ENS 46874: Difference between revisions

From kanterella
Jump to navigation Jump to search
Created page by program invented by Mark Hawes
 
Created page by program invented by StriderTol
 
Line 17: Line 17:
| event date = 05/22/2011 14:44 EDT
| event date = 05/22/2011 14:44 EDT
| last update date = 06/07/2011
| last update date = 06/07/2011
| title = Safe Shutdown Operability Concern Associated With Offsite Power Circuits
| title = Safe Shutdown Operability Concern Associated with Offsite Power Circuits
| event text = On May 22, 2011, at 1444 hours, the Fermi 2 Control Room was notified by the Central System Supervisor that the switchyard voltage for both the 345kV (Division II) and 120kV (Division I) offsite power circuits following a generator trip would not be sufficient to sustain operability of the safety-related loads. Technical Specification (TS) 3.8.1 'AC-Sources Operating,' Condition E was entered at 1444 hours. At 1535, both offsite power circuit voltages were at acceptable levels and the offsite circuits were declared operable. Technical Specification (TS) 3.8.1, Condition E was exited at 1535 hours. Abnormal Operating Procedure (AOP) 20.300 GRID was entered. The Emergency Diesel Generators (EDG) remained operable during the degraded voltage condition. The ability of the EDGs to fulfill their design function was not affected by this condition.
| event text = On May 22, 2011, at 1444 hours, the Fermi 2 Control Room was notified by the Central System Supervisor that the switchyard voltage for both the 345kV (Division II) and 120kV (Division I) offsite power circuits following a generator trip would not be sufficient to sustain operability of the safety-related loads. Technical Specification (TS) 3.8.1 'AC-Sources Operating,' Condition E was entered at 1444 hours. At 1535, both offsite power circuit voltages were at acceptable levels and the offsite circuits were declared operable. Technical Specification (TS) 3.8.1, Condition E was exited at 1535 hours. Abnormal Operating Procedure (AOP) 20.300 GRID was entered. The Emergency Diesel Generators (EDG) remained operable during the degraded voltage condition. The ability of the EDGs to fulfill their design function was not affected by this condition.
The event is being reported per 50.72(b)(3)(V)(A), as any event or condition that at the time of discovery could have prevented fulfillment of the safety function of structures or systems that are needed to shutdown the reactor and maintain it in a safe shutdown condition.
The event is being reported per 50.72(b)(3)(V)(A), as any event or condition that at the time of discovery could have prevented fulfillment of the safety function of structures or systems that are needed to shutdown the reactor and maintain it in a safe shutdown condition.

Latest revision as of 21:06, 1 March 2018

ENS 46874 +/- *RETRACTED*
Where
Fermi 
Michigan (NRC Region 3)
Reporting
10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
Time - Person (Reporting Time:+22.32 h0.93 days <br />0.133 weeks <br />0.0306 months <br />)
Opened: Jim Konrad
17:03 May 23, 2011
NRC Officer: Joe O'Hara
Last Updated: Jun 7, 2011
46874 - NRC Website
Loading map...