450
PDR
..
. .-
.
- . .
_-
- .
.- -
- -
_


      _ _ _ _ _ _                                     _ _ . _ . . - _ _ _ _ _ _ _                                                             _ _ ___. _ _ _ .
_ _ _ _ _ _
                                                                                                                  -2-
_ _ . _ . . - _ _ _ _ _ _ _
                  e                       Overall, the licensee operated the facility in a satisf actory manner
_ _ ___. _ _ _ .
                                            (paragraph 3.6).
-2-
                  e                      The performance of the operators during the November 17, 1992, reactor
e
                                            shutdown and planned scram was very good (paragraph 3.1).
Overall, the licensee operated the facility in a satisf actory manner
                  e                        in general, plant housekeeping, including radiological housekeeping, has
(paragraph 3.6).
                                            improved over the inspection period. However, oil leaks, oil pooling
The performance of the operators during the November 17, 1992, reactor
                                          and a Jacket water leak identified on the Division I standby diesel
e
                                          generator were examples of poor housekeeping (paragraph 3.2).
shutdown and planned scram was very good (paragraph 3.1).
                  *                      One violation was identified for failure to place the reactor core
in general, plant housekeeping, including radiological housekeeping, has
                                            isolation cooling system in service prior to exceeding 150 psig reactor
e
                                          pressure as required by Technical Specification 3.0.4 (paragraph 3.3).                                                                               ,
improved over the inspection period.
                  *                      The operators' performance during the December 6 shutdown was exemplary,
However, oil leaks, oil pooling
                                          with one exception. A second violation was identified for failure to
and a Jacket water leak identified on the Division I standby diesel
                                            follow the action statements of Technical Specifications 3.3.1 and
generator were examples of poor housekeeping (paragraph 3.2).
                                          3.3.7.6 when the intermediate range monitors and the source range                                                                                     ,
One violation was identified for failure to place the reactor core
                                          monitors, respectively, had not been properly tested to demonstrate
*
                                          operability following a plant shutdown (paragraph 3.4).
isolation cooling system in service prior to exceeding 150 psig reactor
                  *                      A negative trend was identified which involved operators not heeding
pressure as required by Technical Specification 3.0.4 (paragraph 3.3).
                                          procedures and not complying with Technical Specification requirements
,
                                            (paragraph 3.5),
The operators' performance during the December 6 shutdown was exemplary,
                  e                      Overall, the licensee's performance in maintenance activities observed
*
                                          during this inspection period was adequate (paragraph 4.3),
with one exception. A second violation was identified for failure to
                  e                      One violation was identified for failure to establish measures to
follow the action statements of Technical Specifications 3.3.1 and
                                            identify that the filter elements in a safety-related unit cooler had
3.3.7.6 when the intermediate range monitors and the source range
                                          deteriorated and were breaking down and clogging the cooling coils
                                            (paragraph 4.1).
                  *                        The licensee's failure to promptly assess the status of five similar
                                            safety-related unit coolers, following the identification of preventive
,
,
                                          maintenance problems in Unit Cooler lHVR*UC5, was considered a weakness
monitors, respectively, had not been properly tested to demonstrate
operability following a plant shutdown (paragraph 3.4).
A negative trend was identified which involved operators not heeding
*
procedures and not complying with Technical Specification requirements
(paragraph 3.5),
Overall, the licensee's performance in maintenance activities observed
e
during this inspection period was adequate (paragraph 4.3),
e
One violation was identified for failure to establish measures to
identify that the filter elements in a safety-related unit cooler had
deteriorated and were breaking down and clogging the cooling coils
(paragraph 4.1).
The licensee's failure to promptly assess the status of five similar
*
safety-related unit coolers, following the identification of preventive
,
maintenance problems in Unit Cooler lHVR*UC5, was considered a weakness
l~
l~
                                            (paragraph 4.1).
(paragraph 4.1).
                  *                        Very good work controls were observed during the replacement of an
Very good work controls were observed during the replacement of an
*
environmentally qualified switch (paragraph 4.2).
,
,
                                            environmentally qualified switch (paragraph 4.2).
t
t
                  e                        Overall, surveillance activities were performed in a commendable manner
Overall, surveillance activities were performed in a commendable manner
                                            during this inspection period (paragraph 5.2).
e
                  *                        Operator knowledge and control of testing activities were good during
during this inspection period (paragraph 5.2).
                                            the performance of surveillance testing of the Division I standby diesel
Operator knowledge and control of testing activities were good during
                                            generator (paragraph 5.1).
*
                                                                                                                                                                                                '
the performance of surveillance testing of the Division I standby diesel
generator (paragraph 5.1).
l
l
'
i
i
I
I
  ~-4               . . . . _ . , , . - - . . - . . .       . _ _ _ - , , . . . , _ , , , . . , . , - - - - , , ,     --_--,,...,,-_m.---,_,-             . - - .-.-r ~ . . . . , , . . .-_...
~-4
. - . . -
. . . . _ . , , . - - . . - . . .
. _ _ _ - , , . . . , _ , , , . . , . , - - - - , , ,
--_--,,...,,-_m.---,_,-
. - -
.-.-r
~ . . . . , , . .
. - _ . . .


      .- -_ . - - . .             .--   ~         _. -.   . .. .     .     . -
.- -_ . - - . .
  l
.--
    '
~
                        .
_. -.
                                                        _3
.
                                                                                                ,
.. .
        o             The licensee evaluation of the certification of_ a test engineer and test
.
                    practices was appropriate and reasonably supported (paragraph 6.1).
. -
        e            The licensee adequately evaluated potential unmonitored release paths at
'
                    River Bend Station (paragraph 6.2).
l
        *            . censee Event Report 92-004 was a good quality report and the
.
                      i censee's corrective actions appeared to be adequate to prevent
_3
                    recuitence (paragraph 7.1).
,
        Summary of Inspection findings:
o
        e           Violation 458/92034-1 was opened (paragraph 3.3).
The licensee evaluation of the certification of_ a test engineer and test
        *           V;olation 458/92034-2 was opened (paragraph 3.4).
practices was appropriate and reasonably supported (paragraph 6.1).
        e           Violation 458/92034-3 was opened (paragraph 4.1).
The licensee adequately evaluated potential unmonitored release paths at
        *           Licensee Event Report 458/92-004 was closed (paragraph 7.1).
e
        Attachments:
River Bend Station (paragraph 6.2).
        *-         Attachment 1 - Persons Contacted and r       Meeting
. censee Event Report 92-004 was a good quality report and the
*
i censee's corrective actions appeared to be adequate to prevent
recuitence (paragraph 7.1).
Summary of Inspection findings:
e
Violation 458/92034-1 was opened (paragraph 3.3).
*
V;olation 458/92034-2 was opened (paragraph 3.4).
e
Violation 458/92034-3 was opened (paragraph 4.1).
*
Licensee Event Report 458/92-004 was closed (paragraph 7.1).
Attachments:
*-
Attachment 1 - Persons Contacted and r
Meeting
.
.


        _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _
_ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _
      .
.
                                                                                      -4-
-4-
                                                                                    DETAILS
DETAILS
.
1 PLANT STATUS
At the beginning of this inspection period, the plant was operating at
100 percent power.
On November 10, 1992, a plant shutdown was initiated as required by 72chnical
Specification 3.0.3 when the only operable control room ventilation chiller
tripped.
Howeve , the shutdown was terminated at 76 percent power when the
chiller was restarted, and full power operation was resumed on November 11.
_
On November 16, the licensee commenced a plant shutdown to Operational
Condition 3 (hot shutdown) to facilitate planned Outage 92-03. On
November 24, the plant was restarted, but the reactor scrammed from 96 percent
.
.
                                      1 PLANT STATUS
power on high neutron flux caused by a main turbine electrohydraulic control
                                      At the beginning of this inspection period, the plant was operating at
"s
                                        100 percent power.
system transient.
                                      On November 10, 1992, a plant shutdown was initiated as required by 72chnical
lhe startup was resumed on November 25, and by November 27,
                                      Specification 3.0.3 when the only operable control room ventilation chiller
' 3
                                        tripped. Howeve , the shutdown was terminated at 76 percent power when the
the pisnt was operating at 100 percent power.
                                        chiller was restarted, and full power operation was resumed on November 11.            _
'
                                      On November 16, the licensee commenced a plant shutdown to Operational
On December 6, the plant was shut down and cooled to ambient conditions for
                                        Condition 3 (hot shutdown) to facilitate planned Outage 92-03. On
planned Outage 92-04 to replace a failed reactor recirculation pump seal.
                                        November 24, the plant was restarted, but the reactor scrammed from 96 percent
The
  .
plant was restarted on December 13 and resumed full power operation on
                                        power on high neutron flux caused by a main turbine electrohydraulic control
December 16.
"s                                       system transient. lhe startup was resumed on November 25, and by November 27,
At the end of this inspection period, the plant was operating at 100 percent
  ' 3                                     the pisnt was operating at 100 percent power.
power.
                                        On December 6, the plant was shut down and cooled to ambient conditions for
2 ONSITE RESP 0i4SE TO EVENTS (93702)
    '
2.1
                                          planned Outage 92-04 to replace a failed reactor recirculation pump seal. The
Inoperability of Both Control Room Ventilation Systems
                                          plant was restarted on December 13 and resumed full power operation on
[
                                          December 16.
At 12:58 p.m., on November 10, 1992, the Division 11 control room ventilation
                                          At the end of this inspection period, the plant was operating at 100 percent
system Chiller 18 tripped on motor overload.
                                          power.
At the time, the Division I
                                            2 ONSITE RESP 0i4SE TO EVENTS (93702)
system was inoperable because maintenance was being performed on the air
                                            2.1     Inoperability of Both Control Room Ventilation Systems                     [
handling unit heaters.
                                            At 12:58 p.m., on November 10, 1992, the Division 11 control room ventilation
In addition, Chiller D, the alternate Division 11
                                              system Chiller 18 tripped on motor overload. At the time, the Division I
chiller, was inoperable because of an unresolved tripping problem that was
                                              system was inoperable because maintenance was being performed on the air
identified on October 18.
                                              handling unit heaters. In addition, Chiller D, the alternate Division 11
At 1:45 p.m.,
                                              chiller, was inoperable because of an unresolved tripping problem that was
a plant shutdown was initiated as requir2d by Technical
                                                identified on October 18.
Specification 3.0.3.
                                              At 1:45 p.m., a plant shutdown was initiated as requir2d by Technical
To maintain the control room atmosphere, Chiller D was
                                                Specification 3.0.3. To maintain the control room atmosphere, Chiller D was
placed in service, ever though it was technically inoperable because of
                                                placed in service, ever though it was technically inoperable because of
spurious trips.
                                                spurious trips.   The matsr on Chiller B was checked for grounds and short
The matsr on Chiller B was checked for grounds and short
                                                circuits, but no problems were found.     bpar checking the motor control
circuits, but no problems were found.
                                                breaker, the elech !cian found a loose pleg on the overcurrent trip device.
bpar checking the motor control
                                                When the plug wa: properly installed, the breaker performed as designed.
breaker, the elech !cian found a loose pleg on the overcurrent trip device.
                                                At 3:32 p.m., Chiller B was restored to service and the plant shutdown was
When the plug wa: properly installed, the breaker performed as designed.
                                                  terminated at about 76 percent power. By 2:27 a.m., on November 11, full
At 3:32 p.m., Chiller B was restored to service and the plant shutdown was
                                                  power operation was resumed. The licensee reported the event at 2:02 p.m., on
terminated at about 76 percent power.
By 2:27 a.m.,
on November 11, full
power operation was resumed. The licensee reported the event at 2:02 p.m., on


