ENS 45460: Difference between revisions

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| event date = 10/23/2009 16:34 EDT
| event date = 10/23/2009 16:34 EDT
| last update date = 10/23/2009
| last update date = 10/23/2009
| title = Plant Shutdown Due To Excess Letdown Heat Exchanger Tube Leak And After-The-Fact Unusual Event
| title = Plant Shutdown Due to Excess Letdown Heat Exchanger Tube Leak and After-The-Fact Unusual Event
| event text = On 10/23/09 at 1633, North Anna Unit 1 was placing Excess Letdown in service per 1-OP-8.5 due to a small unquantifiable throughwall leak on 1-CH-TV-1204B.  At 1634 [the licensee] entered action of TS 3.4.13 due to what appears to be an Excess Letdown Heat Exchanger tube leak.  The Component Cooling Water Head Tank [level] increased from 59% to 79% and the VCT [Volume Control Tank] level dropped 20 % indicating approximately 260 gallons of RCS had flowed into the Component Cooling Water System.  At 1638 Excess Letdown was removed from service and the leak was terminated.  At 1718 [the licensee] commenced ramping Unit 1 from service [TS Required Shutdown] to comply with TS 3.6.1, 'Containment Integrity' due to the throughwall leak on 1-CH-TV-1204B.
| event text = On 10/23/09 at 1633, North Anna Unit 1 was placing Excess Letdown in service per 1-OP-8.5 due to a small unquantifiable throughwall leak on 1-CH-TV-1204B.  At 1634 [the licensee] entered action of TS 3.4.13 due to what appears to be an Excess Letdown Heat Exchanger tube leak.  The Component Cooling Water Head Tank [level] increased from 59% to 79% and the VCT [Volume Control Tank] level dropped 20 % indicating approximately 260 gallons of RCS had flowed into the Component Cooling Water System.  At 1638 Excess Letdown was removed from service and the leak was terminated.  At 1718 [the licensee] commenced ramping Unit 1 from service [TS Required Shutdown] to comply with TS 3.6.1, 'Containment Integrity' due to the throughwall leak on 1-CH-TV-1204B.
The licensee has placed the normal letdown system back in service while the plant is being shut down.  The throughwall leak on 1-CH-TV-1204B is relatively small and unquantifiable compare to the tube leak on the excess letdown heat exchanger.  The licensee plans to proceed to Mode 5 to repair both the Letdown valve and the Excess Letdown Heat Exchanger tube leak.
The licensee has placed the normal letdown system back in service while the plant is being shut down.  The throughwall leak on 1-CH-TV-1204B is relatively small and unquantifiable compare to the tube leak on the excess letdown heat exchanger.  The licensee plans to proceed to Mode 5 to repair both the Letdown valve and the Excess Letdown Heat Exchanger tube leak.

Latest revision as of 22:10, 1 March 2018

ENS 45460 +/-
Where
North Anna Dominion icon.png
Virginia (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

Other Unspec Reqmnt
Time - Person (Reporting Time:+-3 h-0.125 days <br />-0.0179 weeks <br />-0.00411 months <br />)
Opened: Robert Counts
17:34 Oct 23, 2009
NRC Officer: Bill Huffman
Last Updated: Oct 23, 2009
45460 - NRC Website
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