ENS 45460
ENS Event | |
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20:34 Oct 23, 2009 | |
Title | Plant Shutdown Due to Excess Letdown Heat Exchanger Tube Leak and After-The-Fact Unusual Event |
Event Description | On 10/23/09 at 1633, North Anna Unit 1 was placing Excess Letdown in service per 1-OP-8.5 due to a small unquantifiable throughwall leak on 1-CH-TV-1204B. At 1634 [the licensee] entered action of TS 3.4.13 due to what appears to be an Excess Letdown Heat Exchanger tube leak. The Component Cooling Water Head Tank [level] increased from 59% to 79% and the VCT [Volume Control Tank] level dropped 20 % indicating approximately 260 gallons of RCS had flowed into the Component Cooling Water System. At 1638 Excess Letdown was removed from service and the leak was terminated. At 1718 [the licensee] commenced ramping Unit 1 from service [TS Required Shutdown] to comply with TS 3.6.1, 'Containment Integrity' due to the throughwall leak on 1-CH-TV-1204B.
The licensee has placed the normal letdown system back in service while the plant is being shut down. The throughwall leak on 1-CH-TV-1204B is relatively small and unquantifiable compare to the tube leak on the excess letdown heat exchanger. The licensee plans to proceed to Mode 5 to repair both the Letdown valve and the Excess Letdown Heat Exchanger tube leak. The licensee will notify the NRC Resident Inspector.
The licensee determined that it exceeded EAL SU6.1, Unidentified or Pressure Boundary Leakage greater than 10 gpm, for 4 minutes but currently does not meet the EAL Criteria. This requires the licensee to make a 1-hour notification that it has classified the event after-the-fact as an unusual event but did not actually declare the unusual event . The licensee will notify the NRC Resident Inspector and has notified the Virginia Department of Emergency Management. |
Where | |
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North Anna Virginia (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Other Unspec Reqmnt | |
Time - Person (Reporting Time:+-3 h-0.125 days <br />-0.0179 weeks <br />-0.00411 months <br />) | |
Opened: | Robert Counts 17:34 Oct 23, 2009 |
NRC Officer: | Bill Huffman |
Last Updated: | Oct 23, 2009 |
45460 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 546522020-04-09T05:00:0009 April 2020 05:00:00
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