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  9
9
                                              -5-
-5-
        November 10, as required by 10 CFR Part 50.72.     They also initiated Condition
November 10, as required by 10 CFR Part 50.72.
        Report 92-0898 to document the trip of Chiller B and the shutdown event.
They also initiated Condition
        The inspector examined a sin;ilar breaker and noted that the overcurrent ! ip
Report 92-0898 to document the trip of Chiller B and the shutdown event.
        device plug, when-properly irstalled, snapped and locked in place. The
The inspector examined a sin;ilar breaker and noted that the overcurrent ! ip
        inspector questioned how the plug could come loose, and the licensee's
device plug, when-properly irstalled, snapped and locked in place. The
        representative stated that the positive locking feature of the plug would
inspector questioned how the plug could come loose, and the licensee's
        prevent the plug from coming loose and that there was an independent
representative stated that the positive locking feature of the plug would
        verification signed off whenever the plug was installed. In this case, the
prevent the plug from coming loose and that there was an independent
        installer apparently failed to snap the plug in place, and the independe'nt
verification signed off whenever the plug was installed.
        verifier did not notice the error. The licen ce informed the inspectnr that
In this case, the
        44 similar safety-related breaker'overcurrent trip device plugs were chec hd
installer apparently failed to snap the plug in place, and the independe'nt
        and they were all aroperly installed. Because this'was the only time that
verifier did not notice the error. The licen ce informed the inspectnr that
        this type of plug mad come loose, and no others were found, the licensee
44 similar safety-related breaker'overcurrent trip device plugs were chec hd
        considered this to be an isolated incident. The electricians that had
and they were all aroperly installed.
        previously installed the plug in the Chiller 8 controller were counselled on
Because this'was the only time that
        this event. No further corrective action was taken.
this type of plug mad come loose, and no others were found, the licensee
        2.2 Reactor Scram
considered this to be an isolated incident. The electricians that had
        On November 24, 1992, the reactor scrammed on high neutron flux as indicated
previously installed the plug in the Chiller 8 controller were counselled on
        by the average power range monitors. A power ascension was in progress when
this event.
        the electrohydraulic control system pressure regulator automatically shifted
No further corrective action was taken.
        from the manually selected Channel B to Channel A. A large deviation existed
2.2 Reactor Scram
        between the channels prior to the automatic transfer. Therefore, the transfer
On November 24, 1992, the reactor scrammed on high neutron flux as indicated
I       caused the main turbine control-valves to change position from'approximately
by the average power range monitors. A power ascension was in progress when
        35 percent open to 23 percent open. The resulting pressure surge in the
the electrohydraulic control system pressure regulator automatically shifted
        reactor vessel caused a momentary collapse of voids in the reactor, causing an
from the manually selected Channel B to Channel A.
        indicated power increase to greater than the 118 percent high neutron flux
A large deviation existed
        scram setpoint. The inspector was notified and reported to the control room
between the channels prior to the automatic transfer.
Therefore, the transfer
I
caused the main turbine control-valves to change position from'approximately
35 percent open to 23 percent open.
The resulting pressure surge in the
reactor vessel caused a momentary collapse of voids in the reactor, causing an
indicated power increase to greater than the 118 percent high neutron flux
scram setpoint. The inspector was notified and reported to the control room
where he determined that the operators had brought the plant to a stable
l
l
        where he determined that the operators had brought the plant to a stable
condition.
        condition.
The licensee reviewed the event and determined that the pressure regulator
        The licensee reviewed the event and determined that the pressure regulator
circuit was designed to automatically transfer from one channel to the other
        circuit was designed to automatically transfer from one channel to the other
in the event of a rapid failure of one channel. This function was not
        in the event of a rapid failure of one channel. This function was not
intended to provide a smooth automatic transfer when the channels were slowly
        intended to provide a smooth automatic transfer when the channels were slowly
drifting apart, as occurred during this event.
        drifting apart, as occurred during this event.     The licensee found that the
The licensee found that the
        Channel A pressure amplifier card had been slowly drifting out' of calibration.
Channel A pressure amplifier card had been slowly drifting out' of calibration.
        This card was replaced.
This card was replaced.
        The inspector reviewed the posttrip review data package. All other plant
The inspector reviewed the posttrip review data package. All other plant
        systems were determined to have functioned properly.     Several _ items were
systems were determined to have functioned properly.
        reviewed in depth by licensee personnel to verify their accuracy. The
Several _ items were
        inspector observed the facility review committee meetings held to discuss the
reviewed in depth by licensee personnel to verify their accuracy. The
        event and_the readiness to restart the plant.     The questions raised by the
inspector observed the facility review committee meetings held to discuss the
        committee members-were of.high quality and were responded to prior to.an
event and_the readiness to restart the plant.
        authorization to restart. The overall licensee response to the scram was
The questions raised by the
        considered very good.
committee members-were of.high quality and were responded to prior to.an
authorization to restart. The overall licensee response to the scram was
considered very good.
L
L
                                                                                        i
.
..
.
.
i


                                                                                                    _ _ _
_
                                                          -6-
_ _
        During the subsequent startup, the licensee monitored the channel outputs on
-6-
          the emergency response information system to observe any drift. The channels
During the subsequent startup, the licensee monitored the channel outputs on
          continued to drift apart during pressure increases. Each time the licensee
the emergency response information system to observe any drift. The channels
          adjusted the gain to bring the channels back together. During planned
continued to drift apart during pressure increases.
          Outage 92-04, the licensee performed additional troubleshooting of the
Each time the licensee
          pressure regulator circuits. The technicians found that the Channel B
adjusted the gain to bring the channels back together.
          pressure transmitter was not repeatable during calibration. This transmitter
During planned
          was replaced.
Outage 92-04, the licensee performed additional troubleshooting of the
          The River Bend Station Updated Safety Analysis Report, Chapter 15.2, " Increase
pressure regulator circuits.
,            n, Acactor Pressure, ps.iui tca a failure of the pressure regulator.       This                 _
The technicians found that the Channel B
            event is referred to as an "ar.ticipated operatio.nal transient." Therefore,
pressure transmitter was not repeatable during calibration.
            the safety significance of thia failure was low. The licensee was continuing
This transmitter
            to investigate the problem and work with the vendor at the end of this
was replaced.
              inspection period. ihe corrective actions will be reviewed further with the
The River Bend Station Updated Safety Analysis Report, Chapter 15.2, " Increase
              issuance of the licensee event report.
n, Acactor Pressure,
              2.3 Conclusions
ps.iui tca a failure of the pressure regulator.
              e      Overall, the licensee's response to operational events during the report
This
                    period was very good.
,
              *      The operators' response to the motor trip on Chiller B was noteworthy.
event is referred to as an "ar.ticipated operatio.nal transient." Therefore,
                      They entered the shutdown evolution in an expeditious manner and used
_
                      good judgement in utilizing the available equipment to maintain the
the safety significance of thia failure was low.
                      control room atmosphere.
The licensee was continuing
              e      The licensee's response to the November 24 reactor scram was very good,
to investigate the problem and work with the vendor at the end of this
                      including the posttrip review and the facility review committee's
inspection period.
                      evaluation.                                                                               _
ihe corrective actions will be reviewed further with the
              3 OPERATIONAL SAFETY VERIFICATION (71707)
issuance of the licensee event report.
              The objectives of this inspection were to ensure that this facility was being
2.3 Conclusions
              operated safely and in conformance with regulatory requirements and to ensure
Overall, the licensee's response to operational events during the report
              that the licensee's management controls were effectively discharging the
e
              licensee's responsibilities for continued safe operation.
period was very good.
              3.1 Control Room Observations
The operators' response to the motor trip on Chiller B was noteworthy.
              On November 17, the inspectors monitored portions of control room operations
*
              during the shutdown of the plant for planned Outage 92-03. The primary
They entered the shutdown evolution in an expeditious manner and used
              purpose of the outage was to repair the drywell pedestal sump pumps. The
good judgement in utilizing the available equipment to maintain the
                licensee discovered both pumps were not functional when unidentified leakage
control room atmosphere.
                began to fill the sump. Details on the issue were documented in paragraph 2.4
The licensee's response to the November 24 reactor scram was very good,
                of NRC Inspection Report 50-458/92-32.
e
                The reactor was manually scrammed from '9.5 percent power, as delineated in
including the posttrip review and the facility review committee's
                the normal shutdown procedure. The opt       , es executed the appropriate actions
evaluation.
  . . . - . .
_
                  .               _     _     _ _ __ -               __                               ____
3 OPERATIONAL SAFETY VERIFICATION (71707)
The objectives of this inspection were to ensure that this facility was being
operated safely and in conformance with regulatory requirements and to ensure
that the licensee's management controls were effectively discharging the
licensee's responsibilities for continued safe operation.
3.1 Control Room Observations
On November 17, the inspectors monitored portions of control room operations
during the shutdown of the plant for planned Outage 92-03.
The primary
purpose of the outage was to repair the drywell pedestal sump pumps.
The
licensee discovered both pumps were not functional when unidentified leakage
began to fill the sump. Details on the issue were documented in paragraph 2.4
of NRC Inspection Report 50-458/92-32.
The reactor was manually scrammed from '9.5 percent power, as delineated in
the normal shutdown procedure. The opt
es executed the appropriate actions
,
. . .
- . .
.
_
_
_ _ __ -
__
____


. - -                     _ _ _ _ _ _ _ _ _
. - -
                                                -7-
_ _ _ _ _ _ _ _ _
      in response to the scram. The applicable emergency operating procedure was
-7-
      entered when reactor vessel water level shrank to Level 3, but in recovering
in response to the scram.
      level, manipulation of the feedwater controls resulted in slightly overfeeding
The applicable emergency operating procedure was
      the reactor, which caused a high level trip of the operating feedwater pump.
entered when reactor vessel water level shrank to Level 3, but in recovering
      The feedwater pump was promptly restored to service, and the shutdown was
level, manipulation of the feedwater controls resulted in slightly overfeeding
      completed without incident.
the reactor, which caused a high level trip of the operating feedwater pump.
      The licensee explained that, although the reactor vessel level was optimized
The feedwater pump was promptly restored to service, and the shutdown was
      just prior to the scram, compensation for normal shrink and preventing the
completed without incident.
      feedwater system from overfeeding has been difficult for some of the less
The licensee explained that, although the reactor vessel level was optimized
      experienced operators. The licensee had just issued a change to System
just prior to the scram, compensation for normal shrink and preventing the
      Opar e ing Procedure SOP-0009, " Reactor Feedwater System," on November 11,
feedwater system from overfeeding has been difficult for some of the less
      providing specific guidance for the operators during this type of feedwater
experienced operators. The licensee had just issued a change to System
      transient and has been in the process of training the operators on feedwater
Opar e ing Procedure SOP-0009, " Reactor Feedwater System," on November 11,
      transient response during routine requalification training.
providing specific guidance for the operators during this type of feedwater
      Overall, operator performance during the shutdown was very good.
transient and has been in the process of training the operators on feedwater
      3.2 Plant Tours
transient response during routine requalification training.
      On December 1, 1992, the inspector toured the diesel generator building. The
Overall, operator performance during the shutdown was very good.
        inspector noted that the Division I diesel had a lubricating oil leak on the
3.2 Plant Tours
      strainer. Although this leak had been previously identified by the licensee,
On December 1, 1992, the inspector toured the diesel generator building. The
      oil had flowed through the absorbent cloths that had been laid down and was
inspector noted that the Division I diesel had a lubricating oil leak on the
        flowing across the frame and over other equipment. This appeared to be a fire
strainer. Although this leak had been previously identified by the licensee,
        hazard and could have affected the long-term operability of other equipment if
oil had flowed through the absorbent cloths that had been laid down and was
        left uncorrected. The licensee was informed and this situation was corrected.
flowing across the frame and over other equipment.
        On December 2, the inspector observed a small jacket water leak coming from
This appeared to be a fire
        the turbocharger. The leak had accumulated into a white buildup. The                                             _
hazard and could have affected the long-term operability of other equipment if
        licensee wrote a maintenance work order to repair the leak and the buildup was
left uncorrected.
        removed to prevent any corrosion problems.
The licensee was informed and this situation was corrected.
        Throughout this inspection period the housekeeping in the plant continued to
On December 2, the inspector observed a small jacket water leak coming from
          improve. The above examples were indicative of weaknesses in isolated areas.
the turbocharger.
        3.3 Reactor Startup with Safety System inoperable
The leak had accumulated into a white buildup.
        On November 25, 1992, the licensee exceeded 150 psig reactor pressure with the
The
          reactor core isolation cooling (RCIC) system out of service. Technical
_
          Specification 3.7.3 states that the RCIC system shall be operable with an
licensee wrote a maintenance work order to repair the leak and the buildup was
          operable flow path capable of automatically taking suction from the
removed to prevent any corrosion problems.
          suppression pool and transferring the water to the reactor pressure vessel.
Throughout this inspection period the housekeeping in the plant continued to
          This specification is applicable in Operational Conditions 1, 2, and 3, with
improve. The above examples were indicative of weaknesses in isolated areas.
          reactor steam dome pressure greater than 150 psig.   The associated action
3.3 Reactor Startup with Safety System inoperable
          statement requires that the operator restore the system to operable status
On November 25, 1992, the licensee exceeded 150 psig reactor pressure with the
          within 14 days or be in at least hot shutdown within the next 12 hours.
reactor core isolation cooling (RCIC) system out of service. Technical
          Technical Specification 3.0.4 states that entry into an operational condition
Specification 3.7.3 states that the RCIC system shall be operable with an
          or other specified condition shall not be made when the conditions for the
operable flow path capable of automatically taking suction from the
                                                          __   _ _ _ _ _ _ _ _ _ ____ ___________________ - __ - __ __ -
suppression pool and transferring the water to the reactor pressure vessel.
This specification is applicable in Operational Conditions 1, 2, and 3, with
reactor steam dome pressure greater than 150 psig.
The associated action
statement requires that the operator restore the system to operable status
within 14 days or be in at least hot shutdown within the next 12 hours.
Technical Specification 3.0.4 states that entry into an operational condition
or other specified condition shall not be made when the conditions for the
__
_ _ _ _ _ _ _ _ _ ____ ___________________ - __ - __ __ -


