ENS 45888: Difference between revisions
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| event date = 04/30/2010 16:48 CDT | | event date = 04/30/2010 16:48 CDT | ||
| last update date = 06/29/2010 | | last update date = 06/29/2010 | ||
| title = Light Socket Short Causes Isolation Systems | | title = Light Socket Short Causes Isolation Systems to Actuate | ||
| event text = At 1648 CDT, while the Control Bay AUO [Auxiliary Unit Operator] was attempting to change a light bulb for 1-IL-99-1AA, 1A [Reactor Protection System] RPS [Motor Generator] MG Set available light, the light socket shorted causing the loss of 1A RPS. The loss of 1A RPS resulted in Groups 2, 3, 6, and 8 primary containment isolations and initiated Standby Gas Treatment and Control Room Emergency Ventilation. All systems responded as designed. The Control Room operators entered the appropriate abnormal operating instruction, 1-AOI-99-1, to restore the affected systems. Operations entered TS LCO 3.3.1.1 conditions A.1 (place channel in Trip in 12 hours) and C.1 (restore RPS trip capability in 1 hr). At 1734 CDT, Operations exited TS LCO 3.3.1.1 upon restoration of 1A RPS per 1-AOI-99-1. | | event text = At 1648 CDT, while the Control Bay AUO [Auxiliary Unit Operator] was attempting to change a light bulb for 1-IL-99-1AA, 1A [Reactor Protection System] RPS [Motor Generator] MG Set available light, the light socket shorted causing the loss of 1A RPS. The loss of 1A RPS resulted in Groups 2, 3, 6, and 8 primary containment isolations and initiated Standby Gas Treatment and Control Room Emergency Ventilation. All systems responded as designed. The Control Room operators entered the appropriate abnormal operating instruction, 1-AOI-99-1, to restore the affected systems. Operations entered TS LCO 3.3.1.1 conditions A.1 (place channel in Trip in 12 hours) and C.1 (restore RPS trip capability in 1 hr). At 1734 CDT, Operations exited TS LCO 3.3.1.1 upon restoration of 1A RPS per 1-AOI-99-1. | ||
This event is reportable within 8 hours per 10CFR 50.72(b)(3)(iv)(A) 'Any event or condition that results in a valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) [b. General Containment Isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs)], except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' This event also requires an LER within 60 days per 10CFR 50.73(a)(2)(iv)(A). | This event is reportable within 8 hours per 10CFR 50.72(b)(3)(iv)(A) 'Any event or condition that results in a valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) [b. General Containment Isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs)], except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' This event also requires an LER within 60 days per 10CFR 50.73(a)(2)(iv)(A). |
Latest revision as of 21:09, 1 March 2018
Where | |
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Browns Ferry Alabama (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+0.72 h0.03 days <br />0.00429 weeks <br />9.86256e-4 months <br />) | |
Opened: | Tim Taylor 22:31 Apr 30, 2010 |
NRC Officer: | Pete Snyder |
Last Updated: | Jun 29, 2010 |
45888 - NRC Website
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