      _ ____ _ _ _._._ _ _ _ _ ___..__ _ _ _ _ _ . _                                           _.
_ ____ _ _ _._._ _ _ _ _ ___..__ _ _ _ _ _ . _
            4
_.
                                                                    -8-
4
                timiting Condition for Operation are not met and the associated action           -
-8-
                requires a shutdown if they are not met within a specified time _ interval.
timiting Condition for Operation are not met and the associated action
                On November 25, the_ operators were in the process of starting up the reactor.
-
                Earlier in the day, the RCIC system had been isolated because of low reactor
requires a shutdown if they are not met within a specified time _ interval.
                pressure. Following criticality, the reactor operators began to Warm up the
On November 25, the_ operators were in the process of starting up the reactor.
                RCIC system steam lines prior to placing the system in standby lineup. At
Earlier in the day, the RCIC system had been isolated because of low reactor
                8:59 p.m., the reactor steam dome pressure was taken above 150 psig, entering
pressure.
                the specified condition for Technical Specification 3.7.3.     The RCIC steam
Following criticality, the reactor operators began to Warm up the
                lines remained isolated because they were not_ completely warmed. Therefore,
RCIC system steam lines prior to placing the system in standby lineup.
                the shift supervisor advised the control operating foreman to log the'RCIC
At
                system as inoperable and enter the associated Technical Specification action
8:59 p.m., the reactor steam dome pressure was taken above 150 psig, entering
                statement. This action was in violation of Technical Specification 3.0,4
the specified condition for Technical Specification 3.7.3.
                (Violation 458/92034-01).
The RCIC steam
                The licensee reviewed this event and determined that the Shift Supervisor had
lines remained isolated because they were not_ completely warmed.
                incorrectly interpreted the Technical Specifications.     Technical
Therefore,
                Specification 3.7.3 notes that the provisions of Technical Specification 4.0.4
the shift supervisor advised the control operating foreman to log the'RCIC
                are not applicable provided the surveillance is performed within 12 hours
system as inoperable and enter the associated Technical Specification action
                after the reactor steam pressure is adequate to perform the test. The
statement.
                licensee stated that the operators involved in this event were aware that this
This action was in violation of Technical Specification 3.0,4
,              exception had been utilized during previous startups and did not fully explore
(Violation 458/92034-01).
                the differences between an allowed surveillance testing exception and the
The licensee reviewed this event and determined that the Shift Supervisor had
incorrectly interpreted the Technical Specifications.
Technical
Specification 3.7.3 notes that the provisions of Technical Specification 4.0.4
are not applicable provided the surveillance is performed within 12 hours
after the reactor steam pressure is adequate to perform the test. The
licensee stated that the operators involved in this event were aware that this
exception had been utilized during previous startups and did not fully explore
,
'
'
                system not being operable.
the differences between an allowed surveillance testing exception and the
                The inspector noted that General Operating Procedure G0P-0001, " Plant
system not being operable.
                Startup," requires the operator to place the RCIC system in the standby mode
The inspector noted that General Operating Procedure G0P-0001, " Plant
                prior to exceeding 150 psig. The licensee stated that the control operating
Startup," requires the operator to place the RCIC system in the standby mode
                foreman did not challenge the Shift Supervisor on having the system in standby
prior to exceeding 150 psig.
                alignment, even though he read it in G0P-0001.
The licensee stated that the control operating
                3.4 Review of Reactor Shutdown Activities
foreman did not challenge the Shift Supervisor on having the system in standby
                On December 6, the inspector observed portions of the control room operations
alignment, even though he read it in G0P-0001.
                during the shutdown of the plant for planned Outage 92-04. The first stage of
3.4 Review of Reactor Shutdown Activities
                the Reactor Recirculation Pump B shaft seal was failing as indicated by
On December 6, the inspector observed portions of the control room operations
                abnormal staging pressures. The second stage seal was preventing reactor
during the shutdown of the plant for planned Outage 92-04. The first stage of
,                coolant system leakage, but the licensee decided to obtain the required parts,
the Reactor Recirculation Pump B shaft seal was failing as indicated by
I               shutdown and replace the seal . The inspector observed the briefing held by
abnormal staging pressures.
                the Shif t Supervisor just prior to the planned scram. This Shift Supervisor
The second stage seal was preventing reactor
                made specific assignments for each _ operator, stressed clear communications,
coolant system leakage, but the licensee decided to obtain the required parts,
                and covered areas requiring special attention, including feedwater. controls,
,
                Subsequently, the scram was executed from 25 percent power. The operators
I
                responded in a deliberate and orderly manner. The operators' actions to
shutdown and replace the seal .
                control feedwater were excellent. The operators responded to the level shrink     .
The inspector observed the briefing held by
                and stabilized the level at about 30 incnes without receiving a high level
the Shif t Supervisor just prior to the planned scram.
                feedwater pump trip. Overall, the operators' performance was exemplary, with
This Shift Supervisor
                one exception as discussed below.
made specific assignments for each _ operator, stressed clear communications,
and covered areas requiring special attention, including feedwater. controls,
Subsequently, the scram was executed from 25 percent power.
The operators
responded in a deliberate and orderly manner.
The operators' actions to
control feedwater were excellent.
The operators responded to the level shrink
.
and stabilized the level at about 30 incnes without receiving a high level
feedwater pump trip. Overall, the operators' performance was exemplary, with
one exception as discussed below.
I
I
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. . . .
                                  . . . . . ...             .
.
                                                                      .. .
.
                                                                                        .
. . . . .
                                                                                                .
...
                                                                                                  . . . . .
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                                                      -9-
-9-
p
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          On December 7, with the plant in cold shutdown, the Shift Supervisor realized
On December 7, with the plant in cold shutdown, the Shift Supervisor realized
          that the functional test surveillances for all channels of the intermediate
that the functional test surveillances for all channels of the intermediate
          range and source range monitors were not current at the time the plant was
range and source range monitors were not current at the time the plant was
          placed in hot shutdown at 5:29 p.m., on December 6. With these monitors being
placed in hot shutdown at 5:29 p.m., on December 6.
          inoperable, Technical Specifications 3.3.1 and 3.3.7.6 required the reactor
With these monitors being
          mode switch to be locked in the shutdown position and all insertable control
inoperable, Technical Specifications 3.3.1 and 3.3.7.6 required the reactor
          rods verified inserted into the core within I hour of the scram. While the
mode switch to be locked in the shutdown position and all insertable control
          reactor operator did immediately verify that all rods had been inserted into                     j
rods verified inserted into the core within I hour of the scram. While the
reactor operator did immediately verify that all rods had been inserted into
j
the core after the scram, as witnessed by the inspector, the mode switch,
{
t
t
'         the core after the scram, as witnessed by the inspector, the mode switch,
'
                                                                                                            {
which was in the shutdown position, was not locked until the Shift Supervisor
          which was in the shutdown position, was not locked until the Shift Supervisor                     I
I
          noticed the error at approximately 6:30 a.m., on December 7. The licensee                         !
noticed the error at approximately 6:30 a.m., on December 7.
          identified the error on Condition Report 92-0937. Immediate corrective                           l
The licensee
          actions were to verify all rods in, lock the mode switch in shutdown, and                         '
!
          implement the required surveillance tests.
identified the error on Condition Report 92-0937.
          Failure to comply with the action requirements of Technical
Immediate corrective
          Specifications 3.3.1 and 3.3.7.6 is a violation (Violation 458/92034-2).
l
                                                                                                            l
actions were to verify all rods in, lock the mode switch in shutdown, and
          The surveillance tests for the intermediate range monitors were' completed at
'
          2 p.m., on' December 7, and then the source range monitors were tested at
implement the required surveillance tests.
          9:12 p.m. The inspector questioned why the source range monitors were tested
Failure to comply with the action requirements of Technical
                                                                                                            ;
Specifications 3.3.1 and 3.3.7.6 is a violation (Violation 458/92034-2).
          last because, at the time the error was discovered, the reactor was in the                       '
l
          source range. Although the actions were in compliance with Technical
The surveillance tests for the intermediate range monitors were' completed at
          Specifications, the reactivity in the reactor core could have been better
2 p.m., on' December 7, and then the source range monitors were tested at
          monitored with the source range instruments. The licensee agreed to consider
9:12 p.m.
          this as a safer practice in the future.
The inspector questioned why the source range monitors were tested
          3.5 Negative Trend in Operator Performance
;
          in vie,: of the two violations addressed in paragraphs 3.3 and 3.4 of this
last because, at the time the error was discovered, the reactor was in the
          report, and considering two additional Technical Specification violations
'
          cited in NRC Inspection Report 50-458/92-32, the inspectors expressed concern
source range. Although the actions were in compliance with Technical
          that an unacceptable trend was developing. The licensee had recognized the
Specifications, the reactivity in the reactor core could have been better
          negative trend, and initiated corrective actions, including the following:
monitored with the source range instruments. The licensee agreed to consider
          e        On December 15, plant management held a meeting with all shift
this as a safer practice in the future.
                    supervisors to discuss the unsatisfactory performance trend, emphasizing
3.5 Negative Trend in Operator Performance
                    professionalism in operations, good communications between watch-
in vie,: of the two violations addressed in paragraphs 3.3 and 3.4 of this
                    standers, self-checking, and the oversight roles of the shif t
report, and considering two additional Technical Specification violations
                    supervisors and shift technical. advisors.
cited in NRC Inspection Report 50-458/92-32, the inspectors expressed concern
          e        The licensee implemented a case study on the RCIC issue, discussed in
that an unacceptable trend was developing.
                    paragraph 3.3, to present to all operators.
The licensee had recognized the
          *        The licensee committed to discuss all of- the recent procedure / Technical
negative trend, and initiated corrective actions, including the following:
                    Specification violations with all operations watch sections.
On December 15, plant management held a meeting with all shift
e
supervisors to discuss the unsatisfactory performance trend, emphasizing
professionalism in operations, good communications between watch-
standers, self-checking, and the oversight roles of the shif t
supervisors and shift technical. advisors.
The licensee implemented a case study on the RCIC issue, discussed in
e
paragraph 3.3, to present to all operators.
The licensee committed to discuss all of- the recent procedure / Technical
*
Specification violations with all operations watch sections.


        _       _ - _ _ - _ _ _ _ .
_
_ - _ _ - _ _ _ _ .
'
'
                                                        -10-
-10-
  e      Where appropriate, operating procedure revisions were initiated to
Where appropriate, operating procedure revisions were initiated to
          clarify the specific requirements and prompt the operators as an
e
          enhancement.
clarify the specific requirements and prompt the operators as an
  The inspectors will continue to monitor these corrective actions and will
enhancement.
  document the findings during the closure review of the associated licensee
The inspectors will continue to monitor these corrective actions and will
  event raports.
document the findings during the closure review of the associated licensee
  3.6 Conclusions
event raports.
  e      Overall, the licensee operated the facility in a satisfactory manner,
3.6 Conclusions
  o      The performance of the operators during the November 17, 1992, reactor
Overall, the licensee operated the facility in a satisfactory manner,
          shutdown and planned scram was very good,
e
  e      Overall, plant housekeeping, including radiological housekeeping, has
The performance of the operators during the November 17, 1992, reactor
          improved over the inspection period. However, oil leaks, oil pooling
o
          and a jacket water leak identified on the Division I standby diesel
shutdown and planned scram was very good,
          generator were examples of poor housekeeping.
Overall, plant housekeeping, including radiological housekeeping, has
  e      One violation was identified for failure to place the RCIC system in
e
          service prior to exceeding 150 psig reactor pressure as required by
improved over the inspection period. However, oil leaks, oil pooling
          Technical Specification 3.0.4.
and a jacket water leak identified on the Division I standby diesel
  e      A second violation was identified for failure to follow the action
generator were examples of poor housekeeping.
          statements of Technical Specifications 3.3.1 and 3.3.7.6, when the
One violation was identified for failure to place the RCIC system in
            intermediate range monitors and the source range monitors, respectively,
e
          had not been properly tested following a plant shutdown.
service prior to exceeding 150 psig reactor pressure as required by
    e      Overall, the operators' performance during the December 6 shutdown was                                                                                                 [
Technical Specification 3.0.4.
            exemplary,
A second violation was identified for failure to follow the action
    o      A negative trend was identified which involved operators not heeding
e
            procedures and not complying with Technical Specification requirements.
statements of Technical Specifications 3.3.1 and 3.3.7.6, when the
    4 M0KTHLY MAINTENANCE OBSERVATIONS (62703)
intermediate range monitors and the source range monitors, respectively,
    The station maintenance activities addressed below were observed and
had not been properly tested following a plant shutdown.
    documentation reviewed to ascertain that the activities were conducted in
Overall, the operators' performance during the December 6 shutdown was
    accordance with the licensee's approved maintenance programs, the Technical
[
    Specifications, and NRC Regulations.
e
    4.1   Lack of Maintenance on High Pressure Core Spras Pump Room Cooler Filter
exemplary,
    On December 2, 1992, during an NRC management tour, the inspector noted a
A negative trend was identified which involved operators not heeding
    buildup of foreign material on the discharge screen from Auxiliary Building
o
    Unit Cooler lHVR*UC5. This unit cooler provides cooling air to the high
procedures and not complying with Technical Specification requirements.
    pressure core spray pump room. Approximately one-third of the discharge
4 M0KTHLY MAINTENANCE OBSERVATIONS (62703)
                                                                                                                                                                                    1
The station maintenance activities addressed below were observed and
                                                                                                                                                                                    {
documentation reviewed to ascertain that the activities were conducted in
                                                                                                                                                                                    ,
accordance with the licensee's approved maintenance programs, the Technical
                                      . - - - - _ - . _     _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _________ _ ____ __
Specifications, and NRC Regulations.
4.1
Lack of Maintenance on High Pressure Core Spras Pump Room Cooler Filter
On December 2, 1992, during an NRC management tour, the inspector noted a
buildup of foreign material on the discharge screen from Auxiliary Building
Unit Cooler lHVR*UC5.
This unit cooler provides cooling air to the high
pressure core spray pump room.
Approximately one-third of the discharge
1
{
,
. - - - - _ - . _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _________
_ ____ __


        . _                                 _ _ _ _ _ _ . _ _ . . _ _ _ _ _                                                 __ _       . _ _ - _ - - ._ . .
. _
  :'
_ _ _ _ _ _ . _ _ . . _ _ _ _ _
__ _
. _ _ - _ - - ._
.
.
:'
-11-
,
,
                                                                                                          -11-
screen was blocked.
                                          screen was blocked.                     This condition was reported to the main control room,
This condition was reported to the main control room,
                                          lhe Shift Supervisor issued Condition Report 92-0930 to document the problem.
lhe Shift Supervisor issued Condition Report 92-0930 to document the problem.
                                          The licensee initiated Preventive Maintenance Work Order p562428 to evaluate
The licensee initiated Preventive Maintenance Work Order p562428 to evaluate
and clean the unit cooler,
The technicians inspected the internal filters and
,
,
                                          and clean the unit cooler,                              The technicians inspected the internal filters and
found that they had collapsed onto the cooling coils and that the filter media
                                          found that they had collapsed onto the cooling coils and that the filter media
                                          had disintegrated and had been drawn into the coils. The filters and filter
,
,
                                          media were removed.                     The coils were cleaned, and a determination was made that
had disintegrated and had been drawn into the coils.
                                          further cleaning was not necessary. New filters were installed, The filter
The filters and filter
                                          media was bagged and transferred to radioactive waste storage in accordance
media were removed.
The coils were cleaned, and a determination was made that
further cleaning was not necessary. New filters were installed, The filter
media was bagged and transferred to radioactive waste storage in accordance
'
'
                                          with the instructions of-the radiation protection technicians.
with the instructions of-the radiation protection technicians.
                                          The licensee reviewed the maintenance history of Unit Cooler lHVR*UC5.
The licensee reviewed the maintenance history of Unit Cooler lHVR*UC5.
                                          Initially, preventive maintenance on all plant unit coolers provided for the
Initially, preventive maintenance on all plant unit coolers provided for the
                                          replacement of filters on a routine basis.                             During Refueling Outage 2, the
replacement of filters on a routine basis.
                                          licensee determined that this was excessive. Therefore, the preventive
During Refueling Outage 2, the
                                          maintenance tasks were scheduled to be performed only when the operators
licensee determined that this was excessive.
                                          requested them. This was an acceptable solution for most of the unit coolers,
Therefore, the preventive
                                          because they had external filters that could be readily observed and evaluated
maintenance tasks were scheduled to be performed only when the operators
i                                        to determine when they required changing. However, Unit Cooler 1HVR*UC5 had
requested them.
                                          filters internal to the unit cooler casing.                             Therefore, the operators could
This was an acceptable solution for most of the unit coolers,
                                          not routinely observe the filters and did not request preventive maintenance
because they had external filters that could be readily observed and evaluated
                                          to be performed.
to determine when they required changing.
;                                         The inspector noted that the filters were last changed on April 15, 1991. As
However, Unit Cooler 1HVR*UC5 had
,_                                       of the end of this inspection period, the licensee was reviewing maintenance
i
filters internal to the unit cooler casing.
Therefore, the operators could
not routinely observe the filters and did not request preventive maintenance
to be performed.
;
The inspector noted that the filters were last changed on April 15, 1991. As
, _
of the end of this inspection period, the licensee was reviewing maintenance
l
l
                                          records to better understand the basis for changing the filters on April 15
records to better understand the basis for changing the filters on April 15
and why the inaccessibility of the filters had not been identified at that
'
'
                                          and why the inaccessibility of the filters had not been identified at that
time,
                                          time,         filters collapsing and clogging the flowpath in safety-related unit
filters collapsing and clogging the flowpath in safety-related unit
                                          coolers is a condition adverse to quality.                             The licensee's failure to provide
coolers is a condition adverse to quality.
The licensee's failure to provide
measures to identify and correct this condition adverse to quality in Unit
i
i
                                          measures to identify and correct this condition adverse to quality in Unit
I
I                                        Cooler lHVR*UC5 is a violation of 10 CFR Part 50, Appendix B, Criterion XVI
Cooler lHVR*UC5 is a violation of 10 CFR Part 50, Appendix B, Criterion XVI
                                          (Violation 458/92034-3).
(Violation 458/92034-3).
                                          The licensee developed a list of five other safety-related unit coolers which
The licensee developed a list of five other safety-related unit coolers which
,                                        had internal filters.                         Although the problem with preventive maintenance
had internal filters.
1-                                       scheduling was identified on December 3, no action was taken to assess the
Although the problem with preventive maintenance
                                          extent of the degradation on the other unit coolers until after a plant
,
                                          shutdown on December 6.                           The licensee continued to run the plant in
1-
                                          Operational Condition 1 from December 3 through 6 without evaluating the
scheduling was identified on December 3, no action was taken to assess the
                                          operability of the other unit coolers with internal filters.
extent of the degradation on the other unit coolers until after a plant
                                          The inspector questioned the licensee on the potential impact of the-other
shutdown on December 6.
                                          unit coolers,                   lhe licensee inspected and replaced each of the filters prior
The licensee continued to run the plant in
                                          to restarting from planned Outage 92-04 conducted from December 6-11, 1992.
Operational Condition 1 from December 3 through 6 without evaluating the
                                          However, the failure to assess the generic aspects of the other unit coolers
operability of the other unit coolers with internal filters.
                                          in a timely manner was considered a weakness.
The inspector questioned the licensee on the potential impact of the-other
                                                                                                                                                              .
unit coolers,
    - - - _ _ _ - - - _ - _ _ . . _ _ _ _                                          ..,.w ~,,,_m.           y             _
lhe licensee inspected and replaced each of the filters prior
                                                                                                                                ,.7,
to restarting from planned Outage 92-04 conducted from December 6-11, 1992.
                                                                                                                                _   ,
However, the failure to assess the generic aspects of the other unit coolers
in a timely manner was considered a weakness.
.
- - -
- - -
-
. .
..,.w
~,,,_m.
y
_
,.7,
,
_


                                                _ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _     _
_ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
_
*
~12-
At the end of this inspection period, the licensee was in the process of
reviewing the preventive maintenance tasks which were scheduled only as needed
to determine if they were being properly monitored and performed.
4.2 Preventive Maintenance on Environmentally Qualified (E0) Components
On December 18, 1992, the inspector observed the replacement of one of several
EQ pressure switches in accordance with Maintenance Work Order E558245.
This
work was scheduled based on the expiration of the EQ service life of
Switch llSV*PS49B.
The inspector reviewed the work documentation package and
found it to be in order and well written.
The technicians were qualified to
perform the work. The equipment clearance was properly implemented.
The
_
lif ting and reconnection of leads were properly verified and documented to
prevent wiring errors.
A quality control inspector was present and observed
the work.
The overcil performance of this maintenance item was very good.
4.3 Conclusions
e
Overall, the licensee's performance in maintenance activities observed
during this inspection period was adequate.
e
One violation was identified for failure to identify that the filter
elements in a safety-related unit cooler had collapsed onto the cooling
coils, clogging the air flow channels.
The licensee's f ailure to promptly assess the status of five similar
e
safety-related unit coolers, following the identification of preventive
maintenance problems in Unit Cooler lHVR*UC5, was considered a weakness.
*
*
                                            ~12-
Work controls observed were very good during the replacement of an
  At the end of this inspection period, the licensee was in the process of
_
  reviewing the preventive maintenance tasks which were scheduled only as needed
environmentally qualified switch.
  to determine if they were being properly monitored and performed.
The individuals performing the task
  4.2 Preventive Maintenance on Environmentally Qualified (E0) Components
were properly qualified.
  On December 18, 1992, the inspector observed the replacement of one of several
5 BIMONTHLY SURVEILLANCE OBSERVATIONS (61726)
  EQ pressure switches in accordance with Maintenance Work Order E558245. This
The inspectors observed the surveillance testing of safety-related systems and
  work was scheduled based on the expiration of the EQ service life of
components addressed below to verify that the activities were being performed
  Switch llSV*PS49B. The inspector reviewed the work documentation package and
in accordance with the licensee's approved programs and the Technical
  found it to be in order and well written.                  The technicians were qualified to                                                  _
Specifications.
  perform the work. The equipment clearance was properly implemented. The
5.1 Diesel-Generator Operability Tes;
  lif ting and reconnection of leads were properly verified and documented to
On December 4, 1992, the inspector observed portions of the performance of
  prevent wiring errors. A quality control inspector was present and observed
Surveillance Test Procedure STP-309-0201, " Diesel Generator Division I
  the work. The overcil performance of this maintenance item was very good.
Operability Test."
  4.3 Conclusions
The inspector reviewed the procedure and determined that
  e      Overall, the licensee's performance in maintenance activities observed
it implemented the requirements of Technical Specification 4.8.1.1.2.a.1
          during this inspection period was adequate.
through 4.8.1.1.2.a.7, and that it had been performed within its required time
  e      One violation was identified for failure to identify that the filter
frame.
          elements in a safety-related unit cooler had collapsed onto the cooling
The test was properly signed out for performance in the Surveillance
          coils, clogging the air flow channels.
Test Procedure Progress Log and was approved by the control operating foreman.
    e      The licensee's f ailure to promptly assess the status of five similar
          safety-related unit coolers, following the identification of preventive
          maintenance problems in Unit Cooler lHVR*UC5, was considered a weakness.
    *      Work controls observed were very good during the replacement of an                                                                     _
          environmentally qualified switch.     The individuals performing the task
          were properly qualified.
    5 BIMONTHLY SURVEILLANCE OBSERVATIONS (61726)
    The inspectors observed the surveillance testing of safety-related systems and
    components addressed below to verify that the activities were being performed
    in accordance with the licensee's approved programs and the Technical
    Specifications.
    5.1 Diesel-Generator Operability Tes;
    On December 4, 1992, the inspector observed portions of the performance of
    Surveillance Test Procedure STP-309-0201, " Diesel Generator Division I
    Operability Test." The inspector reviewed the procedure and determined                                                             that
    it implemented the requirements of Technical Specification 4.8.1.1.2.a.1
    through 4.8.1.1.2.a.7, and that it had been performed within its required time
    frame. The test was properly signed out for performance in the Surveillance
    Test Procedure Progress Log and was approved by the control operating foreman.


:
:
          .
.
                                            -13-
-13-
  The inspector observed the control room operator and determined that he was
The inspector observed the control room operator and determined that he was
  aware of the procedural requirements. Continuous communications had been
aware of the procedural requirements.
  established, as required, between the control room and the diesel generator
Continuous communications had been
  building. As the generator was unloaded, the operator insured that the
established, as required, between the control room and the diesel generator
  reactive load was maintained within the acceptable region. Good attention was
building.
  paid to all adjustments and the operator was observed following the operations
As the generator was unloaded, the operator insured that the
  self-checking policy.
reactive load was maintained within the acceptable region.
  The inspector observed operators in the diesel generator building performing
Good attention was
  operator rounds in support of the surveillance test. The operators were
paid to all adjustments and the operator was observed following the operations
  f amiliar with the parameters being observed and what the expected values were.   _
self-checking policy.
  All required data taken was compared with the published a :eptance criteria.
The inspector observed operators in the diesel generator building performing
  The inspector independently verified the fuel oil levels and pressures,
operator rounds in support of the surveillance test.
  starting air pressures, and the material condition of the diesel engine.
The operators were
  5.2 Conclusions
f amiliar with the parameters being observed and what the expected values were.
  e      Overall, surveillance activities were performed in a commendable manner
_
          during this inspection period.
All required data taken was compared with the published a :eptance criteria.
  *     Operator knowledge and control of testing activities were very good
The inspector independently verified the fuel oil levels and pressures,
          during the performance of surveillance testing of the Division I standby
starting air pressures, and the material condition of the diesel engine.
          diesel generator.
5.2 Conclusions
  6 OPEN ITEM FOLLOWUP (92701)
Overall, surveillance activities were performed in a commendable manner
  6.1 lest Engineer Certification and Test Practices
e
  The inspector reviewed the licensee's documentation of an evaluation completed
during this inspection period.
  on October 23, 1992, addressing the adequacy of the certification of a             _
*
  pipefitter to a test engineer and addressing the possibility that workers were
Operator knowledge and control of testing activities were very good
  being directed to beat on valves to make sure that they had seated to pass the
during the performance of surveillance testing of the Division I standby
  test.   The licensee concluded that there were no safety issues and that no
diesel generator.
  immediate corrective actions were warranted.
6 OPEN ITEM FOLLOWUP (92701)
  On December 7-8, the inspector reviewed the licensee's documentation.     The
6.1 lest Engineer Certification and Test Practices
  documents showed that the pipefitter in question was qualified and certified
The inspector reviewed the licensee's documentation of an evaluation completed
  as a test engineer in accordance with Procedure TSP-0001, Revision 7, " System
on October 23, 1992, addressing the adequacy of the certification of a
    Engineering Personnel Training and Qualifications." The inspector also
_
    reviewed the individual's resume and the completed personnel qualification
pipefitter to a test engineer and addressing the possibility that workers were
    matrix. The information met or exceeded the qualification criteria delineated
being directed to beat on valves to make sure that they had seated to pass the
    in Procedure TSP-0001. The individual's background, experience, and education
test.
    appeared to be adequate for t.im to perform the function of a Level Il test
The licensee concluded that there were no safety issues and that no
    engineer.   The inspector noted that, during previous outages, the individual
immediate corrective actions were warranted.
    was certified and performed the duties of a level I test engineer and
On December 7-8, the inspector reviewed the licensee's documentation.
    subsequently met the requirements of ANSI /ASME-N45.2.6 - 1978, " Qualification
The
    of Nuclear Power Plant Inspection, Examination and Testing Personnel," for
documents showed that the pipefitter in question was qualified and certified
    Level II.
as a test engineer in accordance with Procedure TSP-0001, Revision 7, " System
Engineering Personnel Training and Qualifications." The inspector also
reviewed the individual's resume and the completed personnel qualification
matrix.
The information met or exceeded the qualification criteria delineated
in Procedure TSP-0001.
The individual's background, experience, and education
appeared to be adequate for t.im to perform the function of a Level Il test
engineer.
The inspector noted that, during previous outages, the individual
was certified and performed the duties of a level I test engineer and
subsequently met the requirements of ANSI /ASME-N45.2.6 - 1978, " Qualification
of Nuclear Power Plant Inspection, Examination and Testing Personnel," for
Level II.


    '
'
  Y
Y
l                                             -14-
l
      With regard to the second concern, the licensee's quality assurance staf f
-14-
      informed the inspector that they had discussed the issue with a few workers,
With regard to the second concern, the licensee's quality assurance staf f
      the licensee's Mechanical Process System Supervisor, and the contractor's lead
informed the inspector that they had discussed the issue with a few workers,
      test engineer. The consensus was that, once a test was deemed unacceptable,
the licensee's Mechanical Process System Supervisor, and the contractor's lead
      valves have been perturbod during the course of troubleshooting, but never
test engineer.
      with the objective of obtaining satisfactory test results. The licensee did
The consensus was that, once a test was deemed unacceptable,
      not identify any evidence that indicated the test engineer had directed anyone
valves have been perturbod during the course of troubleshooting, but never
      to strike a valve to seat with the objective of obtaining satisfactory test
with the objective of obtaining satisfactory test results.
      results.   The inspector concluded that the licensee's review was reasonable.
The licensee did
      6.2 Potential Unmonitored Release Paths
not identify any evidence that indicated the test engineer had directed anyone
      The inspector reviewed an engineering evaluation performed by the licensee
to strike a valve to seat with the objective of obtaining satisfactory test
      addressing:   (1) potential unmonitored radiological releases from the turbine
results.
      building via the lubricating oil reservoir, and (2) the potential of the
The inspector concluded that the licensee's review was reasonable.
      instrument air system being contaminated and distributing contamination to the
6.2 Potential Unmonitored Release Paths
      control room, technical support center, and operations support center during
The inspector reviewed an engineering evaluation performed by the licensee
      an accident.
addressing:
      The licensee explained that radioactive steam leakage into the turbine bearing
(1) potential unmonitored radiological releases from the turbine
      lubricating oil would be precluded by the design of the turbine seals,
building via the lubricating oil reservoir, and (2) the potential of the
      bearings, and gland sealing system. In order for the lubricating oil
instrument air system being contaminated and distributing contamination to the
      reservoir to become contaminated, four barriers would have to fail and the
control room, technical support center, and operations support center during
      steam leakage rate would have to be significant. This would attract the
an accident.
      attention of the operators, who coul<i take action such as shutting down the
The licensee explained that radioactive steam leakage into the turbine bearing
lubricating oil would be precluded by the design of the turbine seals,
bearings, and gland sealing system.
In order for the lubricating oil
reservoir to become contaminated, four barriers would have to fail and the
steam leakage rate would have to be significant.
This would attract the
attention of the operators, who coul<i take action such as shutting down the
turbine.
In addition, there was not a pathway by which the air in the
,
,
      turbine. In addition, there was not a pathway by which the air in the
i
i    reservoir could be discharged into the turbine building, based on Flow
reservoir could be discharged into the turbine building, based on Flow
      Diagram 12210-FSK-16-38.
Diagram 12210-FSK-16-38.
      The engineering evaluation approached the instrument air issues from a normal
The engineering evaluation approached the instrument air issues from a normal
      operation and an accident perspective. During normal operation, contamination
operation and an accident perspective.
During normal operation, contamination
was not a problem because of the delay time involved in any radionuclides
,
,
      was not a problem because of the delay time involved in any radionuclides
traveling from the air compressor intakes to the points of release.
'
'
      traveling from the air compressor intakes to the points of release.
During design basis accident conditions, the worst case being a main steamline
      During design basis accident conditions, the worst case being a main steamline
break in the steam tunnel and assuming that the instrument air compressors
      break in the steam tunnel and assuming that the instrument air compressors
;
;     picked up all of the activity, the highest exposure would be 6 Rem for the
picked up all of the activity, the highest exposure would be 6 Rem for the
i     30-day thyroid iodine dose.     The evaluation concluded that if 100 percent of
i
;     the radioactive material followed the rupture disk pathway to the control room
30-day thyroid iodine dose.
The evaluation concluded that if 100 percent of
;
the radioactive material followed the rupture disk pathway to the control room
l
intakes, the 30-day thyroid iodine dose would be 15.3 Rem to the operators,
with 23 Rem to the technical support center personnel.
The operations support
!
center could be evacuated, as delineated in the emergency implementation
procedures.
These values were within the 30 Rem allowable dose stated in
l
l
      intakes, the 30-day thyroid iodine dose would be 15.3 Rem to the operators,
10 CFR Part 100.
      with 23 Rem to the technical support center personnel. The operations support
The inspector concluded that the licensee's evaluation adequately addressed
!    center could be evacuated, as delineated in the emergency implementation
the potential release paths.
      procedures. These values were within the 30 Rem allowable dose stated in
l      10 CFR Part 100.
      The inspector concluded that the licensee's evaluation adequately addressed
'
'
      the potential release paths.


    ..
..
                                            -15-
-15-
  6.3 Conclusions
6.3 Conclusions
  e       The licensee evaluation of the certification of a test engineer and test
e
I         practices was appropriate and reasonably supported,
The licensee evaluation of the certification of a test engineer and test
I
practices was appropriate and reasonably supported,
l
l
  e      The licensee adequately evaluated potential unmonitored release paths at
The licensee adequately evaluated potential unmonitored release paths at
          River Bend Station.
e
  7 ONSITE REVIEW 0F A LICENSEE EVENT REPORTS (92700)
River Bend Station.
  7.1   (Closed) Licensee Event Report 458/92-004:   Increased Surveillance (Per
7 ONSITE REVIEW 0F A LICENSEE EVENT REPORTS (92700)
        Technical Specification 4.0.5) Missed for Standb_y Service Water Pumps due
7.1
        to Procedural Deficiency
(Closed) Licensee Event Report 458/92-004:
  This licensee event report involved five instances where the licensee failed
Increased Surveillance (Per
Technical Specification 4.0.5) Missed for Standb_y Service Water Pumps due
to Procedural Deficiency
This licensee event report involved five instances where the licensee failed
to test one control building chilled water pump and three standby service
!
!
  to test one control building chilled water pump and three standby service
I
I
water pumps at an increased frequency as required by Technical
  water pumps at an increased frequency as required by Technical
l
l
  Specification 4.0.5, and ASME Code, Section XI, IWP-3230(a). Each pump was
Specification 4.0.5, and ASME Code, Section XI, IWP-3230(a).
j determined to be in the alert range as defined in the ASME Code. The licensee
Each pump was
  demonstrated that each of the pumps were capable of performing their intended
j
  safety functions. Therefore, there was minimal safety significance to this
determined to be in the alert range as defined in the ASME Code.
  issue.
The licensee
  The root cause was determined to be an ambiguity which existed on the
demonstrated that each of the pumps were capable of performing their intended
  licensee's Surveiliaiice Test Scheduling Completion / Exception Form. When a
safety functions.
Therefore, there was minimal safety significance to this
issue.
The root cause was determined to be an ambiguity which existed on the
licensee's Surveiliaiice Test Scheduling Completion / Exception Form.
When a
I
I
  pump was tested and found to be in the alert range, and it was already on an
pump was tested and found to be in the alert range, and it was already on an
  increased frequency schedule, the form required the user to indicate that no
increased frequency schedule, the form required the user to indicate that no
  frequency change was required. This was misconstrued by the scheduling
frequency change was required.
  personnel to mean the normal frequency and, as a result, the next test was
This was misconstrued by the scheduling
personnel to mean the normal frequency and, as a result, the next test was
l
l
  scheduled at the normal frequency instead of at an increased frequency.
scheduled at the normal frequency instead of at an increased frequency.
,
,
l The licensee changed the above referenced form to explicitly state whether or
l
The licensee changed the above referenced form to explicitly state whether or
I
I
  not the components were in the alert range, leaving no doubt what the next
not the components were in the alert range, leaving no doubt what the next
  text frequency should be. The inspectors reviewed the change to the form,
text frequency should be.
  which was Enclosure 3 to Administrative Procedure ADM-0015, Revision 13,
The inspectors reviewed the change to the form,
  " Station Surveillance Test Program." The change appeared adequate to prevent
which was Enclosure 3 to Administrative Procedure ADM-0015, Revision 13,
l future problems of this nature.
" Station Surveillance Test Program." The change appeared adequate to prevent
  7.2 Conclusions
l
  e       Licensee Event Report 92-004 was a good quality report and the
future problems of this nature.
7.2 Conclusions
e
Licensee Event Report 92-004 was a good quality report and the
licensee's corrective actions appeared to be adequate to prevent
,
,
          licensee's corrective actions appeared to be adequate to prevent
l
l          recurrence.
recurrence.
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Line 722: Line 1,016:
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      -
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.
            .
_ . __ _ _
                                            ATTACHMENT 1
_
        1     PERSONS CONTACTED
. . _ _ _ . _ _ _ _ . _ _.
        1.1     Licensee Personnel
. . ._ _ _
        0. L. Andrews, Director, Quality Assurance
_ . __ _ __
        R. E. Barnes, Supervisor, Maintenance Engineering
-
        P.. E. Cole, Supervisor, Control Process Systems
.
        J. W. Cook, Senior Technical Specialist
-
        T. C. Crouse, Manager, Administration
ATTACHMENT 1
        W. L. Curran, Cajun Site Representative
1
        P. E. Freehill, Assistant Plant Manager - Outage Management
PERSONS CONTACTED
        E. L. Glass,' Supervisor, Instrument & Control
1.1
        W. C. Hardy, Radiation Protection, Supervisor
Licensee Personnel
        V. F. Klco, Principal Engineer - NSAG
0. L. Andrews, Director, Quality Assurance
        I. M. Malik, Supervisor, Operations Quality Assurance
R. E. Barnes, Supervisor, Maintenance Engineering
        C. R. Maxson, Senior Compliance Analyst
P.. E. Cole, Supervisor, Control Process Systems
                .
J. W. Cook, Senior Technical Specialist
        C. L. Miller, Supervisor, Maintenance Support
T. C. Crouse, Manager, Administration
        W. H. Odell, Manager, Oversight
W. L. Curran, Cajun Site Representative
        S. R. Radebaugh, APM - Maintenance
P. E. Freehill, Assistant Plant Manager - Outage Management
        B. R. Smith, Mechanical Maintenance Supervisor
E. L. Glass,' Supervisor, Instrument & Control
        M. A. Stein, Director, Design Engineering
W. C. Hardy, Radiation Protection, Supervisor
        W. J. Trudell, Assistant Operations Supervisor
V. F. Klco, Principal Engineer - NSAG
        1.2 Other Personnel Contacted
I. M. Malik, Supervisor, Operations Quality Assurance
        The personnel listed above attended the exit meeting. In addition to the
C. R. Maxson, Senior Compliance Analyst
        personnel listed above, the inspectors contacted other personnel during this
.
        inspection period.
C. L. Miller, Supervisor, Maintenance Support
        2 EXIT MEETING
W. H. Odell, Manager, Oversight
        An exit meeting was conducted on December 22, 1992.                 During this. meeting, the
S. R. Radebaugh, APM - Maintenance
        inspectors reviewed the scope and findings of the report. The licensee did
B. R. Smith, Mechanical Maintenance Supervisor
        not identify as proprietary any information provided to, or reviewed by, the
M. A. Stein, Director, Design Engineering
        inspectors.
W. J. Trudell, Assistant Operations Supervisor
1.2 Other Personnel Contacted
The personnel listed above attended the exit meeting.
In addition to the
personnel listed above, the inspectors contacted other personnel during this
inspection period.
2 EXIT MEETING
An exit meeting was conducted on December 22, 1992.
During this. meeting, the
inspectors reviewed the scope and findings of the report. The licensee did
not identify as proprietary any information provided to, or reviewed by, the
inspectors.
I
I
1
1
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Latest revision as of 17:15, 12 December 2024

Insp Rept 50-458/92-34 on 921108-1219.Violations Noted.Major Areas Inspected:Onsite Response to Events,Operational Safety Verification,Maintenance & Surveillance Observations,Open Item Followup & Onsite Review of LER
ML20127C997
Person / Time
Site: River Bend Entergy icon.png
Issue date: 01/08/1993
From: Gagliardo J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20127C974 List:
References
50-458-92-34, NUDOCS 9301150056
Download: ML20127C997 (16)


See also: IR 05000458/1992034

Text

'

I

APPENDIX B

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

inspection Report:

50-458/92-34

Operating License: HPF-47

Licensee:

Gulf States Utilities

P.O. Box 220

4

St. Francisville, Louisiana 70775-0220

Facility Name:

River Bend Station

-

1

Inspection At:

St. Francisville, Louisiana

l

Inspection Conducted:

November 8 through December 19, 1992

Inspectors:

W. F. Smith, Senior Resident inspector

D. P. Loveless, Resident inspector

R. H. Bernhard, Senior Resident inspector,

Grand Gulf Nuclear Station, Region 11

J. M. Keeton, Examiner, Operational Programs Section,

J Di ision of Reactor Safety

I

>

Approved:

gliardo, Chlef, Project Section C

Ifa

'

.

inspection Summary

Areas inspected:

Routine, unannounced inspection of onsite response to

events, operational safety verification,- maintenance and surveillance-

observations, open item followup, and onsite review of a licensee event

report.

Results:

Overall, the licensee's responses to operational events during the

e

report period were very good (paragraph 2.3).

The operators' response to the motor trip on Chiller B was noteworthy.

e

They entered the shutdown evolution in an expeditious manner and used

good judgement in utilizing the available equipment to maintain the

control room atmosphere (paragraph 2.1).

e

The licensee's response to the November 24 reactor scram was very good,

including the posttrip review and the facility review committee response

(paragraph 2.2).

,

-9301150056 9301og

gDR- ADOCK 05000450

PDR

..

. .-

.

- . .

_-

- .

.- -

- -

_

_ _ _ _ _ _

_ _ . _ . . - _ _ _ _ _ _ _

_ _ ___. _ _ _ .

-2-

e

Overall, the licensee operated the facility in a satisf actory manner

(paragraph 3.6).

The performance of the operators during the November 17, 1992, reactor

e

shutdown and planned scram was very good (paragraph 3.1).

in general, plant housekeeping, including radiological housekeeping, has

e

improved over the inspection period.

However, oil leaks, oil pooling

and a Jacket water leak identified on the Division I standby diesel

generator were examples of poor housekeeping (paragraph 3.2).

One violation was identified for failure to place the reactor core

isolation cooling system in service prior to exceeding 150 psig reactor

pressure as required by Technical Specification 3.0.4 (paragraph 3.3).

,

The operators' performance during the December 6 shutdown was exemplary,

with one exception. A second violation was identified for failure to

follow the action statements of Technical Specifications 3.3.1 and

3.3.7.6 when the intermediate range monitors and the source range

,

monitors, respectively, had not been properly tested to demonstrate

operability following a plant shutdown (paragraph 3.4).

A negative trend was identified which involved operators not heeding

procedures and not complying with Technical Specification requirements

(paragraph 3.5),

Overall, the licensee's performance in maintenance activities observed

e

during this inspection period was adequate (paragraph 4.3),

e

One violation was identified for failure to establish measures to

identify that the filter elements in a safety-related unit cooler had

deteriorated and were breaking down and clogging the cooling coils

(paragraph 4.1).

The licensee's failure to promptly assess the status of five similar

safety-related unit coolers, following the identification of preventive

,

maintenance problems in Unit Cooler lHVR*UC5, was considered a weakness

l~

(paragraph 4.1).

Very good work controls were observed during the replacement of an

environmentally qualified switch (paragraph 4.2).

,

t

Overall, surveillance activities were performed in a commendable manner

e

during this inspection period (paragraph 5.2).

Operator knowledge and control of testing activities were good during

the performance of surveillance testing of the Division I standby diesel

generator (paragraph 5.1).

l

'

i

I

~-4

. - . . -

. . . . _ . , , . - - . . - . . .

. _ _ _ - , , . . . , _ , , , . . , . , - - - - , , ,

--_--,,...,,-_m.---,_,-

. - -

.-.-r

~ . . . . , , . .

. - _ . . .

.- -_ . - - . .

.--

~

_. -.

.

.. .

.

. -

'

l

.

_3

,

o

The licensee evaluation of the certification of_ a test engineer and test

practices was appropriate and reasonably supported (paragraph 6.1).

The licensee adequately evaluated potential unmonitored release paths at

e

River Bend Station (paragraph 6.2).

. censee Event Report 92-004 was a good quality report and the

i censee's corrective actions appeared to be adequate to prevent

recuitence (paragraph 7.1).

Summary of Inspection findings:

e

Violation 458/92034-1 was opened (paragraph 3.3).

V;olation 458/92034-2 was opened (paragraph 3.4).

e

Violation 458/92034-3 was opened (paragraph 4.1).

Licensee Event Report 458/92-004 was closed (paragraph 7.1).

Attachments:

  • -

Attachment 1 - Persons Contacted and r

Meeting

.

_ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _

.

-4-

DETAILS

.

1 PLANT STATUS

At the beginning of this inspection period, the plant was operating at

100 percent power.

On November 10, 1992, a plant shutdown was initiated as required by 72chnical

Specification 3.0.3 when the only operable control room ventilation chiller

tripped.

Howeve , the shutdown was terminated at 76 percent power when the

chiller was restarted, and full power operation was resumed on November 11.

_

On November 16, the licensee commenced a plant shutdown to Operational

Condition 3 (hot shutdown) to facilitate planned Outage 92-03. On

November 24, the plant was restarted, but the reactor scrammed from 96 percent

.

power on high neutron flux caused by a main turbine electrohydraulic control

"s

system transient.

lhe startup was resumed on November 25, and by November 27,

' 3

the pisnt was operating at 100 percent power.

'

On December 6, the plant was shut down and cooled to ambient conditions for

planned Outage 92-04 to replace a failed reactor recirculation pump seal.

The

plant was restarted on December 13 and resumed full power operation on

December 16.

At the end of this inspection period, the plant was operating at 100 percent

power.

2 ONSITE RESP 0i4SE TO EVENTS (93702)

2.1

Inoperability of Both Control Room Ventilation Systems

[

At 12:58 p.m., on November 10, 1992, the Division 11 control room ventilation

system Chiller 18 tripped on motor overload.

At the time, the Division I

system was inoperable because maintenance was being performed on the air

handling unit heaters.

In addition, Chiller D, the alternate Division 11

chiller, was inoperable because of an unresolved tripping problem that was

identified on October 18.

At 1:45 p.m.,

a plant shutdown was initiated as requir2d by Technical Specification 3.0.3.

To maintain the control room atmosphere, Chiller D was

placed in service, ever though it was technically inoperable because of

spurious trips.

The matsr on Chiller B was checked for grounds and short

circuits, but no problems were found.

bpar checking the motor control

breaker, the elech !cian found a loose pleg on the overcurrent trip device.

When the plug wa: properly installed, the breaker performed as designed.

At 3:32 p.m., Chiller B was restored to service and the plant shutdown was

terminated at about 76 percent power.

By 2:27 a.m.,

on November 11, full

power operation was resumed. The licensee reported the event at 2:02 p.m., on

'

'

.

.

9

-5-

November 10, as required by 10 CFR Part 50.72.

They also initiated Condition

Report 92-0898 to document the trip of Chiller B and the shutdown event.

The inspector examined a sin;ilar breaker and noted that the overcurrent ! ip

device plug, when-properly irstalled, snapped and locked in place. The

inspector questioned how the plug could come loose, and the licensee's

representative stated that the positive locking feature of the plug would

prevent the plug from coming loose and that there was an independent

verification signed off whenever the plug was installed.

In this case, the

installer apparently failed to snap the plug in place, and the independe'nt

verifier did not notice the error. The licen ce informed the inspectnr that

44 similar safety-related breaker'overcurrent trip device plugs were chec hd

and they were all aroperly installed.

Because this'was the only time that

this type of plug mad come loose, and no others were found, the licensee

considered this to be an isolated incident. The electricians that had

previously installed the plug in the Chiller 8 controller were counselled on

this event.

No further corrective action was taken.

2.2 Reactor Scram

On November 24, 1992, the reactor scrammed on high neutron flux as indicated

by the average power range monitors. A power ascension was in progress when

the electrohydraulic control system pressure regulator automatically shifted

from the manually selected Channel B to Channel A.

A large deviation existed

between the channels prior to the automatic transfer.

Therefore, the transfer

I

caused the main turbine control-valves to change position from'approximately

35 percent open to 23 percent open.

The resulting pressure surge in the

reactor vessel caused a momentary collapse of voids in the reactor, causing an

indicated power increase to greater than the 118 percent high neutron flux

scram setpoint. The inspector was notified and reported to the control room

where he determined that the operators had brought the plant to a stable

l

condition.

The licensee reviewed the event and determined that the pressure regulator

circuit was designed to automatically transfer from one channel to the other

in the event of a rapid failure of one channel. This function was not

intended to provide a smooth automatic transfer when the channels were slowly

drifting apart, as occurred during this event.

The licensee found that the

Channel A pressure amplifier card had been slowly drifting out' of calibration.

This card was replaced.

The inspector reviewed the posttrip review data package. All other plant

systems were determined to have functioned properly.

Several _ items were

reviewed in depth by licensee personnel to verify their accuracy. The

inspector observed the facility review committee meetings held to discuss the

event and_the readiness to restart the plant.

The questions raised by the

committee members-were of.high quality and were responded to prior to.an

authorization to restart. The overall licensee response to the scram was

considered very good.

L

.

..

.

.

i

_

_ _

-6-

During the subsequent startup, the licensee monitored the channel outputs on

the emergency response information system to observe any drift. The channels

continued to drift apart during pressure increases.

Each time the licensee

adjusted the gain to bring the channels back together.

During planned

Outage 92-04, the licensee performed additional troubleshooting of the

pressure regulator circuits.

The technicians found that the Channel B

pressure transmitter was not repeatable during calibration.

This transmitter

was replaced.

The River Bend Station Updated Safety Analysis Report, Chapter 15.2, " Increase

n, Acactor Pressure,

ps.iui tca a failure of the pressure regulator.

This

,

event is referred to as an "ar.ticipated operatio.nal transient." Therefore,

_

the safety significance of thia failure was low.

The licensee was continuing

to investigate the problem and work with the vendor at the end of this

inspection period.

ihe corrective actions will be reviewed further with the

issuance of the licensee event report.

2.3 Conclusions

Overall, the licensee's response to operational events during the report

e

period was very good.

The operators' response to the motor trip on Chiller B was noteworthy.

They entered the shutdown evolution in an expeditious manner and used

good judgement in utilizing the available equipment to maintain the

control room atmosphere.

The licensee's response to the November 24 reactor scram was very good,

e

including the posttrip review and the facility review committee's

evaluation.

_

3 OPERATIONAL SAFETY VERIFICATION (71707)

The objectives of this inspection were to ensure that this facility was being

operated safely and in conformance with regulatory requirements and to ensure

that the licensee's management controls were effectively discharging the

licensee's responsibilities for continued safe operation.

3.1 Control Room Observations

On November 17, the inspectors monitored portions of control room operations

during the shutdown of the plant for planned Outage 92-03.

The primary

purpose of the outage was to repair the drywell pedestal sump pumps.

The

licensee discovered both pumps were not functional when unidentified leakage

began to fill the sump. Details on the issue were documented in paragraph 2.4

of NRC Inspection Report 50-458/92-32.

The reactor was manually scrammed from '9.5 percent power, as delineated in

the normal shutdown procedure. The opt

es executed the appropriate actions

,

. . .

- . .

.

_

_

_ _ __ -

__

____

. - -

_ _ _ _ _ _ _ _ _

-7-

in response to the scram.

The applicable emergency operating procedure was

entered when reactor vessel water level shrank to Level 3, but in recovering

level, manipulation of the feedwater controls resulted in slightly overfeeding

the reactor, which caused a high level trip of the operating feedwater pump.

The feedwater pump was promptly restored to service, and the shutdown was

completed without incident.

The licensee explained that, although the reactor vessel level was optimized

just prior to the scram, compensation for normal shrink and preventing the

feedwater system from overfeeding has been difficult for some of the less

experienced operators. The licensee had just issued a change to System

Opar e ing Procedure SOP-0009, " Reactor Feedwater System," on November 11,

providing specific guidance for the operators during this type of feedwater

transient and has been in the process of training the operators on feedwater

transient response during routine requalification training.

Overall, operator performance during the shutdown was very good.

3.2 Plant Tours

On December 1, 1992, the inspector toured the diesel generator building. The

inspector noted that the Division I diesel had a lubricating oil leak on the

strainer. Although this leak had been previously identified by the licensee,

oil had flowed through the absorbent cloths that had been laid down and was

flowing across the frame and over other equipment.

This appeared to be a fire

hazard and could have affected the long-term operability of other equipment if

left uncorrected.

The licensee was informed and this situation was corrected.

On December 2, the inspector observed a small jacket water leak coming from

the turbocharger.

The leak had accumulated into a white buildup.

The

_

licensee wrote a maintenance work order to repair the leak and the buildup was

removed to prevent any corrosion problems.

Throughout this inspection period the housekeeping in the plant continued to

improve. The above examples were indicative of weaknesses in isolated areas.

3.3 Reactor Startup with Safety System inoperable

On November 25, 1992, the licensee exceeded 150 psig reactor pressure with the

reactor core isolation cooling (RCIC) system out of service. Technical Specification 3.7.3 states that the RCIC system shall be operable with an

operable flow path capable of automatically taking suction from the

suppression pool and transferring the water to the reactor pressure vessel.

This specification is applicable in Operational Conditions 1, 2, and 3, with

reactor steam dome pressure greater than 150 psig.

The associated action

statement requires that the operator restore the system to operable status

within 14 days or be in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Technical Specification 3.0.4 states that entry into an operational condition

or other specified condition shall not be made when the conditions for the

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timiting Condition for Operation are not met and the associated action

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requires a shutdown if they are not met within a specified time _ interval.

On November 25, the_ operators were in the process of starting up the reactor.

Earlier in the day, the RCIC system had been isolated because of low reactor

pressure.

Following criticality, the reactor operators began to Warm up the

RCIC system steam lines prior to placing the system in standby lineup.

At

8:59 p.m., the reactor steam dome pressure was taken above 150 psig, entering

the specified condition for Technical Specification 3.7.3.

The RCIC steam

lines remained isolated because they were not_ completely warmed.

Therefore,

the shift supervisor advised the control operating foreman to log the'RCIC

system as inoperable and enter the associated Technical Specification action

statement.

This action was in violation of Technical Specification 3.0,4

(Violation 458/92034-01).

The licensee reviewed this event and determined that the Shift Supervisor had

incorrectly interpreted the Technical Specifications.

Technical Specification 3.7.3 notes that the provisions of Technical Specification 4.0.4

are not applicable provided the surveillance is performed within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

after the reactor steam pressure is adequate to perform the test. The

licensee stated that the operators involved in this event were aware that this

exception had been utilized during previous startups and did not fully explore

,

'

the differences between an allowed surveillance testing exception and the

system not being operable.

The inspector noted that General Operating Procedure G0P-0001, " Plant

Startup," requires the operator to place the RCIC system in the standby mode

prior to exceeding 150 psig.

The licensee stated that the control operating

foreman did not challenge the Shift Supervisor on having the system in standby

alignment, even though he read it in G0P-0001.

3.4 Review of Reactor Shutdown Activities

On December 6, the inspector observed portions of the control room operations

during the shutdown of the plant for planned Outage 92-04. The first stage of

the Reactor Recirculation Pump B shaft seal was failing as indicated by

abnormal staging pressures.

The second stage seal was preventing reactor

coolant system leakage, but the licensee decided to obtain the required parts,

,

I

shutdown and replace the seal .

The inspector observed the briefing held by

the Shif t Supervisor just prior to the planned scram.

This Shift Supervisor

made specific assignments for each _ operator, stressed clear communications,

and covered areas requiring special attention, including feedwater. controls,

Subsequently, the scram was executed from 25 percent power.

The operators

responded in a deliberate and orderly manner.

The operators' actions to

control feedwater were excellent.

The operators responded to the level shrink

.

and stabilized the level at about 30 incnes without receiving a high level

feedwater pump trip. Overall, the operators' performance was exemplary, with

one exception as discussed below.

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On December 7, with the plant in cold shutdown, the Shift Supervisor realized

that the functional test surveillances for all channels of the intermediate

range and source range monitors were not current at the time the plant was

placed in hot shutdown at 5:29 p.m., on December 6.

With these monitors being

inoperable, Technical Specifications 3.3.1 and 3.3.7.6 required the reactor

mode switch to be locked in the shutdown position and all insertable control

rods verified inserted into the core within I hour of the scram. While the

reactor operator did immediately verify that all rods had been inserted into

j

the core after the scram, as witnessed by the inspector, the mode switch,

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which was in the shutdown position, was not locked until the Shift Supervisor

I

noticed the error at approximately 6:30 a.m., on December 7.

The licensee

!

identified the error on Condition Report 92-0937.

Immediate corrective

l

actions were to verify all rods in, lock the mode switch in shutdown, and

'

implement the required surveillance tests.

Failure to comply with the action requirements of Technical Specifications 3.3.1 and 3.3.7.6 is a violation (Violation 458/92034-2).

l

The surveillance tests for the intermediate range monitors were' completed at

2 p.m., on' December 7, and then the source range monitors were tested at

9:12 p.m.

The inspector questioned why the source range monitors were tested

last because, at the time the error was discovered, the reactor was in the

'

source range. Although the actions were in compliance with Technical

Specifications, the reactivity in the reactor core could have been better

monitored with the source range instruments. The licensee agreed to consider

this as a safer practice in the future.

3.5 Negative Trend in Operator Performance

in vie,: of the two violations addressed in paragraphs 3.3 and 3.4 of this

report, and considering two additional Technical Specification violations

cited in NRC Inspection Report 50-458/92-32, the inspectors expressed concern

that an unacceptable trend was developing.

The licensee had recognized the

negative trend, and initiated corrective actions, including the following:

On December 15, plant management held a meeting with all shift

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supervisors to discuss the unsatisfactory performance trend, emphasizing

professionalism in operations, good communications between watch-

standers, self-checking, and the oversight roles of the shif t

supervisors and shift technical. advisors.

The licensee implemented a case study on the RCIC issue, discussed in

e

paragraph 3.3, to present to all operators.

The licensee committed to discuss all of- the recent procedure / Technical

Specification violations with all operations watch sections.

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Where appropriate, operating procedure revisions were initiated to

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clarify the specific requirements and prompt the operators as an

enhancement.

The inspectors will continue to monitor these corrective actions and will

document the findings during the closure review of the associated licensee

event raports.

3.6 Conclusions

Overall, the licensee operated the facility in a satisfactory manner,

e

The performance of the operators during the November 17, 1992, reactor

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shutdown and planned scram was very good,

Overall, plant housekeeping, including radiological housekeeping, has

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improved over the inspection period. However, oil leaks, oil pooling

and a jacket water leak identified on the Division I standby diesel

generator were examples of poor housekeeping.

One violation was identified for failure to place the RCIC system in

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service prior to exceeding 150 psig reactor pressure as required by

Technical Specification 3.0.4.

A second violation was identified for failure to follow the action

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statements of Technical Specifications 3.3.1 and 3.3.7.6, when the

intermediate range monitors and the source range monitors, respectively,

had not been properly tested following a plant shutdown.

Overall, the operators' performance during the December 6 shutdown was

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exemplary,

A negative trend was identified which involved operators not heeding

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procedures and not complying with Technical Specification requirements.

4 M0KTHLY MAINTENANCE OBSERVATIONS (62703)

The station maintenance activities addressed below were observed and

documentation reviewed to ascertain that the activities were conducted in

accordance with the licensee's approved maintenance programs, the Technical

Specifications, and NRC Regulations.

4.1

Lack of Maintenance on High Pressure Core Spras Pump Room Cooler Filter

On December 2, 1992, during an NRC management tour, the inspector noted a

buildup of foreign material on the discharge screen from Auxiliary Building

Unit Cooler lHVR*UC5.

This unit cooler provides cooling air to the high

pressure core spray pump room.

Approximately one-third of the discharge

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screen was blocked.

This condition was reported to the main control room,

lhe Shift Supervisor issued Condition Report 92-0930 to document the problem.

The licensee initiated Preventive Maintenance Work Order p562428 to evaluate

and clean the unit cooler,

The technicians inspected the internal filters and

,

found that they had collapsed onto the cooling coils and that the filter media

,

had disintegrated and had been drawn into the coils.

The filters and filter

media were removed.

The coils were cleaned, and a determination was made that

further cleaning was not necessary. New filters were installed, The filter

media was bagged and transferred to radioactive waste storage in accordance

'

with the instructions of-the radiation protection technicians.

The licensee reviewed the maintenance history of Unit Cooler lHVR*UC5.

Initially, preventive maintenance on all plant unit coolers provided for the

replacement of filters on a routine basis.

During Refueling Outage 2, the

licensee determined that this was excessive.

Therefore, the preventive

maintenance tasks were scheduled to be performed only when the operators

requested them.

This was an acceptable solution for most of the unit coolers,

because they had external filters that could be readily observed and evaluated

to determine when they required changing.

However, Unit Cooler 1HVR*UC5 had

i

filters internal to the unit cooler casing.

Therefore, the operators could

not routinely observe the filters and did not request preventive maintenance

to be performed.

The inspector noted that the filters were last changed on April 15, 1991. As

, _

of the end of this inspection period, the licensee was reviewing maintenance

l

records to better understand the basis for changing the filters on April 15

and why the inaccessibility of the filters had not been identified at that

'

time,

filters collapsing and clogging the flowpath in safety-related unit

coolers is a condition adverse to quality.

The licensee's failure to provide

measures to identify and correct this condition adverse to quality in Unit

i

I

Cooler lHVR*UC5 is a violation of 10 CFR Part 50, Appendix B, Criterion XVI

(Violation 458/92034-3).

The licensee developed a list of five other safety-related unit coolers which

had internal filters.

Although the problem with preventive maintenance

,

1-

scheduling was identified on December 3, no action was taken to assess the

extent of the degradation on the other unit coolers until after a plant

shutdown on December 6.

The licensee continued to run the plant in

Operational Condition 1 from December 3 through 6 without evaluating the

operability of the other unit coolers with internal filters.

The inspector questioned the licensee on the potential impact of the-other

unit coolers,

lhe licensee inspected and replaced each of the filters prior

to restarting from planned Outage 92-04 conducted from December 6-11, 1992.

However, the failure to assess the generic aspects of the other unit coolers

in a timely manner was considered a weakness.

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At the end of this inspection period, the licensee was in the process of

reviewing the preventive maintenance tasks which were scheduled only as needed

to determine if they were being properly monitored and performed.

4.2 Preventive Maintenance on Environmentally Qualified (E0) Components

On December 18, 1992, the inspector observed the replacement of one of several

EQ pressure switches in accordance with Maintenance Work Order E558245.

This

work was scheduled based on the expiration of the EQ service life of

Switch llSV*PS49B.

The inspector reviewed the work documentation package and

found it to be in order and well written.

The technicians were qualified to

perform the work. The equipment clearance was properly implemented.

The

_

lif ting and reconnection of leads were properly verified and documented to

prevent wiring errors.

A quality control inspector was present and observed

the work.

The overcil performance of this maintenance item was very good.

4.3 Conclusions

e

Overall, the licensee's performance in maintenance activities observed

during this inspection period was adequate.

e

One violation was identified for failure to identify that the filter

elements in a safety-related unit cooler had collapsed onto the cooling

coils, clogging the air flow channels.

The licensee's f ailure to promptly assess the status of five similar

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safety-related unit coolers, following the identification of preventive

maintenance problems in Unit Cooler lHVR*UC5, was considered a weakness.

Work controls observed were very good during the replacement of an

_

environmentally qualified switch.

The individuals performing the task

were properly qualified.

5 BIMONTHLY SURVEILLANCE OBSERVATIONS (61726)

The inspectors observed the surveillance testing of safety-related systems and

components addressed below to verify that the activities were being performed

in accordance with the licensee's approved programs and the Technical

Specifications.

5.1 Diesel-Generator Operability Tes;

On December 4, 1992, the inspector observed portions of the performance of

Surveillance Test Procedure STP-309-0201, " Diesel Generator Division I

Operability Test."

The inspector reviewed the procedure and determined that

it implemented the requirements of Technical Specification 4.8.1.1.2.a.1

through 4.8.1.1.2.a.7, and that it had been performed within its required time

frame.

The test was properly signed out for performance in the Surveillance

Test Procedure Progress Log and was approved by the control operating foreman.

.

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The inspector observed the control room operator and determined that he was

aware of the procedural requirements.

Continuous communications had been

established, as required, between the control room and the diesel generator

building.

As the generator was unloaded, the operator insured that the

reactive load was maintained within the acceptable region.

Good attention was

paid to all adjustments and the operator was observed following the operations

self-checking policy.

The inspector observed operators in the diesel generator building performing

operator rounds in support of the surveillance test.

The operators were

f amiliar with the parameters being observed and what the expected values were.

_

All required data taken was compared with the published a :eptance criteria.

The inspector independently verified the fuel oil levels and pressures,

starting air pressures, and the material condition of the diesel engine.

5.2 Conclusions

Overall, surveillance activities were performed in a commendable manner

e

during this inspection period.

Operator knowledge and control of testing activities were very good

during the performance of surveillance testing of the Division I standby

diesel generator.

6 OPEN ITEM FOLLOWUP (92701)

6.1 lest Engineer Certification and Test Practices

The inspector reviewed the licensee's documentation of an evaluation completed

on October 23, 1992, addressing the adequacy of the certification of a

_

pipefitter to a test engineer and addressing the possibility that workers were

being directed to beat on valves to make sure that they had seated to pass the

test.

The licensee concluded that there were no safety issues and that no

immediate corrective actions were warranted.

On December 7-8, the inspector reviewed the licensee's documentation.

The

documents showed that the pipefitter in question was qualified and certified

as a test engineer in accordance with Procedure TSP-0001, Revision 7, " System

Engineering Personnel Training and Qualifications." The inspector also

reviewed the individual's resume and the completed personnel qualification

matrix.

The information met or exceeded the qualification criteria delineated

in Procedure TSP-0001.

The individual's background, experience, and education

appeared to be adequate for t.im to perform the function of a Level Il test

engineer.

The inspector noted that, during previous outages, the individual

was certified and performed the duties of a level I test engineer and

subsequently met the requirements of ANSI /ASME-N45.2.6 - 1978, " Qualification

of Nuclear Power Plant Inspection, Examination and Testing Personnel," for

Level II.

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With regard to the second concern, the licensee's quality assurance staf f

informed the inspector that they had discussed the issue with a few workers,

the licensee's Mechanical Process System Supervisor, and the contractor's lead

test engineer.

The consensus was that, once a test was deemed unacceptable,

valves have been perturbod during the course of troubleshooting, but never

with the objective of obtaining satisfactory test results.

The licensee did

not identify any evidence that indicated the test engineer had directed anyone

to strike a valve to seat with the objective of obtaining satisfactory test

results.

The inspector concluded that the licensee's review was reasonable.

6.2 Potential Unmonitored Release Paths

The inspector reviewed an engineering evaluation performed by the licensee

addressing:

(1) potential unmonitored radiological releases from the turbine

building via the lubricating oil reservoir, and (2) the potential of the

instrument air system being contaminated and distributing contamination to the

control room, technical support center, and operations support center during

an accident.

The licensee explained that radioactive steam leakage into the turbine bearing

lubricating oil would be precluded by the design of the turbine seals,

bearings, and gland sealing system.

In order for the lubricating oil

reservoir to become contaminated, four barriers would have to fail and the

steam leakage rate would have to be significant.

This would attract the

attention of the operators, who coul<i take action such as shutting down the

turbine.

In addition, there was not a pathway by which the air in the

,

i

reservoir could be discharged into the turbine building, based on Flow

Diagram 12210-FSK-16-38.

The engineering evaluation approached the instrument air issues from a normal

operation and an accident perspective.

During normal operation, contamination

was not a problem because of the delay time involved in any radionuclides

,

traveling from the air compressor intakes to the points of release.

'

During design basis accident conditions, the worst case being a main steamline

break in the steam tunnel and assuming that the instrument air compressors

picked up all of the activity, the highest exposure would be 6 Rem for the

i

30-day thyroid iodine dose.

The evaluation concluded that if 100 percent of

the radioactive material followed the rupture disk pathway to the control room

l

intakes, the 30-day thyroid iodine dose would be 15.3 Rem to the operators,

with 23 Rem to the technical support center personnel.

The operations support

!

center could be evacuated, as delineated in the emergency implementation

procedures.

These values were within the 30 Rem allowable dose stated in

l

10 CFR Part 100.

The inspector concluded that the licensee's evaluation adequately addressed

the potential release paths.

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6.3 Conclusions

e

The licensee evaluation of the certification of a test engineer and test

I

practices was appropriate and reasonably supported,

l

The licensee adequately evaluated potential unmonitored release paths at

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River Bend Station.

7 ONSITE REVIEW 0F A LICENSEE EVENT REPORTS (92700)

7.1

(Closed) Licensee Event Report 458/92-004:

Increased Surveillance (Per

Technical Specification 4.0.5) Missed for Standb_y Service Water Pumps due

to Procedural Deficiency

This licensee event report involved five instances where the licensee failed

to test one control building chilled water pump and three standby service

!

I

water pumps at an increased frequency as required by Technical

l

Specification 4.0.5, and ASME Code,Section XI, IWP-3230(a).

Each pump was

j

determined to be in the alert range as defined in the ASME Code.

The licensee

demonstrated that each of the pumps were capable of performing their intended

safety functions.

Therefore, there was minimal safety significance to this

issue.

The root cause was determined to be an ambiguity which existed on the

licensee's Surveiliaiice Test Scheduling Completion / Exception Form.

When a

I

pump was tested and found to be in the alert range, and it was already on an

increased frequency schedule, the form required the user to indicate that no

frequency change was required.

This was misconstrued by the scheduling

personnel to mean the normal frequency and, as a result, the next test was

l

scheduled at the normal frequency instead of at an increased frequency.

,

l

The licensee changed the above referenced form to explicitly state whether or

I

not the components were in the alert range, leaving no doubt what the next

text frequency should be.

The inspectors reviewed the change to the form,

which was Enclosure 3 to Administrative Procedure ADM-0015, Revision 13,

" Station Surveillance Test Program." The change appeared adequate to prevent

l

future problems of this nature.

7.2 Conclusions

e

Licensee Event Report 92-004 was a good quality report and the

licensee's corrective actions appeared to be adequate to prevent

,

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recurrence.

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ATTACHMENT 1

1

PERSONS CONTACTED

1.1

Licensee Personnel

0. L. Andrews, Director, Quality Assurance

R. E. Barnes, Supervisor, Maintenance Engineering

P.. E. Cole, Supervisor, Control Process Systems

J. W. Cook, Senior Technical Specialist

T. C. Crouse, Manager, Administration

W. L. Curran, Cajun Site Representative

P. E. Freehill, Assistant Plant Manager - Outage Management

E. L. Glass,' Supervisor, Instrument & Control

W. C. Hardy, Radiation Protection, Supervisor

V. F. Klco, Principal Engineer - NSAG

I. M. Malik, Supervisor, Operations Quality Assurance

C. R. Maxson, Senior Compliance Analyst

.

C. L. Miller, Supervisor, Maintenance Support

W. H. Odell, Manager, Oversight

S. R. Radebaugh, APM - Maintenance

B. R. Smith, Mechanical Maintenance Supervisor

M. A. Stein, Director, Design Engineering

W. J. Trudell, Assistant Operations Supervisor

1.2 Other Personnel Contacted

The personnel listed above attended the exit meeting.

In addition to the

personnel listed above, the inspectors contacted other personnel during this

inspection period.

2 EXIT MEETING

An exit meeting was conducted on December 22, 1992.

During this. meeting, the

inspectors reviewed the scope and findings of the report. The licensee did

not identify as proprietary any information provided to, or reviewed by, the

inspectors.

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